N814GF

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2009-04-13 Matched by certificate designator
ATA 2130

PILOT REPORTED LOSS OF CABIN PRESSURIZATION DURING FLIGHT AND DIVERTED TO LAND. MX TROUBLESHOOTING AND GROUND ENGINE RUNS COULD NOT DUPLICATE PROBLEM. SUBSEQUENT TEST FLIGHT DUPLICATED DISCREPANCY. PROBLEM IDENTIFIED AS A WEAK OR INTERMITTENT CABIN PRESSURIZATION FLOW CONTROL VALVE (PN 3200335-2). PART REPLACED AND ACFT RETURNED TO SERVICE. (K)

Source: SDR FAU2009F00000 · FAA SDRS