N847MH

EUROCOPTER EC 130 B4 · 2007 · Valid Registration

Registered owner: MUSTANG LEASING LLC, NV (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
MAVERICK AIRSTAR LLC (Q2KA)Certificate holderMatched by certificate designator
MAVERICK HELICOPTER INC (M7KA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2008-11-17 Matched by certificate designator
ATA 5210

DURING ROUTINE INSPECTION THE MOST AFT OTBD CORNER OF THE MOUNTING FLANGE ASSEMBLY WHICH INCLUDES THE UPPER LOCKING PIN MECHANISM WAS CRACKED. A NEW ASSEMBLY WAS INSTALLED.

Source: SDR M7KA0908084266 · FAA SDRS
O · 2008-09-01 Matched by certificate designator
ATA 5210

FOUND SEVERAL HINGE SEGMENTS CRACKED ON ONE END OF THE HINGE LENGTH DURING ROUTINE INSPECTION. THIS IS FAIRLY COMMON DEFECT. (K)

Source: SDR M7KA0810084266 · FAA SDRS
O · 2008-09-01 Matched by certificate designator
ATA 5340

FOUND CRACKED DURING ROUTINE INSPECTION. RECOMMEND THIS PART BE MFG OF A MORE DURABLE MATERIAL SUCH AS STAINLESS STEEL. THIS IS A FAIRLY COMMON DEFECT. (K)

Source: SDR M7KA0811084266 · FAA SDRS
O · 2008-05-12 Matched by certificate designator
ATA 6710

A FAULT CODE WAS GENERATED ON SHUTDOWN INDICATING A DEFECT OF COLLECTIVE POTENTIOMETER. A NEW PART WAS INSTALLED, NO FURTHER FAULT WAS DETECTED. THIS IS RECURRING FAILURE FOR THIS PART WHICH HAS EFFECTED DISPATCH RELIABILITY FOR THIS MODEL HELICOPTER. SUGGEST AN ALTERATION OF FAULT SENSING SOFTWARE TO REDUCE FAULT SENSITIVITY TO PERHAPS A SIGNAL LOSS OF 0.5 SECOND RATHER THAN 1/20TH OF A SECOND. AN OPTIC RATHER THAN A RESISTANCE BASED SENSOR SHOULD BE CONSIDERED AS CONTACT POINT IS DAMAGED BY AC VIBRATION WHEN AC POWER SETTINGS ARE SET FOR CRUISE FLIGHT. (K)

Source: SDR M7K2008F00027 · FAA SDRS
O · 2008-05-12 Matched by certificate designator
ATA 6220

(REF 0505084266) DURING ROUTINE INSP, ADHESIVE BEAD FOR A STAR ARM END BUSHING WAS FOUND CRACKED. FURTHER EXAMINATION UTILIZING A SOAP WATER DETECTION METHOD REVEALED RELATIVE MOTION BETWEEN BUSHING AND STAR ARM END. WITH ROTOR HUB SLEEVES REMOVED, BUSHING COULD BE MOVED MANUALLY. A SECOND BUSHING WAS FOUND LOOSE. A SERVICEABLE REPLACEMENT STARFLEX WAS INSTALLED. THIS IS A DEFECT THAT RECENTLY HAS BECOME MORE COMMON THAN IN THE PAST. SUFFGEST A DIFFERENT ADHESIVE BE UTILIZED OR STAR ARM ENDS AND BUSHINGS BE DESIGNED TO HAVE A LARGER ADHESIVE BONDING SURFACE SUCH AS ADDING INNER BUSHING AND OUTER STAR ARM END SPLINING. THERE WAS NO EVIDENCE OF ANY IMMINENT FAILURE FOR THE PART OR EXCESSIVE PLAY DEVELOPMENT OF THE BUSHING. SUGGEST THAT THE APPLICATION OF A SLIPPAGE MARK BETWEEN THE STAR ARM AND THE BUSHINGS TO SHOW BUSHING ROTATION BE ADDED AS A RECAUTION TO DETECT DANGEROUS MOVEMENT. (K)

Source: SDR M7K2008F00013 · FAA SDRS
O · 2008-04-14 Matched by certificate designator
ATA 6700

A FAULT CODE WAS GENERATED ON SHUTDOWN INDICATING A DEFECTIVE COLLECTIVE POTENTIOMETER. A NEW PART WAS INSTALLED AND NO FURTHER FAULT WAS DETECTED. THIS IS A RECURRING FAULT FOR THIS PART WHICH HAS EFFECTED THE DISPATCH RELIABILITY FOR THIS MODEL AC. SUGGEST NEW DESIGN OR MFG BE FOUND FOR THIS PART AS SOON AS POSSIBLE. (K)-

Source: SDR M7K2008F00132 · FAA SDRS
J · 2008-03-03 Matched by certificate designator
ATA 3150

PILOT REPORTS AMBER GOVERNOR LIGHT ILLUMINATED DURING FLIGHT. A FAULT CODE WAS GENERATED INDICATING THE POTENTIOMETER AS THE LIKELY DEFECTIVE UNIT. A NEW PART WAS INSTALLED AND NO FURTHER DEFECTS WERE NOTED. THIS IS A RECURRING PROBLEM FOR THIS PART THAT HAS EFFECTED THE DISPATCH RELIABILITY FOR THIS AC MODEL. (K)

Source: SDR M7K2008F00071 · FAA SDRS