N922LR

IAI LTD GULFSTREAM G150 · 2011 · Valid Registration

Registered owner: CAPITAL HOLDINGS 210 LLC, DE (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
JET LINX AVIATION, LLC (9JLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

L · 2023-07-27 Matched by certificate designator
ATA 3350

SVC DR FWD MID LVL EXIT SIGN 1 BULB INOP- RELAMPED

Source: SDR MASA2023072700099 · FAA SDRS
L · 2023-07-27 Matched by certificate designator
ATA 3350

SVC DR AFT MID LVL EXIT SIGN 1 BULB INOP- RELAMPED

Source: SDR MASA2023072700097 · FAA SDRS
L · 2023-07-27 Matched by certificate designator
ATA 3350

ROW 13 A/F MID LVL EXIT SIGN 1 BULB INOP - RELAMPED

Source: SDR MASA2023072700098 · FAA SDRS
N · 2021-10-01 Matched by certificate designator
ATA 5270

THE FLIGHT CREW REPORTED OF A BAGGAGE/FUEL DOOR CAS MESSAGE. OPERATIONS WERE CONTINUED PER MEL 52-4. THE MAINTENANCE TEAM TROUBLESHOT AND FOUND THE FUEL DOOR MICROSWITCH TO BE DEFECTIVE. THE SWITCH WAS REPLACED WITH NEW AND RIGGED. OPERATIONS WERE SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021100526529 · FAA SDRS
J · 2021-07-08 Matched by certificate designator
ATA 7897

THE FLIGHT CREW REPORTED FAULTS WITH THE THRUST REVERSER SYSTEM. THE SYSTEM FAULT WAS DEFERRED ON MEL AND OPERATIONS WERE CONTINUED. THE MAINTENANCE TEAM TROUBLESHOT AND DETERMINED THE RIGHT THRUST REVERSER HARNESS WAS DEFECTIVE. THE HARNESS WAS REMOVED AND A REPAIRED HARNESS WAS INSTALLED. OPS CHECKS WERE SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021072829979 · FAA SDRS
J · 2021-07-08 Matched by certificate designator
ATA 3444

THE FLIGHT CREW REPORTED DESCRIBING A FAULT WITH THE RADAR ALTIMETER WITH INDICATORS "RA" AND "TCAS FAIL" ILLUMINATED ON BOTH PFD'S FOLLOWED BY "GROUND PROX AND WINDSHEAR FAIL" CAS MESSAGES. THE MAINTENANCE VENDOR TROUBLESHOT AND DETERMINED THE RADAR ALTIMETER WAS DEFECTIVE. THE UNIT WAS REMOVED AND AN OVERHAULED UNIT WAS INSTALLED. THE MX VENDOR ALSO REMOVED AND REPLACED THE NO1 AND NO2 RADAR ALTIMETER ANTENNAS. OPS CHECKS WERE SATISFACTORY. THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021072826517 · FAA SDRS
O · 2019-10-14 Matched by certificate designator
ATA 2622

AFT PORTABLE FIRE EXT LOW PRESSURE. REPLACED FIRE EXT.

Source: SDR MASA2019101412090 · FAA SDRS