N821UP

BEECHCRAFT CORP B300 · 2014 · Valid Registration

Registered owner: WHEELS UP PARTNERS LLC, NY (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
CIRCADIAN AVIATION LLC (O2GA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2022-09-17 Matched by certificate designator
ATA 3200

ON APPROACH THE RIGHT MAIN LANDING GEAR ANNUNCIATOR WAS VERY DIM. CREW CYCLED THE LANDING GEAR AND LIGHT CAME ON BRIGHT. A GO AROUND WAS EXECUTED. TOWER NOTIFIED EMERGENCY VEHICLES TO STANDBY AS A PRECAUTION. LANDING WAS UNEVENTFUL. MAINTENANCE TROUBLESHOT THE DISCREPANCY TO AN INTERMITTENT RIGHT MAIN LANDING GEAR ANNUNCIATOR LIGHT BULB. REPLACED BULB. CYCLED GEAR SEVERAL TIMES WITH NO DEFECTS NOTED. AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR O2GA2022091782101 · FAA SDRS
O · 2022-05-24 Matched by certificate designator
ATA 5610

AT FL270 NOTICED DELAMINATION AND CRACK ON UPPER LEFT CORNER OF THE RIGHT WINDSHIELD. RAN CHECKLIST AND DIVERTED TO KSTL. LANDING WAS UNEVENTFUL. MAINTENANCE REPLACED THE RIGHT WINDSHIELD AND TEMP CONTROLLER. AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR O2GA2022053182101 · FAA SDRS
J · 2017-01-05 Matched by certificate designator
ATA 2200

DURING CRUISE FLIGHT, THE RUDDER BOOST ANNUNCIATOR INTERMITTENTLY CAME ON SEVERAL TIMES DURING FLIGHT. FOLLOWED ABNORMAL PROCEDURES, DIVERTED AND LANDED UNEVENTFULLY. MAINTENANCE TROUBLESHOT AND REPLACED THE AUTOPILOT TRIM SWITCH. SYSTEM OPS CHECKED WERE GOOD. AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR O2GA2017011082101 · FAA SDRS
K J · 2016-05-29 Matched by certificate designator
ATA 7920

AT CRUISE ALTITUDE LT ENG OIL PRESS WENT TO 85 PSI & CONTINUED TO DROP. OIL WAS OBSERVED COMING FROM THE LT ENG BEHIND THE PROPELLER, AT 65 PSI ENG WAS SHUT DOWN. AN EMER WAS DECLARED & ACFT DIVERTED. SECURED THE OIL VENT LINE FROM THE TORQUE TRANSMITTER AT THE POWER SECTION CASE. ENG WAS SERVICED WITH OIL. ENG GND RUNS PERFORMED WITH NO DEFECTS NOTED. A SUCCESSFUL OPERATIONAL CHECK FLIGHT WAS PERFORMED & A POST OCF INSPECTION WAS ALSO PERFORMED WITH NO DEFECTS NOTED. ACFT WAS RETURNED TO SERVICE.

Source: SDR O2GA2016053182101 · FAA SDRS
O · 2016-02-20 Matched by certificate designator
ATA 7321

RIGHT ENG POWER LEVER DOES NOT RESPOND PROPERLY TO LEVER MOVEMENT. R & R THE RT ENG FCU. GND OPERATIONS & LEAK CHECKS WERE GOOD. A SUCCESSFUL OPERATIONAL CHECK FLIGHT WAS PERFORMED & ACFT IT WAS RTS.

Source: SDR O2GA2016022082101 · FAA SDRS
O · 2016-01-31 Matched by certificate designator
ATA 7321

RIGHT ENG CONDITION LEVER WILL NOT ADVANCE OUT OF FUEL CUT OFF. REPLACED THE RT ENG FUEL CONTROL UNIT. A SUCCESSFUL OPERATIONAL CHECK FLIGHT WAS PERFORMED. ACFT WAS RTS.

Source: SDR O2GA2016013182102 · FAA SDRS
O · 2016-01-25 Matched by certificate designator
ATA 7321

DURING OPERATIONAL CHECK FLIGHT FOR FCU REPLACEMENT EXCESSIVE TORQUE SPLIT WITH THROTTLES MATCHED. RIGGED & ADJUSTED THE RT ENG FCU. A SUCCESSFUL OCF WAS PERFORMED. ACFT WAS RTS.

Source: SDR O2GA2016012582102 · FAA SDRS
O · 2016-01-17 Matched by certificate designator
ATA 7321

THE RT FUEL CUT OFF LEVER IS VERY HARD TO MOVE IN EITHER DIRECTION. REPLACED THE RIGHT FCU. OPERATION & LEAK CHECKED OK. ACFT WAS RTS.

Source: SDR O2GA2016011782101 · FAA SDRS
R · 2015-10-27 Matched by certificate designator
ATA 7321

DURING TAKEOFF ROLL, ACFT BEGAN TO YAW & RT ENG POWER ROLLED BACK. TAKEOFF WAS ABORTED & ACFT EXITED THE RUNWAY SAFELY. TROUBLE SHOT THE DISCREPANCY TO A FAULTY RT ENG FUEL CONTROL UNIT. THE RT ENG FUEL CONTROL UNIT WAS REPLACED & A SUCCESSFUL OPERATIONAL CHECK FLIGHT WAS PERFORMED WITH NO DEFECTS NOTED. ACFT WAS RETURNED TO SERVICE.

Source: SDR O2GA2015102782101 · FAA SDRS
J · 2015-07-26 Matched by certificate designator
ATA 2131

AT 25,000' CRUISE THE ACFT SUDDENLY DEPRESSURIZED. CABIN ALTITUDE INDICATED 25,000', WHITE ALT & RED CAB ALT LIGHTS ILLUMINATED. PAX OXYGEN MASKS DEPLOYED, LIGHT ILLUMINATED & WARNING HORN SOUNDED. ACFT LANDED SAFELY. R & R THE CABIN PRESSURIZATION CONTROLLER & SECURED THE PAX OXYGEN MASKS. A SUCCESSFUL SYS OPERATIONAL CHECK WAS PERFORMED. ACFT WAS RETURNED TO SERVICE.

Source: SDR O2GA2015080582101 · FAA SDRS
K · 2015-04-20 Matched by certificate designator
ATA 2810

FUEL LEAK ON RT WING BY WW. REPLACED THE RT AFT BOX & NACELLE FUEL BLADDERS. LEAK CHECKED OK. ACFT WAS RETURNED TO SERVICE. THIS SDR IS BEING SUBMITTED DUE TO A TREND OF NUMEROUS B300 WHEELS UP FLEET FUEL BLADDER LEAK REPORTS. BELIEVES THAT THE LEAKING FUEL BLADDERS ARE THE RESULT OF A BAD BATCH FROM ONE MANUFACTURER. THE REPLACEMENT FUEL BLADDERS ARE FROM A DIFFERENT MANUFACTURER HAVE BEEN RELIABLE.

Source: SDR O2GA2015043082101 · FAA SDRS