N810MH

EUROCOPTER EC 130 B4 · Valid Registration

Registered owner: AIRSTAR LEASING LLC, NV (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
ALEXAIR INC. (X33A)Certificate holderMatched by certificate designator

Accident & incident history

Accident · 2007-11-15 Unresolved
Eurocopter France EC 130 B4 None injuryoperator not yet resolved
Source: NTSB case SEA08CA027

Maintenance disclosures

O · 2008-11-17 Matched by certificate designator
ATA 5302

DURING ROUTINE 500 HOUR INSPECTION A CRACK WAS FOUND RADIATING FROM AN ATTACHMENT FITTING SCREW BORE TO THE EDGE OF THE SPAR. A NEW SPAR WAS MATCH DRILLED AND INSTALLED IAW EUROCOPTER REPAIR SCHEME.

Source: SDR M7KA1031083949 · FAA SDRS
O · 2008-11-17 Matched by certificate designator
ATA 6220

DURING ROUTINE INSPECTION 1 OF 3 FREQUENCY ADAPTERS FOUND TO HAVE A CRACK IN THE ELASTOMER NEARING ITS MAXIMUM ALLOWABLE LIMITATION OF 10MM. A NEW KIT OF 3 MATCHED ADAPTERS WERE INSTALLED.

Source: SDR M7KA1026083949 · FAA SDRS
O · 2008-06-12 Matched by certificate designator
ATA 6220

DURING ROUTINE INSPECTION WITH ROTOR HEAD SLEEVE ASSY REMOVED ONE OF THE STAR ARM END BUSHINGS WAS FOUND TO TURN SLIGHTLY WITH HAND PRESSURE APPLIED. THE STARFLEX WAS REMOVED FOR REPAIR OF BONDING DEFECT. THIS IS A COMMON FAILURE FOR THIS PART. THE MFG CLAIMS TO HAVE A REPAIR FOR THIS DEFECT BUT OFFERS ONLY AN EXCHANGE ASSY. SUGGEST A NEW ADHESIVE SYS OR PART DESIGN BE TRIED TO REDUCE THIS TYPE OF DEFECT FOR AN EXPENSIVE PART. A SLIPPAGE MARK PAINTED ACROSS THE EDGE OF THE BUSHING AND ONTO THE STAR ADHESIVE BEAD HELPS IN DETECTION OF THIS DEFECT WHILE IN SERVICE BY INDICATING THE BUSHING HAS TURNED. (K)

Source: SDR M7K2008F00041 · FAA SDRS
K · 2008-06-12 Matched by certificate designator
ATA 7261

DURING ROUTINE INSPECTION EXCESSIVE OIL LEAKAGE WAS NOTED AT THE MODULE 5 OUTPUT MAGNETIC SEAL. CLOSE INSPECTION OF THE REMOVED SEAL REVEALED NO OBVIOUS DEFECT. A NEW SEAL WAS INSTALLED WITH NO FURTHER LEAKAGE NOTED. (K)

Source: SDR M7K2008F00034 · FAA SDRS
O · 2008-05-12 Matched by certificate designator
ATA 6510

(REF 0421083949) THE TAIL ROTOR DRIVE FREE WHEEL ASSEMBLY OUTPUT SHAFT SEAL OF MODULE 5 BEGAN TO WEEP AND PROGRESSIVELY THE WEEP BECAME A LEAK. A NEW SEAL WAS INSTALLED AND NO FURTHER LEAKAGE WAS NOTED. (K)

Source: SDR M7K2008F00006 · FAA SDRS
O · 2008-03-03 Matched by certificate designator
ATA 6700

PILOT REPORTED THAT WHEN ADJUSTING POWER FOR CRUISE FLIGHT THE ENGINE HAD FLUCTUATIONS WHEN PASSING THROUGH A CERTAIN COLLECTIVE POSITION THAT WERE REPEATABLE IF SELECTING THE POSITION IN QUESTION. UPON SHUTDOWN A FAULT CODE WAS GENERATED INDICATING THE COLLECTIVE POTENTIOMETER WAS FAULTY. A NEW POTENTIOMETER WAS INSTALLED AND NO FURTHER DEFECT NOTED. THIS IS A VERY COMMON FAULT FOR THIS PART THAT EFFECTS THIS MODEL AIRCRAFTS DISPATCH RELIABILITY. (K)

Source: SDR M7K2008F00108 · FAA SDRS
O · 2008-01-08 Matched by certificate designator
ATA 7320

PILOT REPORTS AMBER GOVERNOR LIGHT CAME ON IN FLIGHT. NO FAULT CODE WAS GENERATED INDICATING A POTENTIOMETER DEFECT HOWEVER CIRCUMSTANCES REPORTED POINTED TO THIS. A NEW POTENTIOMETER HAS BEEN INSTALLED. PROBLEM FIXED THIS PART HAS LASTED MUCH LONGER THAN TYPICAL THIS IS A RECURRING PROBLEM FOR THIS PART THAT HAS EFFECTED THE DISPATCH RELIABILITY OF THIS MODE AC. THIS PART CAN ON OCCASION ALSO CAUSE ENGINE FLUCTUATIONS IN FLIGHT WHEN THE RESISTANCE VALUE SIGNAL IS DISRUPTED FOR A LITTLE AS 1/20TH OF A SECOND, WHICH IS THE SAMPLE RATE FOR THE ENGINE CONTROL SYS. AN ADDITIONAL FACTOR FOR THESE TYPE OF FAULTS IS NO RESET FUNCTION AVAILABLE TO THE PILOT TO DIFFERENTIATE BETWEEN A MOMENTARY OR AN ACTIVE FAULT. ONCE THE AMBER WARNING LIGHT IS ILLUMINATED IT REMAINS ON UNTIL THE FLIGHT IS TERMINATED EVEN IF SIGNAL DISRUPTION WAS ONLY FOR 1/20TH OF A SECOND DURING AN IN-FLIGHT TURBULENCE EVENT. (K)

Source: SDR M7K2008F00069 · FAA SDRS
O · 2008-01-08 Matched by certificate designator
ATA 3150

PILOT REPORTS AMBER GOVERNOR LIGHT CAME ON IN FLIGHT. NO FAULT CODE WAS GENERATED INDICATING A POTENTIOMETER DEFECT HOWEVER CIRCUMSTANCES REPORTED POINTED TO THIS. A NEW POTENTIOMETER HAS BEEN INSTALLED. PROBLEM FIXED THIS PART HAS LASTED MUCH LONGER THAN TYPICAL THIS IS A RECURRING PROBLEM FOR THIS PART THAT HAS EFFECTED THE DISPATCH RELIABILITY OF THIS MODE AC. THIS PART CAN ON OCCASION ALSO CAUSE ENGINE FLUCTUATIONS IN FLIGHT WHEN THE RESISTANCE VALUE SIGNAL IS DISRUPTED FOR A LITTLE AS 1/20TH OF A SECOND, WHICH IS THE SAMPLE RATE FOR THE ENGINE CONTROL SYS. AN ADDITIONAL FACTOR FOR THESE TYPE OF FAULTS IS NO RESET FUNCTION AVAILABLE TO THE PILOT TO DIFFERENTIATE BETWEEN A MOMENTARY OR AN ACTIVE FAULT. ONCE THE AMBER WARNING LIGHT IS ILLUMINATED IT REMAINS ON UNTIL THE FLIGHT IS TERMINATED EVEN IF SIGNAL DISRUPTION WAS ONLY FOR 1/20TH OF A SECOND DURING AN IN-FLIGHT TURBULENCE EVENT. (K)

Source: SDR M7K2008F00068 · FAA SDRS
N · 2007-09-19 Matched by certificate designator
ATA 6297

NR (ROTOR RPM) MAGNETIC SENSING PICKUP LOOP BROKEN CAUSING INTERMITTENT NR INDICATION FLUCTUATIONS DURING FLIGHT. PROBABLE CAUSE IS THAT WIRE AND FRAGILE COIL WIRE IS HAIR THIN. SUGGEST A STRONGER WIRE HARNESS BE USED. (K)

Source: SDR M7K2008F00136 · FAA SDRS