N971K

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2004-11-29 Matched by certificate designator
ATA 2910

CREW REPORTED THAT LANDIND GEAR EXTENSION TOOK LONGER THAN NORMAL TO EXTEND. WHEN DOWN AND LOCKED WAS ACHIEVED, CREW NOTICED COMPLETE LOSS OF HYDRAULIC PRESSURE. NORMAL LANDING WAS MADE USING EMERGENCY BRAKES. JACKED AIRCRAFT AND PERFORMED GEAR SWINGS. FOUND CAUSE TO BE A PIN HOLE IN LT SPOILER DOWN LINE ON TOP OF CENTER WING SECTION. CORROSION IS PROBABLE CAUSE FOR PIN HOLE. (K)

Source: SDR KNI2005F00000 · FAA SDRS
L · 2002-11-22 Unresolved
ATA 3415

MACH OVERSPEED SWITCH FAILED DURING FUNCTIONAL TEST.

Source: SDR I122003F00000 · FAA SDRS