N917PG

CESSNA 750 · 1999 · Valid Registration

Registered owner: AIR PLAY I LLC, DE (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2025-09-05 Matched by certificate designator
ATA 3610

DURING CLIMB PILOT RECEIVED EICAS MESSAGE "PAC HP VLV OPN L-R"

Source: SDR AJXA2025090800037 · FAA SDRS
J · 2023-10-13 Matched by certificate designator
ATA 5200

DURING CLIMB THE CREW HEARD A NOISE FROM THE FRONT OF THE AIRCRAFT AND A WARNING LIGHT FOR THE NOSE AVIONICS DOOR OPEN. THE CREW WAS ABLE TO RETURN TO THE DEPARTURE AIRPORT SAFELY. THE DOOR WAS INSPECTED FOR THE PROPER ADJUSTMENT OF THE NOSE DOOR LATCHES AND PROPERLY SECURED. AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR AJXA2023101600024 · FAA SDRS
K · 2023-02-27 Matched by certificate designator
ATA 2900

IN FLIGHT DURING CLIMB PILOT RECEIVED CAS MESSAGE "HYDRAULIC VOLUME LOW B". AFTER LANDING AND INSPECTING AIRCRAFT WE FOUND THAT THE HYDRAULIC PTU CONTROLLER SOLENOID LEAKING. THE PART WAS REPLACED WITH AN OVERHAULED UNIT AND NO FURTHER DEFECTS WERE DETECTED.

Source: SDR AJXA2023022700022 · FAA SDRS
O · 2022-08-21 Matched by certificate designator
ATA 3260

DURING TAKEOFF THE PILOT ATTEMPTED TO RETRACT THE LANDING GEAR. DURING THE PROCESS OF RETRACTION THE RIGHT HAND GREEN INDICATION DOWN AND LOCK STAYED ILLUMINATED. DUE TO THIS PROBLEM THE PILOT RETURNED TO HIS POINT OF DEPARTURE. WE PERFORMED GEAR SWINGS ON THE AIRCRAFT AND FOUND THAT FOUND RH MLG DOWNLOCK SWITHC WAS INOP. WE CHANGED THE SWITCH/ PERFORMED THE GEAR SWINGS AND THE ISSUE WAS CLEARED

Source: SDR AJXA2022082100020 · FAA SDRS
J · 2020-02-10 Matched by certificate designator
ATA 3610

DURING FLIGHT THE RIGHT HAND BLEED WARNING LIGHT CAME ON. THE AIRCRAFT SAFELY MADE AN UNSCHEDULED LANDING IN CHARLESTON SOUTH CAROLINA. THE PNEUMATIC LINES IN THE RIGHT HAND PYLON WERE INSPECTED AND THE TECHNICIAN LOCATED A SEAL BLOWN OUT ON ONE OF THE DUCT. THE SEAL WAS REPLACED AND SATISFACTORY OPS CHECK WAS PERFORMED IN THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR AJXA2020022500006 · FAA SDRS
J · 2019-12-29 Matched by certificate designator
ATA 7830

LH THRUST REVERSER ARM CAME ON DURING CLIMB WITH AMBER TR UNLOCK LIGHT. THE AIRCRAFT RETURNED TO ITS POINT OF ORIGIN AND WAS GROUNDED.

Source: SDR AJXA2019123000004 · FAA SDRS
J · 2019-11-09 Matched by certificate designator
ATA 2130

DURING CLIMB AIRCRAFT DID NOT PRESSURIZE. AIRCRAFT RETURNED TO POINT OF ORIGIN AND SAFELY LANDED. ONCE AIRCRAFT LANDED PILOTS MEL’D PRESSURIZATION SYSTEM AND RETURNED TO FXE FOR MAINTENANCE. AIRCRAFT IS CURRENTLY AWAITING MAINTENANCE TO TROUBLESHOOT PRESSURIZATION SYSTEM.

Source: SDR AJXA2019110900003 · FAA SDRS
J · 2019-08-15 Matched by certificate designator
ATA 2130

AIRCRAFT WOULD NOT PRESSURIZE DURING CLIMB. THE AIRCRAFT RETURN SAFELY TO DEPARTURE AND TAXIED TO THE SERVICE CENTER TO TROUBLESHOOT THE FAILURE. TESTED THE PRESSURIZATION SYSTEM AND WAS UNABLE TO DUPLICATE THE FAULT OR FIND ANY DEFECT THAT CAUSED THE PROBLEM. THE AIRCRAFT WAS RETURNED TO SERVICE AND HAS NOT EXPERIENCED ANY ADDITIONAL PROBLEMS WITH THE PRESSURIZATION SYSTEM.

Source: SDR AJXA201908150244 · FAA SDRS
J · 2019-07-25 Matched by certificate designator
ATA 2130

AIRCRAFT WOULD NOT PRESSURIZE DURING CLIMB. THE AIRCRAFT RETURN SAFELY TO DEPARTURE AND TAXIED TO THE MANUFACTURER SERVICE CENTER TO TROUBLESHOOT THE FAILURE. MANUFACTURER TESTED THE PRESSURIZATION SYSTEM AND WAS UNABLE TO DUPLICATE THE FAULT OR FIND ANY DEFECT THAT CAUSED THE PROBLEM. THE AIRCRAFT WAS RETURNED TO SERVICE AND HAS NOT EXPERIENCED ANY ADDITIONAL PROBLEMS WITH THE PRESSURIZATION SYSTEM.

Source: SDR AJXA201908220001 · FAA SDRS