N823GA

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
Universal Jet AviationOperator2012-07-13 – 2012-07-13Operator named in NTSB report

Accident & incident history

Acc · 2012-07-13 Operator named in NTSB report
GULFSTREAM GIV Fatal injury NUSNUniversal Jet Aviation
Source: NTSB case DCA12RA110

Maintenance disclosures

F J · 2007-08-07 Matched by certificate designator
ATA 2731

ON AUG 7, 2007 UPON LANDING, THE CREW CALLED MAINT AND REPORTED THAT UPON DESCENT FROM 41,000 FT, THEY GOT A FGC1 FAIL MESSAGE ALONG WITH A FWD TRIM LIMIT MESSAGE. THEY WERE UNABLE TO TRIM THE AIRCRAFT ELEVATORS. THEY COMPLIED WITH THE AC CHECKLIST TO RESET BOTH MESSAGES WITH NO SUCCESS. THEY DISCONNECTED THE AUTOPILOT AND DECLARED AN EMERGENCY WITH ATC AND MANUALLY LANDED THE AC AT AIRPORT WITHOUT INCIDENT. REQUESTED TECH SUPPORT, TECH FOUND THAT HARDWARE ATTACHING THE ELEVATOR TRIM DRIVE SHAFT PILLOW BLOCK HAD LOOSENED CAUSING THE DRIVE SHAFT TO SEPARATE FROM THE OUTPUT SHAFT. THE TECH RESECURED THE HARDWARE AND ATTACHED THE OUTPUT SHAFT TO THE DRIVE INPUT SHAFT. THE TECHNICIAN THEN RIGGED THE ELEVATOR

Source: SDR WWQ2007F00000 · FAA SDRS
K J · 2005-10-13 Matched by certificate designator
ATA 2910

AFTER TAKEOFF, CREW WAS ALERTED THAT THE FLIGHT HYDRAULIC SYSTEM PRESSURE HAD FALLEN BELOW LIMITS, SOON AFTER THE CREW NOTICED THAT THE QUANTITY WAS NEAR EMPTY. CREW CALL MAINTENANCE FROM AC TO DISCUS THE PROBLEM AND THEY ALL AGREED TO LAND ENROUTE FOR MAINTENANCE. MAINT INSPECTED AC, AFTER AN OPERATIONAL CHECK, FOUND RT OR FLIGHT SIDE HYDRAULIC PUMP PRESSURE LINE WAS LEAKING. AFTER FURTHER INSPECTION OF THE PRESSURE LINE, FOUND THAT THE PERMASWAGE FITTING ON THE LINE WAS THE PROBLEM. A NEW LINE AND FITTING WERE ORDERED AND INSTALLED. FLIGHT HYDRAULIC SYSTEM WAS SERVICED AND A LEAK CHECK COMPLIED WITH. NO FURTHER LEAKS OR PROBLEMS NOTED.

Source: SDR WWQ2005F00000 · FAA SDRS