N777Z
Registered owner: DIEFENTHAL DOUGLAS C, IL (owner ≠ operator)
Operators of this aircraft
Who operated this tail, and how firmly we know it.
No operator established for this aircraft.
Accident & incident history
No NTSB accidents or incidents on file for this aircraft.
Maintenance disclosures
03/17/2019: AFTER CRUISING LEVEL AT FL380 FOR ABOUT 10 MINUTES, THERE WAS A LOUD THUD/THUMP HEARD IN THE AIRCRAFT. THOUGHT MAYBE A DOOR HAD COME OFF THE AIRCRAFT. A BULBS TEST SHOWED NO LOSS OF DOORS. PASSENGERS THOUGHT NOISE CAME FROM RT SIDE OF PLANE. NOT LONG AFTER, WE GOT AN INTERMITTENT GEAR WARNING HORN (2 SEPARATE TIMES). NOT LONG AFTER THE OIL 1 LIGHT BEGAN TO FLICKER ON AND OFF INTERMITTENTLY LIKE A STROBE. CHECK OF THE ENGINE 1 OIL PRESSURE SHOWED FLUCTUATIONS, SLOWLY DECREASING IN PRESSURE, BUT WITH NO CHANGE IN OIL TEMPERATURE, WHICH SEEMED UNCHARACTERISTICALLY LOW. THEN GOT A COMPUTER 1 LIGHT AND PROCEEDED TO ATTEMPT A COMPUTER RESET. ABOUT THE TIME I ATTEMPTED TO RE-SET THE COMPUTER, THERE WAS A LOUDER THUMP HEARD FOLLOWED BY A GRINDING NOISE. AT THIS POINT I SHUT DOWN THE NUMBER 1 ENGINE AND SECURED IT. ENGINE CONTINUED TO ROTATE FREELY AND DID NOT SEIZE. RAN ABNORMAL CHECKLIST. REQUESTED BLOCK ALTITUDE FROM ATC AND DRIFTED DOWN FROM FL380 TO FL340. ASKED ATC TO RELAY OUR SITUATION TO DISPATCH (AIRCRAFT WAS OUT OF WIRELESS INTERNET COVERAGE). PROCEEDED TO DESTINATION (KRSW) AND LANDED WITH ONE ENGINE INOP. DID NOT DECLARE EMERGENCY BUT REQUESTED FIRE TRUCKS BE STRANDING BY AND ALSO REQUESTED A LONG STRAIGHT IN ILS IN CASE THERE WAS UNKNOWN A/C DAMAGE. LANDED FLAPS 48, WITHOUT INCIDENT. 03/18/2018: MAINTENANCE ARRIVED AT THE AIRCRAFT. INSPECTED INSIDE OF COWLING AND FOUND OIL ALL OVER IN THE LOWER COWLING, DIFFICULT TO DETERMINE THE CAUSE. INSPECTED THE EXHAUST AND NOTICED METAL DEBRIS IN THE EXHAUST PIPE SECTION. UPON INSPECTING THE INLET AREA MAINTENANCE FOUND THE FAN ASSEMBLY WAS SEIZED AND WOULD NOT ROTATE. SCHEDULING ENGINE REMOVAL AND REPLACEMENT AT THIS TIME. "SUPPLEMENTAL INFORMATION" AFTER THE ENGINE IN QUESTION HAD BEEN REMOVED AND SHIPPED BACK TO OUR SHOP WE HAD THE LOCAL ENGINE SHOP BORESCOPE THE ENGINE TO SEE IF THEY COULD DETERMINE THE CAUSE OF THE ENGINE ISSUE. AFTER THEY REVIEWED THE BORESCOPE RESULTS THEY INFORMED US THEY BELIEVE ONE OF THE 2ND STAGE LOW PRESSURE TURBINE BLADES CAME LOOSE AND DAMAGED THE ENGINE.
THE CREW REPORTED WHEN DEPARTING FOR A PART 91 FLIGHT, THAT THEY EXPERIENCED A PMP3 FAILURE LIGHT FOLLOWED BY A TK P2 LIGHT ON CLIMB OUT. INDICATION SHOWED NO NR 2 HYDRAULIC SYSTEM PRESSURE OR QUANTITY. THE CREW COMPLETED THE ABNORMAL CHECKLIST AND CONTINUED ITS FLIGHT BUT DECIDED TO DIVERT DUE TO HAVING NO FLAP, SPEED BRAKE OR TILLER CONTROL. THE CREW REPORTED THE REST OF THE FLIGHT AND LANDING WERE UNEVENTFUL. UPON LANDING THE CREW OPENED THE REAR COMPARTMENT AND NOTICED HYDRAULIC FLUID THROUGHOUT THE REAR COMPARTMENT. MAINTENANCE ARRIVED AT THE AIRCRAFT AT APPROXIMATELY 1900 CST SHORTLY AFTER THE ACFT ARRIVED. THE REAR COMPARTMENT WAS INSPECTED AND IT WAS FOUND THAT A NR 2 SYSTEM HYDRAULIC LINE, PN; F50B751604 HAD BROKEN JUST AFT OF THE FITTING TO THE PRESSURE RELIEF VALVE. THE BROKEN HYDRAULIC LINE IS ATTACHED TO THE NR 2 HYDRAULIC SYSTEM PRESSURE RELIEF VALVE, PN: A24518001, SN: 277 AMDT "A".