N742WA

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

E M · 2016-11-03 Matched by certificate designator
ATA 7250

ON CLIMB OUT DEPARTING KMIA NR 2 ENGINE EXPERIENCED HIGH EGT, THROTTLE RETARDED , MINUTES LATER LOUD NOISE WAS HEARD, EGT CLIMBED TO 777 DEGREES CELSIUS AND ENGINE SHUT DOWN PROCEDURE WAS ACCOMPLISHED, FUEL WAS DUMPED AND RTB KMIA. AFTER PARKING FOUND EXCESSIVE TURBINE BLADE DAMAGE.

Source: SDR 2016F00216 · FAA SDRS
O · 2016-10-24 Unresolved
ATA 2565

INADVERTENT SLIDE/RAFT DEPLOYMENT.

Source: SDR WRLA201610240001 · FAA SDRS
R · 2015-10-28 Matched by certificate designator
ATA 7200

NR 1 ENGINE LOST POWER, ALL OF ITS PARAMETERS DISPLAYED IDLE ON ECIAS. POWER RECOVERED IMMEDIATELY. MINUTES LATER SAME ENGINE LOST POWER AGAIN DURING CLIMB OUT. ALL ENGINE PARAMETERS DISPLAYED IDLE ON ECIAS BUT THIS TIME POWER WAS NOT RECOVERED. ENGINE CHECKLIST PERFORMED BY CREW. ENGINE WAS SHUTDOWN IAW PROPER PROCEDURES. ACFT RETURNED TO DEPARTURE SAFELY.

Source: SDR WRNA201510290031 · FAA SDRS
R · 2015-10-28 Matched by certificate designator
ATA 7200

DEPARTING NR 1 ENG LOST POWER, ALL OF ITS PARAMETERS DISPLAYED IDLE ON ECIAS. POWER RECOVERED IMMEDIATELY, MINUTES LATER SAME ENGINE LOST POWER AGAIN DURING CLIMB OUT. ALL ENGINE DISPLAYED IDLE ON ECIAS BUT THIS TIME POWER WAS NOT RECOVERED. ENGINE CHECKLIST PERFORMED BY CREW. ENGINE WAS SHUTDOWN IAW PROPER PROCEDURES. ACFT RETURNED TO DEPARTURE SAFELY.

Source: SDR WRNA201511280001 · FAA SDRS
O · 2012-08-01 Unresolved
ATA 5730

MX HAS ADVISED THAT A CRACK APPROX 3 1/2 FEET IN LENGTH AND ANOTHER CRACK APPROX 8 INCHES IN LENGTH HAVE BEEN FOUND ON TOP OF THE RIGHT WING AFT OF THE LEADING EDGE. THE CRACKS ARE IN 2 SEPARATE PANELS.

Source: SDR WRLA20120801554 · FAA SDRS