N990HA

DASSAULT AVIATION FALCON 7X · 2009 · Valid Registration

Registered owner: TVPX AIRCRAFT SOLUTIONS INC TRUSTEE, UT (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
CLAY LACY AVIATION, INC. (BKEA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2026-06-17 Matched by certificate designator
ATA 2782

DURING REMOVAL OF THE WING LOWER SURFACE REMOVABLE PANELS (T57-10-01-90-801-01/02 ENCLOSED), AND ESPECIALLY DURING REMOVAL OF ACCESS PANELS (PARAGRAPH 3.E.FIG 2), TECHNICIANS NOTICED THAT SCREWS WERE NOT TIGHTENED CORRECTLY ON THE RH MIDDLE SLAT OUTBOARD HOOK R1501CM AND TAB WASHERS WERE NOT BENT ON RH OUTBOARD SLATS ACTUATORS R401CM AND R601CM. ALL DISCREPANCIES CORRECTED BY THE TECHNICIANS DURING REINSTALLATION AND INSPECTION PERFORMED ON ALL COMPONENTS ON BOTH WINGS.

Source: SDR 2026FA0000521 · FAA SDRS
O · 2026-04-01 Matched by certificate designator
ATA 3040

DURING APPLICATION OF SB F7X-630 ON AIRCRAFT, FOUND FEEDER (0V) NUT OF BACK UP WINDSHIELD DE-ICING POWER SUPPLY M1001DG NOT TIGHT.

Source: SDR 2026FA0000246 · FAA SDRS
W · 2026-02-26 Matched by certificate designator
ATA 2810

FOLLOWING REMOVAL OF BOTH WINGS FOR CENTRAL WING PANELS REPLACEMENT, ACCESSES ARE PERFORMED IN THE FEEDER TANKS. PIPES, BRACKETS, PUMPS WERE REMOVED. DURING THESE ACCESSES, COMPONENTS IN THE FEEDERS TANKS ARE DISCOVERED INSTALLED WITHOUT PRC & PAINT PROTECTION IAW AMM. THE AIRPLANE IS JUST OUT OF 2C INSPECTION.

Source: SDR 2026FA0000146 · FAA SDRS
C · 2026-02-16 Matched by certificate designator
ATA 2800

POLLUTION FOUND IN FUEL TANKS AFTER REMOVAL OF BOTH WINGS - FOLLOWING REMOVAL OF BOTH WINGS FOR REPLACEMENT OF LOWER PANELS AFTER 2C INSPECTION PERFORMED IN 2025, WE FOUND CONTAMINATION IN THE WINGS, IN THE CENTRE TANK, IN THE THREE FEEDERS’ TANKS, IN THE FILTERS AND IN THE FUEL PIPES. ANALYSES OF CONTAMINATION CONFIRMED THE PRESENCE OF ALUMINIUM POWDER, MOST PROBABLY GENERATED BY BLENDING’S IN THE CENTRE TANKS. FOLLOWING MANUFACTURER RECOMMENDATION, ALL TANKS, ALL PIPES AND ALL FILTERS NEED TO BE CLEANED. ADDITIONAL ACCESSES AND INSPECTION IN PROGRESS.

Source: SDR 2026FA0000127 · FAA SDRS
O · 2026-02-05 Matched by certificate designator
ATA 2821

DURING INSPECTION/CLEANING OF THE FUEL FILTERS, THE FILTER OF THE BOOSTER PUMP 2 WAS DISCOVERED IN THE HYDRAULIC BAY, BETWEEN HYDRAULIC PIPES. FILTER WAS NOT INSTALLED AS PER AMM.

Source: SDR 2026FA0000092 · FAA SDRS
O · 2026-01-20 Matched by certificate designator
ATA 2897

AIRCRAFT CURRENTLY IN MAINTENANCE. DURING REMOVAL OF FUEL GAUGE 1203 QJ FOUND FUEL TANK CENTER FUSE C1 HARNESS WITH SIGN OF CHAFING.

Source: SDR 2026FA0000062 · FAA SDRS
K · 2022-10-03 Matched by certificate designator
ATA 7210

RECEIVED WO TO PERFORM FWD HYD PUMP SEAL REPLACEMENT ON GEARBOX ENG#3 DUE TO SUSPECT ENGINE OIL LEAK. NOTED HYD LEAK INSTEAD OF OIL LEAK. NOTED ALSO LOWER ENGINE COWL ENGINE OIL CONTAMINATED. PERFORMED ENGINE RUN UP AND FOUND CRACK ON GEARBOX.

Source: SDR 2022F00399 · FAA SDRS
J · 2019-06-29 Matched by certificate designator
ATA 3230

APPROXIMATELY AT 12:00 PM I ARRIVED AT KHPN FROM A FLIGHT FROM KATL, AND RENTED A VEHICLE TO KTEB TO ANSWER A CALL FOR MAINTENANCE OVERSITE ON AIRCRAFT S/N-036. THE PIC DECLARED AN EMERGENCY ON LANDING INTO KTEB AIRPORT FROM KOXC AIRPORT. UPON LANDING WITH EMERGENCY LANDING GEAR EXTENSION EXECUTED, THE AIRCRAFT LANDED SAFELY. EMERGENCY VEHICLES WERE ON STANDBY AT THE AIRCRAFT JUST IN CASE, AND THE AIRCRAFT WAS TOWED WITH GEAR PINS IN PLACE, JUST AS A PRECAUTIONARY MEASURE, DUE TO THE AIRCRAFT HAVING NO STEERING AS A RESULT OF EMERGENCY LANDING GEAR EXTENSION BEING EXECUTED. UPON ARRIVAL, AT APPROX. 1330, FOUND AIRCRAFT OUTSIDE WAITING TO BE TOWED TO A HANGAR. AFTER PLACEMENT OF AIRCRAFT, JACKING TOOK PLACE AND GEAR SWINGS ENSUED FOR TROUBLESHOOTING MEASURES. AT ABOUT 1500, AND AFTER SWINGING THE GEAR SEVERAL TIMES, WE COULD NOT GET THE PROBLEM TO REOCCUR BUT THE CODES IN THE CMC STAYED LATCHED. AFTER FURTHER TROUBLESHOOTING DEEP INTO THE CMC AND PULLING CIRCUIT BREAKERS TO CLEAR CODES, CODES WOULD NOT UNLATCH AND CAME BACK, ALL TROUBLESHOOTING POINTED TO THE LGSCU (LANDING GEAR AND STEERING CONTROL UNIT). AT ABOUT 1600, UPON VERIFYING PROBLEM, ORDERED LGSCU AND LUCKILY THEY HAD A PART IN STOCK. FURTHER TESTING AT ABOUT 1700, OF CONNECTORS GROUND AND POWER PIN OUTS FOR THE LGSCU PROVED TO BE POSITIVE. NO OTHER CIRCUITS WERE INVOLVED THROUGH TESTING OF THE INPUT AND OUTPUT OF THE LGSCU. AFTER ARRIVAL OF PARTS, THE TEAM INSTALLED WITHOUT INCIDENT. TESTING AFTER LGSCU INSTALL, WENT WELL. LANDING GEAR PERFORMED WELL WITH THE HYDRAULIC MULE CONNECTED. NO LATCHED MESSAGES WERE ENCOUNTERED DURING CYCLING OF THE GEAR. THE TEAM ALSO TESTED THE SQUAT SWITCHES WITH NO DEFECTS AT THIS TIME. DOWN JACKED THE AIRCRAFT AND FINISHED THE PAPERWORK AT ABOUT 2430.

Source: SDR BKEA2019070200001 · FAA SDRS
O · 2019-03-29 Matched by certificate designator
ATA 2130

AIRCRAFT DEPARTED, ONCE THE THE AIRCRAFT HAD REACHED ALTITUDE ABOVE FL350, UNABLE TO KEEP PRESSURE CONTROL EITHER VIA AUTO OR MANUAL, CABIN CLIMB OR DESCENT VARIES AT ABOUT 450FPM.BELOW FL340 NORMAL OPS.AIRCRAFT RETURNED TO FOR REPAIRS

Source: SDR BKEA201904010001 · FAA SDRS
B · 2001-02-11 Matched by certificate designator
ATA 3460

ELECTRICAL FUMES NOTED ON FINAL APPROACH. SOURCE OF FUMES WAS DETERMINED TO BE THE FMS. THE FMS WAS MEL''D ON FEBRUARY 10, 2001 FOR THE SAME PROBLEM. THE UNIT WAS DEACTIVATED PER EO8-34-01-629, UNIT CONTINUED MEL''D.

Source: SDR HNAA0100013 · FAA SDRS
W · 2000-02-13 Matched by certificate designator
ATA 5320

FOUND 3 RIVETS MISSING IN STRINGER 31S TO FRAME X167 GUSSET JOINT. ONE HOLE HAD A CLECO STILL INSTALLED FROM FACTORY. REMOVED CLECO AND INSTALLED RIVETS.

Source: SDR HNAA0000019 · FAA SDRS
O · 2000-02-04 Matched by certificate designator
ATA 3220

AFTER TAKEOFF, THE NOSE LANDING GEAR WOULD NOT RETRACT. AIRCRAFT RETURN TO THE AIRPORT. FOUND NOSE LANDING GEAR GROUND LOCK WAS STILL ENGAGED. GROUND LOCK WAS PROPERLY STOWED.

Source: SDR HNAA0000015 · FAA SDRS
L · 1999-12-06 Matched by certificate designator
ATA 3350

LEFT FWD EMERGENCY LIGHT INOP. REMOVED AND REPLACED 3352-P2 POWER SUPPLY BASE AND 3351-PS3 POWER SUPPLY.

Source: SDR HNAA9900165 · FAA SDRS
L · 1997-01-27 Matched by certificate designator
ATA 3350

FLT 3416 - FLL-TPA - DURING PREFLIGHT CHECKS, THE INTERIOR AND EXTERIOR LIGHTS ILLUMINATED WITH SWITCH IN OFF POSITION. REMOVED AND REPLACED DIODE 3351-CR5 AND POWER SUPPLY BASE FOR 3351-PS2. (M)

Source: SDR HNAA9799008 · FAA SDRS
L · 1997-01-27 Matched by certificate designator
ATA 3350

FLT 3416 - FLL-TPA - DURING PREFLIGHT CHECKS, THE INTERIOR AND EXTERIOR LIGHTS ILLUMINATED WITH SWITCH IN OFF POSITION. REMOVED AND REPLACED DIODE 3351-CR5 AND POWER SUPPLY BASE FOR 3351-PS2. (M)

Source: SDR 97ZZZM240 · FAA SDRS
L · 1996-08-13 Matched by certificate designator
ATA 3350

TLH/MCO - FLT 3085 - DURING PRE-FLIGHT CHECKS, FOUND FIRST AND THIRD OVERHEAD EMERGENCY LIGHTS INOPERATIVE. SWAPPED POWER SUPPLIES PS3 AND PS2, ALL OPERATIONS NORMAL. (X)

Source: SDR HNAA9699056 · FAA SDRS