N888CS

GULFSTREAM AEROSPACE G-IV · 2001 · Valid Registration

Registered owner: ZG AVIATION LLC, NY (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
EXECUTIVE JET MANAGEMENT, INC. (CWQA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2024-05-15 Matched by certificate designator
ATA 5210

IN CRUSE AT FL430, CREW NOTICED A LOUD SOUND AND CABIN PRESSURE LOSS. AT THAT TIME CREW PERFORMED AN EMERGENCY DESCENT TO FL160, WHERE THEY WERE ABLE TO GET CABIN PRESSURE STABILIZED. AT THAT TIME CREW MADE THE DECISION TO DIVERT TO DRO DECLARING AN EMERGENCY. ACFT LANDED NORMALLY. O2 MASKS DID NOT DROP. LOCAL MX WERE ABLE TO INSPECT & REPOSITION UPPER PORTION OF DOOR SEAL INTO SEAL RETAINER. THEY PERFORMED 2 GROUND PRESSURIZATION CHECKS, WITH NO DEFECTS FOUND. ACFT REPOSITION TO VNY. VNY MX INSPECTED DOOR SEAL AND FOUND NO DEFECTS. MX CHECKED SEAL INFLATION CHECKS, AND FOUND NO DEFECTS. DUE TO THIS EVENT BEING THE SECOND, MX REPLACED THE DOOR SEAL WITH A NEW SEAL, AND PERFORMED INFLATABLE SEAL SYSTEM OPERATIONAL TEST, NO DEFECTS WERE FOUND. WORLDWIDE JET HAS ALSO IMPLEMENTED FLEET INSPECTION OF THE DOOR SEALS.

Source: SDR WWQA2024051748688 · FAA SDRS
J · 2024-05-03 Matched by certificate designator
ATA 5210

THREE HOURS INTO THE FLIGHT AT FL430. WE HEARD AN INITIAL POP AND AIR NOISE WE DETERMINED TO BE COMING FROM THE MAIN CABIN DOOR. CABIN PRESSURE WAS HOLDING STEADY AT THIS TIME. WE REQUESTED A LOWER ALTITUDE AS A PRECAUTION. WE WERE ASSIGNED FL380 AND BEFORE THAT DESCENT WAS INITIATED ANOTHER POP THIS TIME MUCH LOUDER AND MORE AIR NOISE COULD BE HEARD. SHORT OF DECLARING AN EMERGENCY I TOLD ATC THAT WE WOULD NEED MUCH LOWER AND DONNED MY MASK JOINING MIKE WHO ALREADY HAD HIS ON. FL310 WAS ASSIGNED. SHORTLY AFTER CABIN ALTITUDE WAS STARTING TO ASCEND RAPIDLY WITH 7,000 FPM NOTED. WITH THE NOISE FROM THE DOOR BEING VERY LOUD AND ATC HARD TO HEAR I PLACED 7700 INTO THE TRANSPONDER AND MIKE BEGAN AN EMERGENCY DESCENT WITH A LEFT TURN TO BE ABLE TO LOOK FOR TRAFFIC. I SET 10,000 FEET INTO THE ALTITUDE PRESELECT. THE FA WAS ON O2 IN THE GALLEY AREA DURING THE DESCENT AND UPDATED US ON HOW THE PASSENGERS WERE DOING - THAT THE MASKS HAD DEPLOYED - THAT PAX WERE ON O2 AND SEEMED TO BE DOING WELL. AROUND 15,000 FEET I WAS ABLE TO RE-ESTABLISH COMMUNICATION WITH ATC AND OBTAINED A VERBAL CLEARANCE TO 10,000 FT. WE VERIFIED THE EMERGENCY DESCENT CHECKLIST COMPLETE AND COORDINATED WITH ATC FOR A DIVERSION TO KAMA. UNEVENTFUL VISUAL APPROACH AND LANDING. NO INJURIES DURING THE EMERGENCY PROCEDURE. CORECTIVE ACTION: INSPECTED DOOR SEAL, FOUND UPPER SECTION NOT FULLY SEATED. SEATED SEAL WITH REF TO AMM. PRESSURE & LEAK CHECKS WERE GOOD. ACFT CONTINUED TO VNY.

Source: SDR WWQA2024050943452 · FAA SDRS