N909FX

AEROSPATIALE/AERITALIA ATR 42-300 · 1991 · Valid Registration

Registered owner: FEDERAL EXPRESS CORP, TN (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2025-04-01 Matched by certificate designator
ATA 3500

OXYGEN SYSTEM TRANSMITTER / REGULATOR SLOWLY LEAKING.

Source: SDR MTNA20250401001 · FAA SDRS
M J · 2024-06-04 Matched by certificate designator
ATA 7313

DURING CRUISE OF FLIGHT 8106 BQN-BGI, AIRCRAFT 909FX INCURRED A HIGH ITT ON THE RIGHT ENGINE WHICH RESULTED IN A DECLARED EMERGENCY AND DIVERSION INTO STX. AIRCRAFT 909FX LANDED UNEVENTFULLY. REMOVED AND REPLACED THE #2 ENGINE FUEL NOZZLE KIT.

Source: SDR MTNA20240604001 · FAA SDRS
J · 2022-07-19 Matched by certificate designator
ATA 3200

WHILE CONFIGURING THE AIRCRAFT TO LAND, THE CREW SELECTED THE LANDING GEAR FOR LANDING. BOTH THE FORWARD AND OVERHEAD PANEL’S LANDING GEAR INDICATORS REMAINED RED, INDICATING AN UNSAFE GEAR SITUATION. THE CREW DISCONTINUED THE APPROACH TO LAND, DECLARED AN EMERGENCY, AND RAN THE QRH. THE FLIGHT THEN LANDED WITHOUT ANY FURTHER INCIDENT. MAINTENANCE TROUBLESHOT SYSTEM AND FOUND A BAD LANDING GEAR SELECTOR VALVE AND REPLACED. OPS CHECK GOOD.

Source: SDR MTNA20220719001 · FAA SDRS
B · 2017-09-13 Matched by certificate designator
ATA 2120

DURING DESCENT, THE CREW DETECTED A BURNING ODOR. NO WARNING WAS TRIGGERED. THE CREW DECLARED AN EMERGENCY, AND LANDED WITHOUT INCIDENT. AN OPERATIONAL CHECK OF THE CABIN & FLIGHT COMPARTMENT AIR DISTRIBUTION, SMOKE DETECTION SYSTEM, AVIONICS WINDSHIELD HEAT, AND SIDE WINDOW HEAT WAS PERFORMED. A GVI OF THE AVIONICS RACKS, COCKPIT, CARGO AREAS, AND COWLING WAS PERFORMED, AS WELL AS A GVI FOR OIL LEAKS. OPERATIONAL CHECKS WERE GOOD, NO DEFECTS WERE NOTED, AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR MTNA20170914001 · FAA SDRS
O · 2017-06-27 Matched by certificate designator
ATA 3243

DURING TAXI, THE AIRCRAFT EXPERIENCED A COMPLETE BRAKE FAILURE. THE AIRCRAFT WAS STOPPED USING THE EMERGENCY BRAKE, AND RETURNED TO GATE WITHOUT INCIDENT. THE FO'S MASTER CYLINDER WAS REPLACED, ALONG WITH THE LOW-PRESSURE RESERVOIR AND THE METERING VALVE. THE LOW-PRESSURE SYSTEM WAS BLED, THE OPERATIONAL CHECK WAS GOOD, AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR MTNA2017062701 · FAA SDRS
O · 2013-07-29 Matched by certificate designator
ATA 5330

FOUND CORROSION ON FUSELAGE SKIN BETWEEN FRAMES 17 AND 20 AND BETWEEN STRINGERS 13L AND 14L TO BE OUT OF SRM LIMITS. REPAIRED SKIN IAW SRAS S535R0272. 7876.

Source: SDR MTNA20130801036 · FAA SDRS
O · 2013-07-18 Matched by certificate designator
ATA 5321

FOUND CORROSION ON FLOOR PANEL 214BF, OUT OF LIMITS. REPLACED FLOOR PANEL IAW SRM.

Source: SDR MTNA20130718031 · FAA SDRS
O · 2013-07-18 Matched by certificate designator
ATA 5753

FOUND CORROSION ON RT INBD FLAP, OTBD END RIB, OUT OF LIMITS. REPLACED END RIB IAW SRM.

Source: SDR MTNA20130718032 · FAA SDRS
O · 2013-07-18 Matched by certificate designator
ATA 5753

FOUND CORROSION ON LT INBD FLAP, OTBD END RIB, OUT OF LIMITS. REPLACED END RIB IAW SRM.

Source: SDR MTNA20130718033 · FAA SDRS
O · 2013-07-17 Matched by certificate designator
ATA 5310

FOUND CORROSION ON CREASE BEAM WEB, OUT OF LIMITS. REPLACED WEB IAW SRM.

Source: SDR MTNA20130716029H · FAA SDRS
O · 2013-07-15 Matched by certificate designator
ATA 5310

FOUND CORROSION ON CREASE BEAM WEB, OUT OF LIMITS. REPLACED WEB IAW SRM.

Source: SDR MTNA20130717030H · FAA SDRS
O · 2013-03-27 Matched by certificate designator
ATA 7200

60 MILES OUT OF MYR THE NUMBER ONE ENGINE LOST OIL PRESSURE. THE ENGINE WAS SHUT DOWN THE QRH PROCEDURES WERE APPLIED. AN EMERGENCY WAS DECLARED. THE AIRCRAFT LANDED WITHOUT OTHER PROBLEMS.

Source: SDR MTNA201303270001 · FAA SDRS
O · 2008-04-09 Matched by certificate designator
ATA 5751

DURING INSPECTION LEVEL 2 EXFOLIATION CORROSION WAS FOUND ALONG EDGE OF BEARING OUTER FITTING I/B ON THE RT AILERON OUTBOARD HINGE/SHACKLE ASSEMBLY. THE BEARING OUTER HINGE WAS REPLACED. INSPECTION REASON: MRB 576108-01 REFERENCE ATR 42 SRM 57-61-10 P115-116 FIG 1.

Source: SDR MAC040802 · FAA SDRS
O · 2008-04-09 Matched by certificate designator
ATA 5751

DURING INSPECTION LEVEL 2 CORROSION WAS FOUND ON THE AILERON "TEE PICKUPS" (TEE CLIPS) ON THE LEFT AILERON ASSEMBLY. THE EXFOLIATION CORROSION WAS ALONG THE EDGES AND SIDES OF THE FITTINGS. REFERENCE: ATR 42 SRM 57-61-10 P 115/116 FIG 1. REASON FOR INSPECTION MRB 576108-01.

Source: SDR MAC040803 · FAA SDRS
O · 2005-09-12 Matched by certificate designator
ATA 5315

THE LONGITUDINAL FLOORBEAM BL 0 AT FRAME 15 CRACKED NEAR ATTACH POINT TO THE LATERAL FLOORBEAM. CRACK WAS DISCOVERED DURING TROUBLESHOOTING ANOTHER UNRELATED PROBLEM. REPAIR WAS ACCOMPLISHED PER EO 4225001-42-53-32. THIS PART WAS INSTALLED BY STC ST01189W1.

Source: SDR MAC90501 · FAA SDRS