N875FE

CESSNA 208B · 1990 · Valid Registration

Registered owner: FEDERAL EXPRESS CORPORATION, TN (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
EMPIRE AIRLINES, INC. (COEA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

B · 2024-06-03 Matched by certificate designator
ATA 2421

FLT. 7805 ENROUTE: PHX - NYL AIR TURNBACK/DISCREPANCY: AFTER DEPARTURE ON CLIMBOUT, THE MAIN GENERATOR FAILED. THE AIRCRAFT WAS RETURNED TO PHX AND AN EMERGENCY WAS DECLARED. CORRECTIVE ACTION: MAINTENANCE REPLACED THE STARTER GENERATOR AND A SOAP SAMPLE WAS TAKEN. OPS CHECKS GOOD.

Source: SDR COEA2024060402875 · FAA SDRS
J · 2023-10-04 Matched by certificate designator
ATA 2421

FLT 7801, ENROUTE HII-PHX: DISCREPANCY: GENERATOR OFF LIGHT ILLUMINATED INBOUND TO PHX . WOULD NOT RESET. DECLARED AN EMERGENCY. CONTINUED FLIGHT USING STANDBY POWER. LANDED WITH NO FURTHER ISSUES. CORRECTIVE ACTION: MAINTENANCE REPLACED THE GENERATOR CONTROL UNIT. OPS CHECK GOOD.

Source: SDR COEA2023100505875 · FAA SDRS
N · 2016-11-12 Matched by certificate designator
ATA 3150

ENROUTE, THE PILOT ENCOUNTERED SEVERE TURBULENCE. THE FUEL RESERVOIR LOW LIGHT ILLUMINATED DURING THE TURBULENCE AND REMAINED ILLUMINATED. THE PILOT DECLARED AN EMERGENCY AND DIVERTED. AIRCRAFT LANDED WITHOUT FURTHER INCIDENT. MAINTENANCE COMPLIED WITH THE SEVERE TURBULENCE INSPECTION, NO DEFECTS NOTED. MAINTENANCE REPLACED THE ANNUNCIATOR PANEL. OPS CHECKED GOOD.

Source: SDR COEA2016111201875 · FAA SDRS
N · 2012-08-13 Matched by certificate designator
ATA 5270

ATB: ON CLIMBOUT FROM DRO ON FLT 7774 THE DOOR WARNING LIGHT ILLUMINATED. PILOT TURNED BACK AND LANDED IN DRO WITHOUT INCIDENT. CHECKED DOOR LOCKING MECHANISM, HINGES AND LOCKING PINS. NO DEFECTS NOTED. AIRCRAFT RETURNED TO SERVICE.

Source: SDR COEA2012081301875 · FAA SDRS
K · 1998-05-07 Matched by certificate designator
ATA 3240

WHILE TURNING OUT OF PARKING SPOT TO REPOSITION AIRCRAFT, PILOT REPORTED RT BRAKE PEDAL WENT TO FLOOR AND BRAKING ACTION WENT TO ZERO ON RT SIDE. PILOT SHUT DOWN AIRCRAFT AND SAW THAT RT BRAKE CYLINDER HAD STARTED LEAKING BRAKE FLUID. MAINTENANCE WAS NOTIFIED. REPLACED BRAKE CYLINDER. OPS CHECKED GOOD. AIRCRAFT RETURNED TO SERVICE. (X)

Source: SDR COEA9801875 · FAA SDRS