N808JH

MD HELICOPTERS INC 369E · 2008 · Valid Registration

Registered owner: TREELINE HELICOPTERS INC, TN (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
JACK HARTER HELICOPTERS, INC. (DCGA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2025-09-08 Matched by certificate designator
ATA 6410

DURING A POST FLIGHT MAINTENANCE INSPECTION A SMALL DENT WAS DISCOVERED ON THE OUTBOARD FACE OF ONE OF THE AIRCRAFT TAIL ROTOR BLADES. PILOT REPORTED THERE WAS NO INDICATIONS OR NOISE OF ANYTHING STRIKING THE BLADE. THE BLADE DENT WAS FOUND TO BE WITHIN SERVICEABLE LIMITS. TAIL GEARBOX, HORIZONTAL AND VERTICAL FINS, TAILBOOM, AND DRIVSHAFTS AND COUPLINGS INSPECTED PER MDHI SPECIAL INSPECTIONS SECTION. NO DAMAGE NOTED. AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR DCGA202509100629 · FAA SDRS
O · 2023-08-16 Matched by certificate designator
ATA 5313

DURING A POST FLIGHT INSPECTION, THE MECHANIC FOUND A CRACK ON THE AFT END OF THE RIGHT-HAND STATION 174 DOUBLER CONNECTING THE BOOM FAIRING AND TURTLE BACK OF THE UPPER AFT FUSELAGE.

Source: SDR 2023FA0000430 · FAA SDRS
K · 2019-10-14 Matched by certificate designator
ATA 7321

DURING MAINTENANCE GROUND RUN CHECK OPERATIONS ENGINE FUEL WAS NOTICED COMING OUT OF THE FUEL CONTROL CASE AND LEAKING TO THE GROUND. FUEL CONTROL WAS REMOVED FOR INVESTIGATION AND A SERVICABLE UNIT INSTALLED.

Source: SDR 2019FA0000338 · FAA SDRS
O · 2019-08-29 Matched by certificate designator
ATA 2810

FUEL LEAKING FROM LEFT HAND FUEL BLADDER. REPLACED BOTH LEFT AND RIGHT HAND BLADDERS.

Source: SDR 2019FA0000291 · FAA SDRS
J · 2019-06-25 Matched by certificate designator
ATA 7100

ENGINE CHIP LIGHT ILLUMINATED WHEN ENGINE WAS BROUGHT TO FLIGHT IDLE AFTER ENGINE START UP. MAINTENANCE FOUND 2 FLAKES WITHIN LIMITS ON THE UPPER CHIP PLUG.A 30 MINUTE GROUND RUN WAS PERFORMED, THE PLUGS WERE INSPECTED AGAIN AND FOUND CLEAN. AIRCRAFT RETURNED TO SERVICE.

Source: SDR 2019FA0000194 · FAA SDRS
O · 2019-03-18 Matched by certificate designator
ATA 6210

THE BOTTOM SKIN OF THE MAIN ROTOR BLADE HAS A 4 1/2 INCH CRACK STATING AT THE TRAILING EDGE AND PERPENDICULAR TO SPAN 57 1/4 INCHES IN FOR BLADE TIP.

Source: SDR 2019FA0000075 · FAA SDRS
J · 2018-10-01 Matched by certificate designator
ATA 6320

DURING A POST MAINTENANCE OPERATIONAL CHECK FLIGHT THE MAIN ROTOR GEARBOX CHIP LIGHT ILLUMINATED. A PIECE OF METAL WAS FOUND ON THE CHIP PLUG. THE TRANSMISSION WAS REMOVED AND A SERVICABLE TRANSMISSION WAS INSTALLED.

Source: SDR DCGA2018FA0000398 · FAA SDRS
O · 2016-04-18 Matched by certificate designator
ATA 6210

DURING ROUTINE MAINTENANCE APROXIMATELY 1" INBD FROM THE TIP ON THE TOP OF THE MAIN ROTOR BLADE, PN 500P2100-105, SN 907B A .5" X .5" DELAMINATION WAS FOUND ON THE STAINLESS STEEL L/E OF THE BLADE. THE BLADE WAS REMOVED FROME THE ACFT AT THIS TIME.

Source: SDR 2016FA0000182 · FAA SDRS
J · 2015-12-03 Matched by certificate designator
ATA 7200

PILOT GOT AN INTERMITTENT ENGINE CHIP LIGHT INDICATION AFTER TAKEOFF AND RETURNED FOR LANDING. MAINTENANCE FOUND LIGHT EXTINGUISHED BUT FOUND METAL ON UPPER AND LOWER ENGINE CHIP PLUGS. ENGINE WAS REMOVED FROM THE ACFT FOR FURTHER INSPECTION.

Source: SDR DCGA2015FA0000622 · FAA SDRS
E · 2015-11-22 Matched by certificate designator
ATA 6210

DURING A MAINTENANCE GROUND RUN OPERATION A HIGH LATERAL VIBRATION WAS ENCOUNTERED AND THE ACFT WAS SHUTDOWN. IT WAS DISCOVERED THAT WATER HAD ENTERED THE BLADE DURING A HEAVY RAINFALL THE NIGHT BEFORE. ATTEMPTS TO REMOVE THE WATER WERE UNSUCCESSFUL AND THE BLADE WAS REMOVED FROM THE ACFT FOR EVALUATION.

Source: SDR 2015FA0000613 · FAA SDRS
J · 2015-10-29 Matched by certificate designator
ATA 7200

ENGINE CHIP LIGHT ILLUMINATED DURING TOUR FLIGHT. THE PILOT LANDED ACFT AND CALLED MAINTENANCE. MAINTENACE FOUND METAL FLAKE MEASURING LESS THAN .03125 ON UPPER AND LOWER ENGINE CHIP PLUGS. AFTER CLEANING THE PLUGS A 30 MINUTE GROUND RUN WAS PERFORMED AND THE PLUGS WERE RECHECKED AND FOUND CLEAN. THE ACFT WAS RETURNED TO SERVICE.

Source: SDR DCGA2015FA0000520 · FAA SDRS
J · 2015-07-05 Matched by certificate designator
ATA 6440

PILOT RECIEVED A TAIL GEARBOX DIM CHIP LIGHT IN FLIGHT. THE PILOT PERFORMED AN UNEVENTFUL UNSCHEDULED LANDING AND CALLED MAINTENANCE. THE MECHANIC EXAMINED THE GEARBOX CHIP DETECTOR AND FOUND IT CLEAN. THE MECHANIC REPLACED AN INTERNALLY SHORTING CHIP DETECTOR. OPERATION AND LEAK CHECKS WERE PERFORMED AND RESULTS WERE NORMAL

Source: SDR 2015FA0000313 · FAA SDRS
O · 2015-05-19 Matched by certificate designator
ATA 7250

PILOT REPORTED CHIRPING NOISE FROM ENGINE AT END OF DAY SHUTDOWN. MAINTENANCE REMOVED TURBINE ASSY FOR SUSPECT N2 RUBBING.

Source: SDR DCGA2015FA0000217 · FAA SDRS
N · 2014-04-23 Matched by certificate designator
ATA 7797

PILOT REPORTED AN ENGINE CHIP LIGHT. THE CHIP LIGHT WAS EXTINGUISHED WHEN CHIP PLUGS WERE REMOVED AND CLEANED. DURING OPS CHECKS THE LIGHT CAME BACK ON. MAINTENANCE ULTIMATELY DISCOVERED A SHORTING WIRE IN THE LOWER ENGINE CHIP DETECTOR CONNECTOR. THE BAD PORTION OF WIRE WAS REMOVED AND BOTH UPPER AND LOWER CHIP DETECTOR CONNECTORS WERE REPLACED.

Source: SDR DCGA2014042500280 · FAA SDRS
E · 2010-07-28 Matched by certificate designator
ATA 6220

PILOT EXPERIENCED IN FLIGHT STICK SHAKE AND UNUSUAL VIBRATION. MX SUSPECTS PROBLEM WITH DROOP RING AND FOLLOWERS ON MAIN ROTOR HUB ASSY.

Source: SDR 2010FA0000772 · FAA SDRS