N819JP

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2019-04-22 Matched by certificate designator
ATA 2130

DURING CRUISE AT 40,000FT A LOUD BANG WAS HEARD AND THE CABIN STARTED TO DEPRESSURIZE, PILOTS FOLLOWED THEIR CHECKLIST AND DESCENDED AND LANDED ASAP. THE PROBLEM WAS THAT THE PRESSURIZATION DUCT AT THE WATER SEPARATOR CAME LOOSE FROM THE DUCT ASSY AIR TURBINE DISCHARGE THAT IS A CLAMPED ASSEMBLY. THE WATER SOCK WAS REMOVED AND REPLACED WITH NEW BEFORE THIS FLIGHT, THE SYSTEM WAS INSPECTED AND A FULL OPERATIONAL CHECK WAS PERFORMED BY PRESSURIZING THE AIRCRAFT TO MAX DIFF. NO DEFECTS WERE NOTED AT THAT TIME.

Source: SDR ZESA201942301 · FAA SDRS