N800WS

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
JET LINX AVIATION, LLC (9JLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2022-02-14 Matched by certificate designator
ATA 5755

THE FLIGHT CREW REPORTED DELAMINATION OF THE RIGHT SPEED BRAKE. THE MAINTENANCE VENDOR REMOVED THE DEFECTIVE SPOILER PANEL AND INSTALLED A SERVICEABLE PANEL. OPS CHECKS OK AND THE AIRCRAFT WAS RETURNED TO SERVICE. NOTE SPOILER PANEL WAS SPLIT ALONG FORWARD INBOARD EDGE FOR SEVERAL INCHES.

Source: SDR 9JLA2022042520045 · FAA SDRS
O · 2021-08-28 Matched by certificate designator
ATA 5610

THE FLIGHT CREW REPORTED THAT DURING CRUISE FLIGHT THE PILOTS SIDE WINDOW MADE A POPPING SOUND AND THEN THE OUTER PANE TO THE SIDE WINDOW CRACKED AND SHATTERED. THE FLIGHT CREW DECLARED AN EMERGENCY AND STARTED A DESCENT FOR LANDING. THE CREW SAID THEY HAD NO PRESSURIZATION ISSUES. THE LANDING WAS WITHOUT EVENT. NO CAUSE WAS FOUND THAT CAUSED THE WINDOW OUTER PANE TO FAIL. THE WINDOW WAS REMOVED AND A NEW WINDOW WAS INSTALLED. OPS CHECKS WERE SATISFACTORY AND THE AIRCRAFT WAS RETURN TO SERVICE.

Source: SDR 9JLA2021090220009 · FAA SDRS
J · 2021-05-10 Matched by certificate designator
ATA 2820

THE FLIGHT CREW REPORTED DURING FLIGHT AN AMBER CAS MESSAGE FUEL BOOST PUMP ON RH CAME ON AFTER TURNING FUEL TRANSFER FROM THE LEFT SIDE BACK TO OFF. THE MAINTENANCE VENDOR FOUND THE RIGHT HAND MOTIVE FLOW VALVE P/N 26430-05 S/N 0093 WAS DEFECTIVE. THE VALVE WAS REMOVED AND REPLACED WITH A REPAIRED UNIT. OPS AND LEAK CHECKS WERE SATISFACTORY. THE AIRCRAFT THEN WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021052525668 · FAA SDRS
J · 2021-05-10 Matched by certificate designator
ATA 3097

THE FLIGHT CREW REPORTED DURING FLIGHT RECEIVING AN AMBER ENGINE CONTROL FAULT RIGHT SIDE WHEN THE ANTI-ICE WAS TURNED ON. THE MAINTENANCE VENDOR TROUBLESHOT AND FOUND FAULT CODE VT ACTIVE. TROUBLESHOOTING WIRING AND FOUND CHANNEL B OTBD WING ANTI-ICE CIRCUIT RESISTANCE HIGH. CONNECTOR PE008 WAS REMOVED, THE PINS AND SOCKETS WERE CLEANED. REINSTALLED CONNECTOR. OPS CHECKS WERE SATISFACTORY. THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021052525667 · FAA SDRS
O · 2021-01-15 Matched by certificate designator
ATA 2722

THE FLIGHT CREW REPORTED THAT ON PREFLIGHT CHECKS THAT THE RUDDER BIAS CONTROLS FELT VERY WEAK ON BOTH SIDES. THE MAINTENANCE VENDOR TROUBLESHOT AND DETERMINED THAT THE RUDDER BIAS ACTUATOR WAS DEFECTIVE. THE RUDDER BIAS ACTUATOR WAS REMOVED AND REPLACED WITH AN OVERHAULED UNIT. OPERATIONAL CHECKS WERE SATISFACTORY. THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021020425650 · FAA SDRS
L · 2021-01-15 Matched by certificate designator
ATA 2720

THE FLIGHT CREW INDICATED DURING THE PREFLIGHT CHECKLIST THAT THE RUDDER BIAS SYSTEM FELT VERY WEAK DURING OPERATIONS. THE MAINTENANCE VENDOR VERIFIED THE DISCREPANCY AND REPLACED THE RUDDER BIAS ACTUATOR WITH AN OVERHAULED UNIT. OPERATIONAL CHECKS WERE SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021011825650 · FAA SDRS
J · 2021-01-08 Matched by certificate designator
ATA 3010

THE FLIGHT CREW REPORTED THAT IN FLIGHT RECEIVING A CAS MESSAGE INDICATING THAT THE LEFT WING ANTI-ICE SYSTEM FAILED. THE MAINTENANCE VENDOR TROUBLESHOT AND DETERMINED THE LEFT PYLON PRSOV (VD002) WAS DEFECTIVE. THE DEFECTIVE VALVE WAS REMOVED AND A SERVICEABLE CONDITION VALVE WAS INSTALLED. LEAK CHECK AND FUNCTIONAL CHECKS SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021020421049 · FAA SDRS
J · 2021-01-05 Matched by certificate designator
ATA 3610

THE FLIGHT CREW REPORTED IN FLIGHT THAT THE LEFT SIDE COLD AMBER ANTI-ICE INDICATION WITH ALL ANTI-ICE ON INFLIGHT. THE MAINTENANCE VENDOR TROUBLESHOT AND DETERMINED THE LEFT HIGH PRESSURE SHUTOFF VALVE WAS DEFECTIVE. THE PROSV VALVE WAS REPLACED WITH A INSPECTED PRSOV. LEAK AND OPERATIONS CHECKS, SATISFACTORY. THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021010821049 · FAA SDRS