N763MH

SIKORSKY S-76A · Valid Registration

Registered owner: GM LEASING CO LLC, LA (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
ROTORCRAFT LEASING COMPANY, L.L.C. (YTRA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

X J · 2024-01-24 Matched by certificate designator
ATA 7200

IN FLIGHT ENGINE SHUTDOWN.

Source: SDR YTRA2024012500001 · FAA SDRS
X · 2024-01-24 Matched by certificate designator
ATA 7250

IN FLIGHT ENGINE SHUTDOWN. ON TEARDOWN INSPECTION IT WAS DISCOVERED THAT THE 1ST STAGE TURBINE WHEEL BLADES HAD SEPARATED FORM THE BODY OF THE WHEEL. SEE BLOCK 6 BELOW FOR DETAILED INFORMATION ON WHEEL.

Source: SDR YTRA202402020001 · FAA SDRS
R J · 2021-09-04 Matched by certificate designator
ATA 7200

PILOT REPORTED THAT IN CRUISE FLIGHT THE T5 INDICATION HIGHER THAN THE #2 ENGINE AND THE ENGINE FAILED THE TREND CHECK.

Source: SDR YTRA2021090700001 · FAA SDRS
K J · 2020-02-19 Matched by certificate designator
ATA 2910

#2 SERVO SYSTEM LIGHT ILLUMINATED IN CRUISE FLIGHT. ON INSPECTION FOUND HYDRAULIC TUBE ASSEMBLY IN THE RIGHT HAND WHEEL WELL CRACKED AND LEAKING.

Source: SDR YTRA202002205101 · FAA SDRS
N · 2015-03-06 Matched by certificate designator
ATA 2611

BAGGAGE COMPARTMENT SMOKE DETECTOR CAUTION LIGHT CAME ON IN FLIGHT. ON INSPECTION NO SMOKE OR FIRE WAS NOTED.

Source: SDR YTRA20150316075 · FAA SDRS
K · 2005-02-12 Matched by certificate designator
ATA 7250

AFTER NORMAL LANDING AND SHUTDOWN AT HOSPITAL A LARGE PUDDLE OF OIL WAS FOUND UNDER THE AIRCRAFT. FURTHER INVESTIGATION SHOWED OIL COVERING NR 1 ENGINE DECK AND OIL QUANTITY WAS DOWN BY THREE QUARTS. OIL TEMP AND PRESS WERE NORMAL AT SHUTDOWN. THE LABYRINTH SEAL SUPPLY TUBE WAS FOUND TO BE CRACKED OFF FROM THE ESHAUST COLLECTOR FLANGE ADAPTER AND MISPLACED ABOUT HALF THE TUBE DIAMETER. THIS RESTRICTED AIR FLOW TO THE LAB SEAL ALLOWED OIL TO FLOW OVER THE LAB SEAL. TURBINE SECTION WAS WITHIN 30 CYCLES OF BEING REMOVED DUE TO TURBINE WHEEL CYCLES. MECHANIC ON DISASSEMBLY REPORTED THAT TUBE MAY HAVE BEEN ORIGINALLY TIGHTENED UNDER A TWISTING LOAD. TURBINE SECTION WAS REPLACED.

Source: SDR EGRA200501 · FAA SDRS