N800UP

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
CIRCADIAN AVIATION LLC (O2GA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2021-04-01 Matched by certificate designator
ATA 2435

ENROUTE KHVN TO KRDU AT FL260 AN EICAS “R GEN TIE OPEN” ILLUMINATED. FOLLOWED THE CHECKLIST AND CLEARED EICAS. AFTER ABOUT 4 MINUTES “R GEN TIE OPEN” AGAIN ILLUMINATED FOLLOWED BY “R GEN” ANNUNCIATOR. THE ‘R GEN” EICAS L/R “FIRE” ILLUMINATED IN THE TORQUE GAUGES FOR ONLY A FEW MOMENTS THEN EXTINGUISHED, THERE WAS NO SECONDARY INDICATIONS OF FIRE. EMERGENCY WAS DECLARED AND DIVERTED TO KACY. LANDING WAS UNEVENTFUL. MAINTENANCE ISOLATED THE DISCREPANCY TO A RIGHT ENGINE STARTER GENERATOR ARMATURE FAILURE. SG WAS REPLACED. PERFORMED PWC ENGINE REQUIREMENTS FOR SG FAILURE. AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR O2GA2021040680001 · FAA SDRS
J · 2020-03-20 Matched by certificate designator
ATA 5750

ON APPROACH FLAPS WOULD NOT EXTEND PAST THE APPROACH POSITION. EMERGENCY DECLARED. LANDING WAS UNEVENTFUL. MAINTENANCE REPLACED THE RIGHT WING FLAP SAFETY SWITCH. OPERATIONAL CHECKED OKAY. AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR O2GA2020032380001 · FAA SDRS
F · 2017-11-16 Matched by certificate designator
ATA 2721

RUDDER TRIM FROZE DURING CRUISE FLIGHT. OPERATED NORMAL AT LOWER ALTITUDES. MAINTENANCE PERFORMED THE REQUIREMENTS OF NTO LETTER FOR TRIM ACTUATOR LUBE. OPS CHECK FLIGHT WAS UNSUCCESSFUL. AIRCRAFT DIVERTED. MAINTENANCE REPLACED THE RUDDER TRIM ACTUATOR.

Source: SDR O2GA2017112180001 · FAA SDRS
O · 2016-07-14 Matched by certificate designator
ATA 7200

DURING SCHEDULED ROUTINE RIGHT ENGINE MAINTENANCE BORESCOPE INSPECTION, REVEALED FOD DAMAGE. ENGINE WAS REMOVED AND REPLACED WITH A RENTAL UNIT. A SUCCESSFUL OPERATIONAL CHECK FLIGHT WAS PERFORMED. AIRCRAFT WAS RTS.

Source: SDR O2GA2016071880001 · FAA SDRS
B · 2015-07-03 Matched by certificate designator
ATA 2435

WHEN LT ENG START SWITCH WAS PLACED INTO, IGNITION & ENG START POSITION, NO N1 ROTATION WAS OBSERVED & VOLTAGE ON THE VOLTAGE SELECTOR DROPPED TO ZERO. APPROX THREE SECONDS INTO THE START SEQUENCE, SMOKE WAS OBSERVED BELLOWING OUT FROM TOP OF ENG COWL VENT. AN IMMEDIATE ENG SHUTDOWN SEQUENCE WAS INITIATED & ACFT WAS EVACUATED. CREW & PAXS EVACUATED THE ACFT WITHOUT INCIDENT. AFTER SHUTDOWN THERE WAS NO MORE SMOKE OBSERVED FROM ENG COWL. REPLACED THE LT STARTER GEN & A SUCCESSFUL OPERATIONAL CHECK WAS PERFORMED. ACFT WAS RETURNED TO SERVICE.

Source: SDR O2GA2015070680001 · FAA SDRS