N917SF

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2006-02-01 Matched by certificate designator
ATA 3210

DURING SCHEDULED INSPECTION IT WAS DISCOVERED THAT THE LANDING GEAR RETRACT PUSH-PULL TUBE HAD BEEN STRIKING THE FUEL LINES IN THE RT GEAR WELL. DAMAGE TO THE PUSH-PULL TUBE WAS MINIMAL AND LIMITED TO THE PAINT BEING REMOVED, DAMAGE TO THE FUEL LINES WAS SUCH THAT APPROXIMATELY 40% OF THE LINE WALL THICKNESS HAD BEEN WORN AWAY. BOTH FUEL LINES WERE REPLACED. ONE OTHER AIRCRAFT HAD BEEN FOUND WITH THIS CONDITION IN PREVIOUS YEARS, AND ALTHOUGH THAT AIRCRAFT HAD MUCH HIGHER TOTAL TIME (11,000+ HRS.) THE RT WING HAD BEEN PREVIOUSLY REMOVED AND ON THAT AIRCRAFT THE LINES WORE TO THE POINT OF LEAKING.

Source: SDR 917SF · FAA SDRS
O · 2005-05-25 Matched by certificate designator
ATA 7120

WHILE PERFORMING A SCHEDULED INSPECTION, 3 OF THE 4 ENGINE MOUNT (CUSHION) BOLTS WERE FOUND LOOSE. 2 REQUIRED 1 FULL TURN TO TIGHTEN, AND THE 3RD TOOK ALMOST 2 TURNS TO TIGHTEN. THE SELF LOCKING FEATURE OF THE NUTS WAS CHECKED AND APPEARED TO BE OK. IT CAN ONLY BE ASSUMED THAT THE BOLTS WERE NOT PROPERLY TORQUED BY THE MFG AT ENGINE INSTALLATION. THE BOLTS WERE TORQUED IAW SRM AND THE OPPOSITE ENGINE MOUNT BOLTS WERE CHECKED AND FOUND TO BE PROPERLY TORQUED. (K)

Source: SDR SFO2005F00002 · FAA SDRS