N740CA

CESSNA 402C · 1980 · Valid Registration

Registered owner: HYANNIS AIR SERVICE INC, MA (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
HYANNIS AIR SERVICE INC. (HYIA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

S · 2022-03-15 Matched by certificate designator
ATA 6114

PILOT REPORTED THE LEFT PROPELLER CONTROL WAS UNRESPONSIVE AT CLIMB OUT AND PERFORMED AN AIR RETURN. COMPANY MAINTENANCE INSPECTED THE LEFT PROPELLER AND FOUND CRACKS IN THE PROPELLER HUB AT ALL 3 BLADE SOCKET LOCATIONS. AT BLADE 1 LOCATION THE CRACK IS APPROXIMATELY 75% OF CIRCUMFERENCE. AT BLADE 2 LOCATION CRACK IS APPROXIMATELY 50% OF CIRCUMFERENCE. AT BLADE 3 LOCATION CRACK IS JUST VISIBLE AND LESS THAT 1 INCH. THE PROPELLER HAS BEEN REMOVED FOR TEAR DOWN EVALUATION BY MCCAULEY SERVICE CENTER. OPERATOR HAS INSTITUTED A FLEET WIDE DETAILED VISUAL INSPECTION.

Source: SDR HYIA20220316001 · FAA SDRS
B · 2021-03-09 Matched by certificate designator
ATA 2297

THE PILOT REPORTED A BURNING SMELL AFTER THE AUTOPILOT CB POPPED DURING FLIGHT. MAINTENANCE INSPECTED AND FOUND CHAFFED WIRING AT THE PTT SWITCH. THE WIRES WERE REPAIRED WITH NO FURTHER DEFECTS NOTED.

Source: SDR HYIA20210311002 · FAA SDRS
O · 2018-12-14 Matched by certificate designator
ATA 7603

PILOT REPORTED RIGHT ENGINE THROTTLE STUCK AT 35 INCHES MAP. THE ENGINE WAS SHUT DOWN AND THE AIRCRAFT RETURNED TO THE FIELD WITHOUT INCIDENT. INSPECTION FOUND THE RIGHT THROTTLE CABLE PROPERLY ATTACHED AT BOTH ENDS, AND THE CABLE FAILED INTERNALLY. THE CABLE WAS REPLACED WITH NO FURTHER DEFECT NOTED.

Source: SDR HYIA20181218002 · FAA SDRS
O · 2018-09-04 Matched by certificate designator
ATA 5310

WHILE CONDUCTING OTHER MAINTENANCE, AN AREA OF CORROSION WAS NOTED ON THE FUSELAGE FRAME ASSEMBLY AT FS 214.00, JUST ABOVE THE 501110-12 STRIKER PLATE FOR THE LOWER PASSENGER DOOR PIN. THE 501110-12 STRIKER PLATE WAS REMOVED FOR FURTHER INSPECTION. UPON REMOVAL OF THE STRIKER PLATE, MORE CORROSION WAS DISCOVERED. THIS AREA OF CORROSION WAS MEASURED AT 2.12 HIGH BY .77 WIDE, WITH A DEPTH OF .058. THE FUSELAGE FRAME AND STRIKER PLATE WILL BE REPLACED WITH FACTORY NEW PARTS.

Source: SDR HYIA20180906001 · FAA SDRS
O · 2018-08-27 Matched by certificate designator
ATA 5410

DURING MAINTENANCE, CHAFING DAMAGE WAS FOUND ON THE RIGHT NACELLE CROSSOVER BEAM.

Source: SDR HYIA20180827001 · FAA SDRS
O · 2018-08-27 Matched by certificate designator
ATA 5415

DURING MAINTENANCE, CORROSION WAS FOUND ON THE UPPER SURFACE OF THE RIGHT NACELLE OUTBOARD FITTING, AROUND THE FASTENER HOLES OF THE TOP FORWARD FACE OF THE FITTING, JUST FORWARD OF THE FIREWALL. THE DEPTH OF THIS CORROSION IS .019 IN. THE FITTING WAS REPLACED.

Source: SDR HYIA20180827002 · FAA SDRS
R J · 2017-09-07 Matched by certificate designator
ATA 8530

CREW REPORTED ENGINE ROUGHNESS IN FLIGHT AT POWER REDUCTION FOR CRUISE AND MIXTURE FULL RICH. THE ACFT LANDED SAFELY AT ITS INTENDED DESTINATION WITH NO ISSUE. INSPECTION DISCOVERED LOW DIFFERENTIAL COMPRESSION CHECK RESULT AT CYLINDER NR 4 OF THE LT ENGINE. A BORESCOPE INSPECTION WAS PERFORMED. THE VALVE DOES NOT APPEAR TO EXHIBIT THE COMMON GREEN COLOR INDICATING HEAT DAMAGE. DIFFERENTIAL COMPRESSION CHECK AND BORESCOPE INSPECTION PERFORMED IAW M-O MANUAL. UPON REMOVAL OF THE ROCKER BOX COVER TO FACILITATE REPLACEMENT OF THE CYLINDER, THE EXHAUST VALVE ROTOCOIL WAS FOUND TO BE SEVERELY DAMAGED.

Source: SDR HYIA09092017001 · FAA SDRS
E · 2017-08-23 Matched by certificate designator
ATA 8530

CREW REPORTED A STRONG VIBRATION FROM RT ENGINE AS MIXTURE WAS REDUCED BELOW 100 PPH. THE CREW ENRICHED THE MIXTURE AND ELECTED TO DIVERT TO KHYA AS A PRECAUTION. INSPECTION DISCOVERED LOW DIFFERENTIAL COMPRESSION, 0 PSI/80PSI, AT CYLINDER POSITION NUMBER 1 OF THE RT ENGINE. A BORESCOPE INSPECTION WAS PERFORMED AND EXHAUST VALVE FACE EXHIBITED CLASSIC SIGNS OF OVERHEATING. THERE IS ALSO EVIDENCE OF EXHAUST VALVE SEAT RECESSION. IMAGES OF EXHAUST VALVE AND SEAT WILL BE PROVIDED AS A SUPPLEMENT TO THIS RECORD TO ILLUSTRATE DAMAGE. DIFFERENTIAL COMPRESSION CHECK AND BORESCOPE PROCEDURES WERE PERFORMED IN ACCORDANCE WITH THE LATEST REVISION OF CMI M-0 MANUAL. THESE INSPECTION PROCEDURES WERE LAST PERMED 34.2 FLIGHT HOURS PRIOR TO THIS EVENT. THIS CYLINDER WAS PURCHASED NEW AND HAS ACCUMULATED 1110.3 HOURS OF OPERATION IN 13 MONTHS. THE INTAKE AND EXHAUST LIFTER ASSOCIATED WITH THIS CYLINDER WERE REPLACED AS A PRECAUTION.

Source: SDR HYIA20170826001 · FAA SDRS
B · 2017-07-15 Matched by certificate designator
ATA 3442

PILOT REPORTED SMELL OF SMOKE IN COCKPIT UPON ACTIVATION OF WEATHER RADAR. MAINTENANCE INSPECTED AND DETERMINED TO BE DUE TO FAULTY INDICATOR. SYSTEM WAS PLACED ON MEL.

Source: SDR HYIA20170718001 · FAA SDRS
O · 2016-08-22 Matched by certificate designator
ATA 8530

CYLINDER REMOVED DUE TO LOW COMPRESSION AT INSPECTION. EXHAUST VALVE DISPLAYS EVIDENCE OF HEAT DAMAGE.

Source: SDR HYIA20160825096 · FAA SDRS
O · 2016-08-22 Matched by certificate designator
ATA 8530

CYLINDER REMOVED DUE TO LOW COMPRESSION AT INSPECTION; EXHAUST VALVE DISPLAYS EVIDENCE OF HEAT DAMAGE.

Source: SDR HYIA20160825094 · FAA SDRS
O · 2016-08-22 Matched by certificate designator
ATA 8530

CYLINDER REMOVED DUE TO LOW COMPRESSION AT INSPECTION, EXHAUST VALVE DISPLAYS EVIDENCE OF HEAT DAMAGE.

Source: SDR HYIA20160825095 · FAA SDRS
O · 2016-06-30 Matched by certificate designator
ATA 6120

PILOT REPORTED LT PROP LEVER DOES NOT CONTROL RPM, LT PROP WILL NOT FEATHER. MAINTENANCE INSPECTED AND FOUND THE LT PROPELLER GOVERNOR CONTROL CABLE BRACKET ATTACH CLAMPS TO BE LOOSE. MAINTENANCE ADJUSTED AND SECURED LT PROP GOVERNOR CABLE BRACKET IAW AMM CH 61.

Source: SDR HYIA20160706001 · FAA SDRS
O · 2015-10-16 Matched by certificate designator
ATA 2750

PILOT REPORTED ON APPROACH, WHEN FLAPS DEPLOYED TO 30 DEGREES THE ACFT ROLLED AGGRESSIVELY TO THE RIGHT. INSPECTED & FOUND THE RT FLAP OTBD FLAP ROD SEVERED. R & R THE FLAP ROD, OPERATIONALLY CHECKED GOOD.

Source: SDR HYIA20151019001 · FAA SDRS
J · 2015-09-30 Matched by certificate designator
ATA 6122

PILOT REPORTED RT PROPELLER OVERSPEED INDICATION ON CLIMB OUT, THEN DIFFICULTY CONTROLLING THE PROPELLER AT A STEADY RPM AFTER THAT POINT. R & R THE RT ENG PROPELLER GOVERNOR, OPERATIONAL & LEAK CHECKED GOOD WITH NO FURTHER DEFECTS AT THAT TIME.

Source: SDR HYIA20151002001 · FAA SDRS
O · 2015-06-21 Matched by certificate designator
ATA 5730

PILOT REPORTED WING LOCKER LT SIDE OPENED IN FLIGHT. INSPECTED LATCH OF LT WING LOCKER WITH NO DEFECTS FOUND. REMOVED LATCH COVER, INSPECTED ALL PINS & RODS, INSPECTED HINGES, INSPECTED SAFETY LATCH WITH NO DEFECTS FOUND.

Source: SDR HYIA20150624003 · FAA SDRS
O · 2015-05-09 Matched by certificate designator
ATA 5720

LT WING LOCKER OPENED IN FLIGHT. INSPECTED & SECURED THE LT WING LOCKER LATCH. OPERATIONALLY CHECKED GOOD.

Source: SDR HYIA20150515001 · FAA SDRS
O · 2015-04-20 Matched by certificate designator
ATA 3240

THE LT BRAKE STUCK & THE RT BRAKE FAILURE DURING TAXI. VISUALLY CHECKED THE RT BRAKE, SERVICED MASTER CYLINDER & BLED BRAKE SYS. REPLACED LT BRAKE CALIPER & SERVICED BRAKE SYS. BOTH SIDES OPERATIONALLY CHECKED GOOD.

Source: SDR HYIA20150428001 · FAA SDRS
B · 2015-03-08 Matched by certificate designator
ATA 3442

PILOT REPORTED A FAINT SMELL AFTER WEATHER RADAR STOPPED WORKING INFLIGHT. THE CB DID NOT POP. R & R WEATHER RADAR INDICATOR & TRANSCEIVER ANTENNA WITH NO FURTHER SMELLS NOTED.

Source: SDR HYIA20150312001 · FAA SDRS
O · 2012-12-28 Matched by certificate designator
ATA 3230

AT SCHEDULED INSPECTION, NLG DRAG BRACE, PN 5142002-5 WAS FOUND TO BE CRACKED IN THE AREA OF NLG ACTUATOR ATTACH POINT. METHOD OF INSPECTION WAS DYE PENETRANT. THIS CRACK WAS FOUND TO BE BEYOND LIMIT ALLOWABLE OF MEB91-11R1. THIS UNIT HAS BEEN SCRAPPED & A REPLACEMENT DRAG BRACE HAS BEEN INSTALLED IN ACFT.

Source: SDR HYIA20140414042 · FAA SDRS