N793DC

BEECH B200 · 1991 · Valid Registration

Registered owner: BILLINGS CLINIC, MT (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
LYNCH FLYING SERVICE INC (HSRA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2024-11-05 Matched by certificate designator
ATA 5610

AIRCRAFT WAS IN CRUISE FLIGHT AT 16,000 FT ENROUTE KBZN FROM KBIL WHEN THE RIGHT (COPILOT) WINDSHIELD SHATTERED. AT THAT TIME, THE FLIGHT CREW RETURNED TO KBIL AND LANDED WITHOUT INCIDENT.

Source: SDR 2024FA0000823 · FAA SDRS
K J · 2023-10-31 Matched by certificate designator
ATA 2910

WHILE ON APPROACH INTO BFI FROM BIL, THE LANDING GEAR EXTENDED UN-COMMANDED, THE LANDING GEAR HANDLE LIGHT (IN-TRANSIT LIGHT) ILLUMINATED, THE "HYD LOW" ANNUNCIATOR LIGHT ILLUMINATED AND THE LANDING GEAR CIRCUIT BREAKER POPPED. THE THREE GREEN "GEAR DOWN AND LOCKED" LIGHTS DID NOT ILLUMINATE. THE CREW PERFORMED A "GO-AROUND". THEY SELECTED THE LANDING GEAR HANDLE DOWN AND RESET THE LANDING GEAR CIRCUIT BREAKER BUT THE GEAR DID NOT EXTEND TO THE DOWN AND LOCKED POSITION. THE CB POPPED AGAIN AFTER 5 SECONDS. THE CREW THEN PERFORMED A MANUAL LANDING GEAR EXTENSION WHICH LOCKED ALL THREE GEAR DOWN AND THE THREE GREEN LIGHTS ILLUMINATED. THEY THEN LANDED AT BFI WITHOUT INCIDENT. DURING THE POST FLIGHT INSPECTION THE CREW DISCOVERED HYDRAULIC FLUID DRIPPING OUT OF THE RIGHT MAIN LANDING GEAR WELL. MAINTENANCE INSPECTED THE AIRCRAFT AND FOUND A HYDRAULIC LINE TO THE RIGHT MAIN LANDING GEAR ACTUATOR HAD RUPTURED AND THE LANDING GEAR HYDRAULIC RESERVOIR EMPTY.

Source: SDR 2023F00320 · FAA SDRS
J · 2022-12-17 Matched by certificate designator
ATA 7500

ON CLIMB OUT FROM KBIL THE FLIGHT CREW OBSERVED THE "LEFT BLEED FAIL" ANNUNCIATOR LIGHT ILLUMINATE. THEY RETURNED TO KBIL WITHOUT INCIDENT. MAINTENANCE REPLACED THE LEFT BLEED AIR PRESSURE SWITCH WITH A SERVICEABLE PRESSURE SWITCH AND THE SYSTEM OPS CHECKED GOOD. THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 2022F00525 · FAA SDRS
J · 2022-12-15 Matched by certificate designator
ATA 5210

ON CLIMB OUT FROM KBIL THE FLIGHT CREW NOTICED LOSS OF PRESSURIZATION. DESCENDED AND RETURNED TO KBIL WITHOUT INCIDENT. UPON INSPECTION, IT WAS DISCOVER THAT THE CABIN DOOR SEAL HAD A CUT IN IT. MAINTENANCE REPLACED THE CABIN DOOR SEAL AND RETURNED THE AIRCRAFT TO SERVICE.

Source: SDR 2022F00524 · FAA SDRS
J · 2010-06-25 Matched by certificate designator
ATA 3610

BLEED AIR FAIL WARNING LIGHT CAME ON IN FLIGHT. FOUND BLEED TUBE SPLIT.

Source: SDR HSRR13038 · FAA SDRS