N742MA

PITTS S-1T · 1982 · Valid Registration

Registered owner: OBE AVIATION LLC, PA (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

Acc · 2025-09-02 Unresolved
PITTS S-1T None injury Part 91operator not yet resolved Not yet finalized — may be revised.
Source: NTSB case ERA25LA381

Maintenance disclosures

Service Difficulty Reports filed with the FAA for this airframe. Filing is largely voluntary — the number of reports is not a measure of reliability. To verify a report, search its control number at the FAA SDRS site.

28 reports on file, 2009-01-01 – 2012-07-11.

OTHER · 2012-07-11 Unresolved
ATA 5230

Part: SKIN — DENTED (CARGO DOOR) · corrosion level 2 · airframe 28,272 hrs · 11,682 cycles

DURING PHASE INSPECTION, FOUND SEVERAL DENTS IN AFT CARGO DOOR SKIN. REPLACED AFT CARGO DOOR SKIN IAW DRAWING 146A6110 AND SRM 51-40-02.

Source: SDR MYWA07112012742
FALSE WARNING · 2012-05-01 Unresolved
ATA 2162

Part: WARNING SYSTEM — FALSE ACTIVATION (COCKPIT) · airframe 28,141 hrs · 11,610 cycles

ETOPS SIGNIFICANT SYSTEM: FLT DECK ZONE TEMP LIGHT COMES ON ON RECALL. RESETS WITH MASTER CAUTION.

Source: SDR MYWA120054
WARNING INDICATION · 2012-04-29 Unresolved
ATA 2162

Part: WARNING SYSTEM — ACTIVATED (COCKPIT) · airframe 28,134 hrs · 11,606 cycles

ETOPS SIGNIFICANT SYSTEM: CONTROL CAB ZONE TEMP LIGHT ILLUMINATED ON RECALL DURING DESCENT. PERFORMED ZONE TEMP CONTROL BITE TEST, FOUND FLT DECK LIGHT ILLUMINATED, CLEARS THE FAULT AND OPS CHECK OK IAW AMM 21-61-00.

Source: SDR MYWA120053
FALSE WARNING · 2012-04-25 Unresolved
ATA 2162

Part: WARNING SYSTEM — FALSE ACTIVATION (COCKPIT) · airframe 28,131 hrs · 11,604 cycles

ETOPS SIGNIFICANT SYSTEM: CONT CAB ZONE TEMP LIGHT ILLUMINATED DURING RECALL ON DESCENT. ACCOMPLISHED BITE TEST ON BOTH ZONE TEMP CONTROLLERS IAW FIM TASK 21-62 TASK 801 NO FAULTS NOTED. OPS CHECK NORMAL. ZONE TEMP LIGHTS ARE EXTINGUISHED DURING RECALL.

Source: SDR MYWA120052
FLUID LOSS · 2012-02-09 Unresolved
ATA 7320

Part: TUBE — DAMAGED (FUEL SYSTEM) · airframe 27,779 hrs · 11,426 cycles

ETOPS SIGNIFICANT SYSTEM: DURING HMU OPS CHECK FOUND TUBE ON OIL FUEL SERVO TO FUEL PUMP LEAKING. ON T/S FOUND TUBE AND FITTING NICKED. REMOVED AND REPLACED TUBE & FITTING BETWEEN OIL FUEL SERVO & FUEL PUMP IAW AMM 73-11-01 AND LEAK CHECK GOOD IAW AMM 71-00-00 TEST 3A-IDLE POWER.

Source: SDR MYWA120019
FLUID LOSS · 2012-02-07 Unresolved
ATA 7320

Part: HMU — LEAKING (NR 2 ENGINE) · airframe 27,779 hrs · 11,426 cycles

ETOPS SIGNIFICANT SYSTEM: FOUND NR 2 ENGINE LEAKING FUEL FROM HMU LOWER PLATE. REMOVED AND REPLACED NR 2 ENGINE HMU PER B737-800 AMM 73-21-10 PENDING OPS/LEAK CHECK SEE ITEM 12 LOG PAGE 237890, OPS CHECK GOOD IAW AMM 71-00-00, TEST 3A - IDLE POWER.

Source: SDR MYWA120018
OTHER · 2012-02-04 Unresolved
ATA 3610

Part: VALVE — STUCK (BLEED AIR SYS) · airframe 27,774 hrs · 11,423 cycles

ETOPS SIGNIFICANT SYSTEM: ON WALKAROUND, WITH APU BLEED ON, LOUD AIR NOISE COMING FROM NR 2 ENGINE INTERNAL. T/S AND FOUND HIGH STAGE VALVE STUCK OPEN, REMOVED HSV AS PER AMM 36-11-03. INSTALLED HIGH STAGE VALVE ON NR 2 ENGINE IAW B737-800 M/M 36-11-06, OPS CHECK NORMAL.

Source: SDR MYWA120017
OTHER · 2012-02-01 Unresolved
ATA 3610

Part: SHUTOFF VALVE — FAULTY (BLEED AIR SYS) · airframe 27,754 hrs · 11,413 cycles

ETOPS SIGNIFICANT SYSTEM: ON TS NR 2 ENGINE COWL ANTI-ICE VALVE, FOUND PRSOV "NOT" MOVING SMOOTHLY TO THE OPEN AND CLOSED POSITION. REMOVED AND REPLACED PRSOV VALVE ON NR 2 ENGINE AND OPS LEAK CHECK OK IAW AMM 36-11-04.

Source: SDR MYWA120016001
OTHER · 2012-02-01 Unresolved
ATA 3020

Part: ANTI-ICE VALVE — MALFUNCTIONED (NR 2 ENGINE) · airframe 27,754 hrs · 11,413 cycles

ETOPS SIGNIFICANT SYSTEM: ON WALKAROUND NOTICED SOUND OF AIR LEAK NR 2 INLET, FOUND OUTBOARD COWL A/I VALVE PARTIALY OPEN. SECURED VALVE CLOSED. REMOVED AND REPLACED ENG COWL TAI VALVE. OPS CHECK OK AND LEAK CHECK OK IAW AMM 30-21-11.

Source: SDR MYWA120015
Earlier reports · 2009–2011 · 19 reports

2011

OTHER · 2011-12-28 Unresolved
ATA 8011

Part: STARTER — FAULTY (NR 2 ENGINE) · airframe 27,650 hrs · 11,347 cycles

ETOPS SIGNIFICANT SYSTEM: ENG NR 2 WON`T START N2 10 PERCENT. REMOVED AND REPLACED NR 2 ENG STARTER IAW B737-800 AMM 80-11-01 OPS CHECKS GOOD WHILE TESTING THE NR 2 STARTER THE START VALVE FAILED HAD TO MANUALLY OPEN VALVE TO TEST STARTER.

Source: SDR MYWA110142
OTHER · 2011-12-28 Unresolved
ATA 8012

Part: START VALVE — MALFUNCTIONED (NR 2 ENGINE) · airframe 27,650 hrs · 11,347 cycles

ETOPS SIGNIFICANT SYSTEM: NR 2 ENG START VALVE FAILED WHILE TESTING THE STARTER. REMOVED AND REPLACED NR 2 ENG START VALVE IAW B737-800 AMM 80-11-03, OPS CHECK AND LEAK CHECKS GOOD.

Source: SDR MYWA110143
WARNING INDICATION · 2011-12-21 Unresolved
ATA 7530

Part: WARNING SYSTEM — ACTIVATED (COCKPIT) · airframe 27,636 hrs · 11,336 cycles

ETOPS SIGNIFICANT SYSTEM: WHILE PERFORMING PT ITEM 14 FMC FAULT CHECK FOUND LEFT ENGINE LONG TIME MESSAGE 75-10391 "VSV POSITION SIGNAL OUT OF RANGE".

Source: SDR MYWA110135
WARNING INDICATION · 2011-12-17 Unresolved
ATA 3610

Part: PRECOOLER — DEFECTIVE (BLEED AIR SYS) · airframe 27,625 hrs · 11,330 cycles

ETOPS SIGNIFICANT SYSTEM: LEFT ENG BLEED TRIPPED JUST BEFORE TOP OF CRUISE. ACCOMPLISHED HEALTH CHECK ON NR 1 ENGINE IAW B737-800 M/M 36-11-00 FOUND PRECOOLER VALVE AT FAULT REMOVED AND REPLACED NR 1 ENGINE PRECOOLER VALVE IAW B737-800 M/M 36-12-02, OPS CHECK NORMAL.

Source: SDR MYWA110131
VIBRATION/BUFFET · 2011-12-17 Unresolved
ATA 7200

Part: ENGINE — VIBRATION (NR 1) · airframe 27,625 hrs · 11,330 cycles

ETOPS SIGNIFICANT SYSTEM: NR 1 ENG VIBRATION ERRATIC FROM OFF BACK LOW TO OFF SCALE HIGH. NO VIBRATION NOTED BY CREW.

Source: SDR MYWA110134
WARNING INDICATION · 2011-12-17 Unresolved
ATA 3610

Part: VALVE — FAULTY (BLEED AIR SYS) · airframe 27,625 hrs · 11,330 cycles

ETOPS SIGNIFICANT SYSTEM: LEFT ENG BLEED TRIPPED JUST BEFORE TOP OF CRUISE. ACCOMPLISHED HEALTH CHECK ON NR 1 ENGINE IAW B737-800 M/M 36-11-00 FOUND PRECOOLER VALVE AT FAULT REMOVED AND REPLACED NR 1 ENGINE PRECOOLER VALVE IAW B737-800 M/M 36-12-02, OPS CHECK NORMAL.

Source: SDR MYWA110132
WARNING INDICATION · 2011-02-28 Unresolved
ATA 3097

Part: WIRE HARNESS — DAMAGED (ENGINE) · airframe 26,370 hrs · 10,657 cycles

ETOPS SIGNIFICANT SYSTEM: RIGHT SIDE WINDOW HEAT OVERHEAT LIGHT ILLUMINATED ON CLIMBOUT. FOLLOWED ABNORMAL PROCEDURES. LIGHT RE-ILLUMINATED. TURNED OFF. REMOVED AND REPLACED WIRE HARNESS MW0326 ON NR 2 ENG IAW AMM 26-11-02. OPS CHECKED GOOD.

Source: SDR MYWA110027

2010

WARNING INDICATION · 2010-09-03 Unresolved
ATA 4920

Part: APU — SHUTDOWN (APU BAY) · airframe 25,525 hrs · 10,293 cycles

ETOPS SIGNIFICANT SYSTEM: MULTIPLE OCCURRENCES OF APU SHUTDOWN.

Source: SDR MYWA100105
WARNING INDICATION · 2010-08-26 Unresolved
ATA 4900

Part: WARNING LIGHT — ILLUMINATED (APU FAULT) · airframe 25,504 hrs · 10,283 cycles

ETOPS SIGNIFICANT SYS: INFLIGHT APU FAULT LIGHT ON WITH APU AUTO SHUTDOWN.

Source: SDR MYWA100094R
WARNING INDICATION · 2010-08-17 Unresolved
ATA 4920

Part: APU — SHUTDOWN · airframe 25,420 hrs · 10,263 cycles

ETOPS SIGNIFICANT SYS: IN FLIGHT, APU FAULT LIGHT AND AUTO SHUTDOWN.

Source: SDR MYWA100094
FLUID LOSS · 2010-05-10 Unresolved
ATA 2782

Part: ACTUATOR — LEAKING (KRUEGER FLAP) · airframe 24,849 hrs · 10,048 cycles

ETOPS SIGNIFICANT SYSTEM - ON WALK AROUND, FOUND NR 4 KRUEGER FLAP ACTUATOR LEAKING.

Source: SDR MYWA100075
OTHER · 2010-02-10 Unresolved
ATA 5210

Part: DOOR — LEAKING (L1) · airframe 24,442 hrs · 9,866 cycles

ETOPS SIGNIFICANT SYSTEM - L1 DOOR PRESSURE LEAK ON CLIMBOUT.

Source: SDR MYWA100033
OTHER · 2010-02-02 Unresolved
ATA 5210

Part: SEAL — NOT SEATED (L1 DOOR) · airframe 24,440 hrs · 9,864 cycles

L1 DOOR PRESSURE AIR LEAK ON CLIMBOUT. OPENED & CLOSED L1 DOOR SEVERAL TIMES. OPS CHECK GOOD IAW AMM 52-10-00. GRD PRESSURE CHECKS GOOD IAW AMM 21-31-00

Source: SDR MYWA100002
WARNING INDICATION · 2010-01-05 Unresolved
ATA 2822

Part: PUMP — FAULTED (FUEL SYSTEM) · airframe 24,324 hrs · 9,809 cycles

ETOPS SIGNIFICANT SYSTEM - TRANSFERRED FROM DMI CONTROL 7018, "LT CENTER FUEL TANK PUMP INOP".

Source: SDR MYWA100006

2009

WARNING INDICATION · 2009-12-11 Unresolved
ATA 7397

Part: CONNECTOR — DIRTY (EEC) · airframe 24,226 hrs · 9,758 cycles

ETOPS SIGNIFICANT SYSTEM - NR 1 ENGINE EEC FAULT CODE DISPLAYED DURING BITE TEST.

Source: SDR MYWA09069
WARNING INDICATION · 2009-12-10 Unresolved
ATA 3150

Part: WARNING SYSTEM — ACTIVATED (COCKPIT) · airframe 24,220 hrs · 9,755 cycles

ETOPS SIGNIFICANT SYSTEM - ON DESCENT INTO MIA PRESSED RE-CALL AND THE "MACH TRIM" LIGHT ILLUMINATED.

Source: SDR MYWA09067
OTHER · 2009-12-05 Unresolved
ATA 4950

Part: BLEED VALVE — DEFECTIVE (APU) · airframe 24,207 hrs · 9,747 cycles

ETOPS SIGNIFICANT SYSTEM - APU DUCT PRESSURE INSUFFICIENT TO START ENGINE.

Source: SDR MYWA09066
OTHER · 2009-12-02 Unresolved
ATA 2312

Part: RADIO — INOPERATIVE (VHF COMM) · airframe 24,194 hrs · 9,739 cycles

ETOPS SIGNIFICANT SYSTEM - NR 2 VHF INOP CAPT'S AND F/O'S POSITION.

Source: SDR MYWA09065
FLT CONT AFFECTED · 2009-01-01 Unresolved
ATA 2740

Part: TRIM MOTOR — INOPERATIVE (STABILIZER) · airframe 22,790 hrs · 9,125 cycles

STAB TRIM FAIL AFTER TAKEOFF. ACFT RETURNED TO BLOCK. MX CLEANED AND INSPECTED CONNECTOR PLUG TO STAB TRIM MOTOR. OPS CHECK GOOD, RETURN TO SERVICE. ACFT ARRIVED, UPON TAXI, STAB TRIM FAILED. MX REMOVED AND REPLACED STAB TRIM MOTOR. ACFT HAS FLOWN WITH NO MORE DISCREPANCIES.

Source: SDR MYWA090101