N806DE

EMBRAER SA EMB-550 · 2016 · Valid Registration

Registered owner: DOUBLE EAGLE AVIATION II LLC, TX (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
EXECUTIVE FLIGHT SERVICES, LLC (E07A)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2019-09-20 Matched by certificate designator
ATA 3350

EMERGENCY LIGHTS STAYS ON IN ARM POSITION OR FLASHES ON/OFF IN ARM AND ON. REPLACED BATTERY PACK.

Source: SDR XMXR20191211024 · FAA SDRS
O · 2019-09-20 Matched by certificate designator
ATA 3350

EMERGENCY LIGHTS STAYS ON IN ARM POSITION OR FLASHES ON/OFF IN ARM AND ON. REPLACED BATTERY PACK.

Source: SDR XMXR20191211023 · FAA SDRS
O · 2018-05-18 Matched by certificate designator
ATA 3350

EMERGENCY LIGHTS FLASH ON AND OFF WHEN SYSTEM IN ARM POSITION. REPLACED THE BATTERY PACK.

Source: SDR E07A201805210003 · FAA SDRS
O · 2018-05-18 Matched by certificate designator
ATA 3350

EMERGENCY LIGHTS FLICKER ON AND OFF WITH SYSTEM IN ARM POSITION. REPLACED THE BATTERY PACK.

Source: SDR E07A201805210004 · FAA SDRS
X J · 2003-03-20 Matched by certificate designator
ATA 7200

AT 133 KNOTS THE NR 1 ENGINE SURGED WITH FLAME-OUT, THE FRONT AND BACK. INSPECTION IN THE FRONT AND BACK, LOOKS OK. DUE TO AD 2002-21-10, THIS IS A GROUP 3 TAKEOFF SURGE AND THE ENGINE WILL BE CHANGED.

Source: SDR DLM11030260 · FAA SDRS
B · 2003-03-08 Matched by certificate designator
ATA 5241

L2 DOOR SMELLS LIKE ELECTRICAL BURNING AND WILL NOT OPERATE ELECTRICALLY. REPLACED LOCK/RELEASE SOLENOID PER M/M. OPS GOOD. NO MORE BURNING SMELL.

Source: SDR DLM11030228 · FAA SDRS
B · 2002-11-23 Matched by certificate designator
ATA 2121

STRONG ELECTRICAL BURNING ODOR DURING DESCENT, JUST AFTER WINDSHIELD HEAT WAS TURNED ON. CREW DEACTIVATED WINDSHIELD HEAT, TURNED ECON OFF AND ISOLATED THE NR 1 PACK. FUMES DISSAPATED. CREW COULD HEAR MOTOR FAN THAT SOUNDED AS IF IT WAS BINDING. FUMES SEEM STRONGEST AROUND C/B PANEL. FOUND AVIONICS COOLING FAN NR 3 WITH C/B POPPED. REPLACED FAN. FAN OPS NORMAL. C/B REMAINS CLOSED.

Source: SDR DLM11021361 · FAA SDRS
J · 2002-11-02 Matched by certificate designator
ATA 3230

GEAR FAILED TO RETRACT ON FIRST ATTEMPT. SECOND ATTEMPT SUCCESSFULL. PERFORMED GEAR SWING TO DUPLICATE PROBLEM. SWUNG GEAR 4 TIMES. NO PROBLEMS NOTED. SYSTEM CHECKS GOOD. DURING GEAR SWING, FOUND LT GEAR OVERCENTER LOCK ACTUATOR LEAKING . R & R LT GEAR OVER CENTER LOCK ACTUATOR PER M/M.

Source: SDR DLM11021285 · FAA SDRS
O · 2002-06-19 Unresolved
ATA 2500

AT CRUISE FLT ATTDS INFORMED US THERE WAS A STRONG ELECTRICAL SMELL IN THE AFT GALLEY CHILLER #8 RED FAIL LIGHT WAS FLASHING. SHUT DOWN CHILLER #8 AND #7. GALLEY POWER WAS ALSO TURNED OFF. DIVERTED TO JFK. SMELL SEEMED TO DISSAPATE. CORR ACTION: FOUND NBR 7 CHILLER FAN GRINDING. CHECKED AREA OF CHILLERS NO EVIDENCE OF ELECT WIRING CHAFFED OR BURNT. CHECKED AFT COOLING FAN FOUND OK #8 CHILLER OPS NORMAL. RPLD #7 CHILLER. PERFORMED OVER WEIGHT LANDING INSPECTION PER M.M.

Source: SDR DLM11020687 · FAA SDRS
L · 2002-04-24 Unresolved
ATA 3350

ON PREFLIGHT, EMERGENCY LIGHT TEST FAIL. EMERGENCY LIGHT BATTERY 6 LO MSG ON. REPLACED EMERGENCY LIGHT BATTERY 6 PER M/M. EMERGENCY LIGHT TEST PASS.

Source: SDR DLM11020479 · FAA SDRS
B · 2001-08-18 Unresolved
ATA 2530

AFT GALLEY FWD OVEN GIVING OFF BURNING SMELL. REPLACED OVEN.

Source: SDR DLM11011359 · FAA SDRS
O · 2001-06-18 Unresolved
ATA 3241

NR 10 TIRE BLOWN ON LANDING. REPLACED NR 10 ANTISKID TRANSDUCER.

Source: SDR DLM11011004 · FAA SDRS
L · 2000-12-18 Unresolved
ATA 2611

IR-1330/18DEC/LAX/ 060558 - FRC-261-02208 LAV 4R SMOKE. DETECTOR BATTERY MISSING. CA-REPLACED DETECTOR BATTERY AT 4R. SMOKE DETETOR TESTS NML. MALF-4T0 POS-CN CTL-C12180302 SKILL-02

Source: SDR DLM11002472 · FAA SDRS
J · 2000-09-24 Unresolved
ATA 3610

AT TOP OF CLIMB GOT NR 2 MANIFOLD FAILURE. SYSTEM RESOLVED ITSELF. FOUND MANIFOLD FAIL COMPUTER BAD. REPLACED SAME.

Source: SDR DLM11001853 · FAA SDRS
N · 1999-10-27 Unresolved
ATA 3150

ATB AURAL WARNING WITH NO VISUAL CAUSE, UNABLE TO SILENCE HORN. REPLACED CAWS UNIT.

Source: SDR DLM11992378 · FAA SDRS
B · 1999-09-01 Unresolved
ATA 3840

PAX AT 3B NOTICED A HOT WIRE SMELL. THE CREW ALSO NOTICED THE SMELL. LATER F/A AND PASSENGER COMPLAINED OF HEADACHES INSPECTED CEILING FWD CABIN FOR BURNING WIRE CK OK. CHECKED SIDEWALL OF FWD CRAGO COMP FOUND NR 1 WATER COMP BEARING FAILURE. REPLACED NR 1 WATER COMP. CKS GOOD.

Source: SDR DLM11991947 · FAA SDRS
B P · 1999-07-10 Unresolved
ATA 2611

THERE WAS A SMALL FIRE OR SMOLDER IN 4R LAV TRASH BIN, IT WAS PUT OUT PROMPTLY BY THE FLIGHT ATTENDANT. NO DAMAGE VISABLE IN CAN. THE SMOKE ALARM DID NOT GO OFF. TESTED SMOKE DETECTOR ON ARRIVAL, CHECKED OK. NO EVIDENCE OF FIRE OR BURNED MATERIAL. TRASH COMPARTMENT AND CONTAINER IN SERVICABLE CONDITION. REPLACED SMOKE DETECTOR PRECAUTIONARY.

Source: SDR DLM11991551 · FAA SDRS
B · 1999-06-28 Unresolved
ATA 2330

ODOR DETECTED IN AREA OF MONITOR 40J. MONITOR HAD BEEN FLICKERING, NO PICTURE. POWER REMOVED FROM MONITOR, ODOR DISAPPEARED. REPLACED MONITOR AND POWER SUPPLY.

Source: SDR DLM11991462 · FAA SDRS
L · 1998-12-26 Unresolved
ATA 3350

FWD CABIN EMERGENCY LIGHT INOP. REMOVED AND REPLACED N01 BATTERY PACK IN THE NR 1 BATTERY POWER SUPPLY, GRD OPS CK OK.

Source: SDR DLM11982631 · FAA SDRS
K · 1998-05-13 Unresolved
ATA 3510

IN CRUISE, FOUND CREW 02 BOTTLE EMPTY. FOUND FLEX LINE TO OBSERVER 02 REGULATOR LEAKING BADLY. REPLACED LINE AND REPLACED 02 BOTTLE. LEAK CK GOOD.

Source: SDR DLM11981027 · FAA SDRS
O · 1997-07-19 Unresolved
ATA 2622

FIRE EXTINGUISHER BOTTLE AT 4L LOW PRESS. REPL BOTTLE.

Source: SDR DLM11971415 · FAA SDRS
O · 1997-05-08 Unresolved
ATA 5330

THE RT FUSELAGE SKIN SURROUNDING THE FWD AND AFT LAV VACUUM WASTE AIR EXHAUST PORTS WERE FOUND CORRODED ON THE OUTER SURFACE AROUND THE AFT EDGES OF THE PORT CUTOUTS AT FS 1937 AND 1959 RESPECTIVELY. THE CORROSION BLEND OUT ON THE FWD PORT HOLE REQUIRED A MAX DEPTH OF 0.016. THE AFT PORT HOLE REQUIRED THAT THE SKIN BE CUTOUT IN THE DAMAGED AREA. FS 1937 - 0.063 EXT 2024-T3 REPAIR DOUBLER; FS 1956 - 0.071 2024-T3 EXT DOUBLER; GENERAL - 2 INTERNAL FINGER DOUBLERS - SEAL AND TREAT.

Source: SDR DLM11970935 · FAA SDRS
F · 1997-01-21 Unresolved
ATA 2540

WITH A/P ON, WHEN FLIGHT SPOILERS WERE EXTENDED TO FULL, THE AIRCRAFT ROLLED LEFT TOWARD 30 DEGREE BANK. SPOILERS DON'T APPEAR TO EXTEND AT 1/3 AND 2/3 POSITION. AILERON TRIM WAS JAMMED DURING APPROACH, WILL NOT MOVE FROM ZERO POSITION. GROUND SPOILERS DID NOT EXTEND ON LANDING. FOUND ICE BUILDUP IN RIGHT WHEEL WELL IN AREA OF CONTROL CABLES. WATER LEAK FROM LAV -M ABOVE. REPLACED WATER FAUCET IN LAV-M.

Source: SDR DLM11970116 · FAA SDRS
L · 1996-11-24 Unresolved
ATA 3350

EMERGENCY LIGHT SYSTEM FAULTED BATTERY PACK NR 3 AND NR 6.

Source: SDR DLM11962581 · FAA SDRS
O · 1996-11-24 Unresolved
ATA 3350

EMERGENCY LIGHT SYSTEM FAULTS BATTERY PACK NR 3 AND NR 6.

Source: SDR DLM11962580 · FAA SDRS
O · 1996-05-09 Unresolved
ATA 7230

ON TAKEOFF LOUD BANG LEFT SIDE, VIBRATION, ABORTED T/O. A/C REPORTED SMOKE AND FIRE, FIRED NR 1 AGENT BOTTLE. SHUTDOWN PER CHECKLIST. FOUND COMPRESSOR HAD FAILED, METAL IN TAILPIPE AND BELOW 2.5 BLEED OPENING. MTC IN PROGRESS.

Source: SDR DLM11961115 · FAA SDRS
N Y · 1996-05-09 Unresolved
ATA 7200

NR 1 ENGINE FAILED DURING T/O RUN. LOUD BANG FROM LEFT SIDE OF A/C HEARD, T/O ABORTED AT 50 KNOTS. A/C REPORTED SMOKE AND FIRE. BLEW NR 1 FIRE BOTTLE AND SHUT DOWN ENGINE. NO EVIDENCE OF FIRE FOUND DURING INSPECTION. CHANGED ENGINE, METAL FOUND IN BLEED VALVE.

Source: SDR DLM11961124 · FAA SDRS
J · 1996-04-10 Unresolved
ATA 2210

BOTH A/P INOP, NO CURRENT FAULTS. ACFT RETURNED ATL. PERFORMED RTS ON BOTH FCC, ALL NORMAL.

Source: SDR DLM11960834 · FAA SDRS
Y · 1996-04-06 Unresolved
ATA 7200

AFTER TAKEOFF AT 2,600 FT AND 270 KIAS, NR 2 ENGINE FAILED. A/C SHUDDERED, RPM ROLLED BACK AND TEMP WENT TO 754, FIRED EXT AGENT FOR NR 2 ENG. FLIGHT RETURNED TO LAX WHERE MAINTENANCE FOUND METAL IN TAIL PIPE. REPLACED ENGINE AND ROUTED TO SHOP.

Source: SDR DLM11960781 · FAA SDRS
L · 1995-12-17 Unresolved
ATA 3350

FAILED EMER LIGHT TEST MSC EMER LIGHT BAT 2 LOW. REPLACED EMER LIGHT BAT 2, OPS CKS OK.

Source: SDR DLM11954721 · FAA SDRS