N897FE

CESSNA 208B · 1990 · Valid Registration

Registered owner: FEDERAL EXPRESS CORPORATION, TN (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
EMPIRE AIRLINES, INC. (COEA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

C B · 2025-01-28 Matched by certificate designator
ATA 7200

FLIGHT NUMBER:4701 ROUTE: KGEG-KPSC DISCREPANCY: EXPERIENCED SMOKE IN THE COCKPIT, DECLARED AN EMERGENCY PERFORMED AIR TURN BACK TO KGEG CORRECTIVE ACTION: CLEANED DEICE FLUID FROM ENGINE COWLING, RAN ENGINE PER C208 CHECKLIST FOR 10 MINUTES WITH HEAT ON, NO ABNORMAL SMOKE OR SMELL NOTED

Source: SDR COEA2025012901897 · FAA SDRS
F · 2020-07-21 Matched by certificate designator
ATA 5312

ELONGATED BOLT HOLES FOUND IN SPLICE-UPPER LH FWD #: 2611118-7 ON MAIN LANDING GEAR BULKHEAD STRUCTURE, FOUND DURING DOCUMENT 16, TASK 53-10-00-256. REQUIRES REPLACEMENT OF SPLICE.

Source: SDR 2020F00344 · FAA SDRS
K · 2016-07-30 Matched by certificate designator
ATA 7261

ON START UP OF THE AIRCRAFT, AN OIL LEAK FROM THE FORWARD ENGINE COMPARTMENT WAS NOTICED. THE PILOT IMMEDIATELY SHUT DOWN THE ENGINE. MAINTENANCE REPLACED THE OIL RETURN TUBE ELBOW AND APPLICABLE O-RINGS IAW PT6-114A MM 79-20-01. GROUND RUN UP FOR OPS OF LEAK CHECK GOOD. AIRCRAFT RETURNED TO SERVICE.

Source: SDR COEA2016073001897 · FAA SDRS
O · 2015-11-27 Matched by certificate designator
ATA 7722

FLIGHT 8786 AIR TURN BACK, WO 208-156061 & DISCREPANCY. INLET TURBINE TEMPERATURE GAUGE FLUCTUATED IN FLIGHT. CREW ELECTED TO RETURN, NO EMER DECLARED & ACFT LANDED WITHOUT INCIDENT. CRIMPED TERMINAL LUGS AT T5 BLOCK. OPERATIONS CHECKED & ENG PERFORMANCE RUNS GOOD. ACFT RETURNED TO SERVICE.

Source: SDR COEA2015112701897 · FAA SDRS
O · 2013-05-29 Matched by certificate designator
ATA 7314

DURING ROUTINE FUEL PUMP GARLOC SEAL REPLACEMENT FOR LEAKAGE, THE MECHANIC INSPECTED THE FUEL PUMP DRIVE GEAR AND IT BECAME DECOUPLED FROM THE FUEL PUMP. THIS IS NOT NORMAL FOR THIS MODEL PUMP. THE ACCESSORY DRIVE GEAR IS HOLLOW AND HAD THE FUEL PUMP DRIVE MIGRATED FORWARD AND DECOUPLED FROM THE PUMP, THE FCU WOULD HAVE LOST REFERENCE AND CAUSED AN INFLIGHT SHUTDOWN. INSPECTION OF THE DRIVE GEAR APPEARS THE RETAINER IS DEFORMED AND INEFFECTIVE.

Source: SDR AWHA20130530001 · FAA SDRS
J · 2007-07-23 Matched by certificate designator
ATA 2610

JUST AFTER TAKEOFF, ON FLIGHT NR 7797 THE PILOT RECEIVED A FIRE WARNING. HE DECLARED AND EMERGECY AND RETURNED. AIRCRAFT LANDED WITHOUT INCIDENT. MAINTENANCE DISCOVERED THE FIRE WARNING TEST BUTTON HAD FALLEN OFF CAUSING A FALSE WARNING. MAINTENANCE REINSTALLED THE FIRE WARNING TEST BUTTON. FOUND FIRE TEST BUTTON LOOSE. MAINTENANCE THEN REMOVED AND REPLACED THE FIRE TEST BUTTON. AIRCRAFT RETURNED TO SERVICE. (K)

Source: SDR COEA0701897 · FAA SDRS