N95WA

BEECH 99 · 1968 · Valid Registration

Registered owner: ALPINE AVIATION INC, UT (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
ALPINE AVIATION, INC. (TIMA)Certificate holderMatched by certificate designator

Accident & incident history

Accident · 1985-07-16 Matched by aircraft (N-number)
Beech 99 None injuryALPINE AVIATION, INC.
Source: NTSB case ATL85FA213
Incident · 1982-04-18 Matched by aircraft (N-number)
Beech BE-99 None injuryALPINE AVIATION, INC.
Source: NTSB case ATL82IA109

Maintenance disclosures

N · 2023-08-03 Matched by certificate designator
ATA 7700

AFTER TAKEOFF WHILE CLIMBING THROUGH ROUGHLY 6000 FEET THE TORQUE AND ITT BEGAN TO SLOWLY FALL. AFTER PILOT NOTICED THE DECREASE HE REQUESTED TO GO BACK TOWARD THE AIRPORT AND BEGAN TO TROUBLE SHOOT. HE INCREASED AND DECREASED THE POWER LEVERS AND NOTICED VERY LITTLE CHANGE. THE TORQUE KEP SLOWLY DECREASING. HE CYCLED THROUGH INVERTERS TO ENSURE IT WASN'T A GAUGE. AT THAT TIME HE REQUESTED A CLEARANCE BACK TO THE AIRPORT AT WHICH TIME HE EXECUTED A VISUAL APPROACH TO RUNWAY 28R.

Source: SDR TIMA202309013006 · FAA SDRS
B · 2019-04-16 Matched by certificate designator
ATA 2497

PILOT REPORTED SMOKE IN COCKPIT WHILE INBOUND. UPON INVESTIGATION, FOUND WIRES CHAFED TO GROUND AND OVERHEATED.

Source: SDR TIMA2019041900006 · FAA SDRS
A Y · 2008-10-27 Matched by certificate designator
ATA 7200

PILOT FELT A POWER SURGE AND SAW FLAMES OUT THE LEFT ENGINE EXHAUST FOR A MOMENT. LEFT PROPELLER STOPPED TURNING. PILOT SECURED ENGINE, CONTINUED ON AND LANDED WITHOUT INCIDENT. INVESTIGATION REVEALED THAT THE PT BLADES WERE MOSTLY GONE. CT BLADES ARE OK. SUSPECT BEARING FAILURE IN POWER SECTION.

Source: SDR TIMA20080006 · FAA SDRS
O · 2005-10-11 Matched by certificate designator
ATA 5751

LT ELEVATOR WAS FOUND CRACKED BEHIND ELEVATOR BALANCE WEIGHT AT THE OB END OF THE ELEVATOR. UPON FURTHER INVESTIGATION IT WAS DISCOVERED THAT THE BALANCE WEIGHT WAS MODIFIED TO INCREASE THE WEIGHT. THE ADDED WEIGHT WAS DETERMINED TO BE INSTALLED BECAUSE THE ELEVATOR HAD BEEN SKINNED WITH ALUMINUM AND WAS PREVIOUSLY SKINNED WITH MAGNESIUM. THE ADDED WEIGHT OF THE ALUMINUM SKIN REQUIRED ADDED WEIGHT FOR BALANCING THE ELEVATOR. THIS ADDED WEIGHT CAUSED THE RIB TO CRACK. ELEVATOR WAS REPLACED WITH AN ALUMINUM ELEVATOR. ALUMINUM ELEVATOR HAS AN ADDITIONAL BALANCE WEIGHT INSTALLED FOR BALANCING PURPOSES. KIT 99-4018S WAS INSTALLED IN THE HORIZ STAB TO PROVIDE AN OPENING FOR THE ADDITIONAL BALANCE WEIGHT. (K)

Source: SDR 2005FA0001571 · FAA SDRS
R J · 2001-05-16 Matched by certificate designator
ATA 7322

ENGINE REPORTEDLY BACKFIRED AND SURGED AT HIGH POWER SETTINGS WHEN MAKING CHANGES IN POWER SETTING. ENGINE PASSED ALL GROUND PERFORMANCE CHECKS SO A FCU WAS REPLACED FOR TROUBLESHOOTING. ITS UNKNOWN WHAT CAUSED THE FCU TO MALFUNCTION DURING THE ACCELERATION MODE.

Source: SDR TIM2001F00003 · FAA SDRS
O · 2000-06-13 Matched by certificate designator
ATA 2711

THE AILERON TRIM TAB DID NOT PASS A VISUAL SURFACE INSPECTION DURING A CHECK OF THE FREE PLAY DURING A DETAILED INSPECTION. REMOVED ENTIRE AILERON ASSY AND INSTALLED A SERVICEABLE AILERON ASSY. THE INSPECTION PROCESS WORKED IN THIS CASE AS DESIGNED SO AN INCREASE IN FREQUENCY IS NOT WARRANTED. THE INSPECTION/CHECK IS FOR FREE-PLAY AND THE DISCREPANCY WAS FOR BOTH FREE-PLAY IN EXCESS OF THE MFG''S RECOMMENDATIONS AND CRACKS IN THE SKIN. CRACKS IN THE SKIN APPEAR TO BE THE RESULT OF IMPROPER GROUND HANDLING. (X)

Source: SDR 20000720SH001 · FAA SDRS
O · 1999-06-18 Matched by certificate designator
ATA 3213

THE TORQUE KNEES (UPPER AND LOWER) WERE FOUND CRACKED DURING INSPECTION. CRACK NEAR CENTER PIVOT BOLT AREA.

Source: SDR 99ZZZX2549 · FAA SDRS
O · 1999-04-26 Matched by certificate designator
ATA 5720

CRACK FOUND IN LEFT GEAR WELL AFT OF MAIN SPAR ON INBOARD SIDE OF THE CAP IN THE VICINITY OF THE NACELLE SPLICE PLATE.

Source: SDR 99ZZZX2109 · FAA SDRS
K · 1999-01-29 Matched by certificate designator
ATA 2810

ON POST-FLIGHT, PILOT REPORTED FUEL LEAKING FROM RT WING FROM GEAR DOOR, FUEL TRACED TO BOX CELL AFT OF SPAR, OUTBOARD OF NACELLE. REPLACED FUEL CELL, POST-WORK OPS CHECKS OK. POSSIBLE CAUSE OF LEAKAGE WAS CONDITION/AGE OF FUEL CELL AND/OR IMPROPER INSTALLATION.

Source: SDR 99ZZZX803 · FAA SDRS