N762JP

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
JET LINX AVIATION, LLC (9JLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

K · 2021-11-22 Matched by certificate designator
ATA 2820

THE FLIGHT CREW NOTED FUEL LEAKING FROM THE VENTRAL FUEL TANK AFTER LANDING. OPERATIONS WERE CONTINUED PER MEL 28-22-1-2. THE MAINTENANCE TEAM DISCOVERED THE REFUELING COUPLING CONNECTOR WAS AT FAULT FOR LEAK. THE O-RINGS ON THE PRESSURE REGULATING VALVE WAS REPLACED WITH NEW. OPS AND LEAK CHECKS WERE SATISFACTORY. THE AIRCRAFT WAS THEN RETURNED TO SERVICE

Source: SDR 9JLA2021120634618 · FAA SDRS
O · 2021-07-29 Matched by certificate designator
ATA 8097

THE FLIGHT CREW REPORTED THAT AFTER STARTING THE NO1 ENGINE THE NO2 ENGINE WOULD NOT START. NO1 ENGINE START SELECT DID NOT ILLUMINATE AND THERE WAS NO ENGINE ROTATION. THE MAINTENANCE VENDOR FOUND THE "B4" CIRCUIT BREAKER ON THE ZL PANEL FOR MAIN START CONTROL TRIPPED. REMOVED AND CLEANED CABLE TERMINALS ON NO1 STARTER TERMINAL BLOCK AND THE REINSTALLED AND TORQUED PER AMM. OPS CHECKS GOOD. AIRCRAFT RETURNED TO SERVICE.

Source: SDR 9JLA2021080227994 · FAA SDRS
J · 2021-04-12 Matched by certificate designator
ATA 3040

THE FLIGHT CREW REPORTED THAT DURING FLIGHT THE COPILOTS A WINDSCREEN DID NOT HEAT. THE MAINTENANCE TEAM DETERMINED THAT THE THERMAL CONTROLLER WAS DEFECTIVE. THE DEFECTIVE CONTROLLER WAS REMOVED AND A NEW UNIT WAS INSTALLED. OPERATIONAL CHECKS WERE SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021041627971 · FAA SDRS