N912SV

BEECH B200 · 1988 · Valid Registration

Registered owner: SAINT VINCENTS HEALTHCARE, MT (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
LYNCH FLYING SERVICE INC (HSRA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2024-02-12 Matched by certificate designator
ATA 2720

DURING A "COMPLETE INSPECTION" IAW BEECH MAINTENANCE MANUAL CH. 05 THE LOWER RUDDER ATTACH BOLTS WERE INCORRECT P.N'S INSTALLED. THE FOLLOWING PARTS WERE FOUND INSTALLED WHICH RESULTED IN THE LOWER RUDDER MOUNT LOOSE ON THE RUDDER BELLCRANK WERE AS FOLLOWS 3 EACH BOLT P.N. 1104-12 (GRIP LENGTH .75 INCHES), IT WAS DISCOVERED THE REQUIRED WASHER P.N. AS960-416 UNDER THE BOLT HEAD AND NUT WERE MISSING AND 3 EACH NUT'S P.N. 130909N32. THE NUTS ARE FOUND TO BE CORRECT P.N.

Source: SDR 2024FA0000143 · FAA SDRS
P · 2023-01-25 Matched by certificate designator
ATA 3416

APPROXIMATELY 45 MINUTES AFTER DEPARTING KBIL WHILE IN CRUISE FLIGHT, THE CREW OBSERVED THE PILOTS ALTIMETER CLIMBING RAPIDLY WITHOUT STOPPING. THE CREW RETURNED TO KBIL WITHOUT INCIDENT. MAINTENANCE REPLACED THE PILOTS ALTIMETER WITH AN OVERHAULED UNIT AND OPS CHECK GOOD.

Source: SDR 2023F00035 · FAA SDRS
J · 2022-10-06 Matched by certificate designator
ATA 3260

10/6/2022: N912SV LEFT KBIL @ APPROXIMATELY 2340 ENROUTE 1S3 (FORSYTH, MT). UPON REACHING CRUISE, THE PILOT OBSERVED THE "GEAR UNSAFE" LIGHT ILLUMINATED. AFTER A FEW MINUTES, THE LIGHT BECAME INTERMITTENT. THE CREW EXTENDED THE LANDING GEAR AND OBSERVED 3 GREEN LANDING GEAR "DOWN AND LOCKED" LIGHTS WITH NO "GEAR UNSAFE" LIGHT. THE CREW DECIDED TO RETURN TO KBIL AT THIS POINT. THE AIRCRAFT LANDED BACK AT KBIL @ APPROXIMATELY 0020 WITHOUT INCIDENT.

Source: SDR 2022F00384 · FAA SDRS
I · 2022-08-25 Matched by certificate designator
ATA 3421

10 MINUTES INTO A FLIGHT TO KLWT FROM KBIL THE FLIGHT CREW OBSERVED THE CO-PILOT ATTITUDE GYRO WAS NOT WORKING PROPERLY. THEY RETURNED TO KBIL WITHOUT INCIDENT.

Source: SDR 2022F00332 · FAA SDRS
B · 2017-06-25 Matched by certificate designator
ATA 2120

PILOT REPORTED AN ODOR FROM THE AIR CONDITIONING VENTS UPON LANDING. THE AIRCRAFT WAS INSPECTED AND NO FAULTS WERE FOUND. THEY THEN TOOK IT ON A TEST FLIGHT AND COULD NOT DUPLICATE THE REPORTED ODOR.

Source: SDR HSRR201706260001 · FAA SDRS
H · 2012-10-31 Matched by certificate designator
ATA 2497

LANDING GEAR FAILED TO RETRACT AFTER TAKEOFF. THE NR 2 ELECTRICAL BUSS WAS WITHOUT POWER. MX FOUND THAT BOTH THE BUSS FEED DIODES HAD FAILED OPEN.

Source: SDR 2012F00233 · FAA SDRS