N752FE

CESSNA 208B · 1990 · Valid Registration

Registered owner: FEDERAL EXPRESS CORPORATION, TN (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
CSA AIR, INC. (SBAA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

R · 2014-09-26 Matched by certificate designator
ATA 6122

AFTER LANDING, DURING TAXI PILOT PULLED POWER CONTROL AFT INTO BETA REVERSE RANGE TO SLOW HIS TAXI SPEED. WHEN BRINGING POWER CONTROL BACK FWD INTO FWD POWER RANGE HE NOTED A BINDING AT BETA REVERSE GATE. PILOT SHUT OWN ACFT & CONTACTED MX. INSPECTED POWER CONTROL RIGGING & SYS FOR PROBLEMS, NONE NOTED. ACFT WAS TEST RUN & OPERATED IN & OUT OF BETA REVERSE RANGE NUMEROUS TIMES. BINDING COMING OUT OF BETA REVERSE WAS NOTED ONE TIME ONLY. PROP GOVERNOR WAS REPLACED WITH OVERHAULED UNIT & RIGGED AS REQUIRED. ACFT WAS AGAIN TEST RUN & PUT IN & OUT OF BETA REVERSE MANY TIMES. POWER CONTROL OPERATED SMOOTHLY ALL THE TIME.

Source: SDR SBAA2014100600003 · FAA SDRS
O · 2013-02-06 Matched by certificate designator
ATA 5730

DURING VISUAL INSPECTION NOTICED THAT RIGHT WING INBOARD TKS PANEL WAS DEFORMED ALONG LEADING EDGE FROM WS.37.00 TO WS 51.00. UPON INSPECTION OF BACKSIDE OF LEADING EDGE FOUND THAT LEADING EDGE WAS PUSHED IN APPROX .50 INCHES DEEP AND .50 INCHES WIDE BETWEEN NOTED WING STATIONS. TKS SYSTEM WAS TESTED AND SEEMED TO OPERATE NORMALLY.

Source: SDR SBAA2013021100001 · FAA SDRS
O · 2011-01-05 Matched by certificate designator
ATA 3421

MFR / ABORTED TAKEOFF: NR 1 ATTITUDE INDICATOR FAILED ON TAKEOFF. PILOT ABORTED TAKEOFF AND LANDED AND RETURNED TO RAMP WITHOUT INCIDENT. MAINTENANCE REMOVED AND REPLACED FLIGHT COMMAND INDICATOR.

Source: SDR COEA2011010501752 · FAA SDRS
B · 2010-11-04 Matched by certificate designator
ATA 3610

FLT 8830 PDX TO MFR: DURING CLIMB, SMOKE AND ELECTRICAL ODOR APPEARED FROM PILOT SIDE CIRCUIT BREAKER PANEL. CREW DECLARED AN EMERGENCY AND LANDED IN EUG WITHOUT INCIDENT. MAINTENANCE INSPECTED CB, SWITCHES, RELAYS & WIRING FOR SIGNS OF BURNING. NO DISCREPANCIES NOTED. PERFORMED GROUND RUN OPERATIONAL CHECK WITH NO DEFECTS NOTED. AIRCRAFT RETURNED TO SERVICE. FLT 7662 FROM EUG TO PDX PILOT NOTED SIDE WINDOW PILLAR EXTREMELY HOT. MX REMOVED AND REPLACED BLEED AIR PRESSURE REGULATOR. PERFORMED GROUND RUN WITH NO DISCREPANCIES NOTED. AIRCRAFT RETURNED TO SERVICE.

Source: SDR COEA2010110401752 · FAA SDRS