N992AF
Registered owner: UAS TRANSERVICES INC, FL (owner ≠ operator)
Operators of this aircraft
Who operated this tail, and how firmly we know it.
| Operator | Role | Period | Basis |
|---|---|---|---|
| AMERIFLIGHT, LLC (JIKA) | Certificate holder | — | Matched by certificate designator |
Accident & incident history
Maintenance disclosures
DURING CRUISE FLIGHT WITH THE AUTO PILOT ACTIVE THE FLIGHT CREW NOTICED THE #1 FUEL FLOW GAUGE WAS NOT WORKING. AFTER PERFORMING SEVERAL CHECKS RELATED TO THE INDICATOR, HE VISUALLY CHECKED THE LEFT WING AND NOTICED FUEL FLOWING OUT OF THE ENGINE NACELLE. HE NOTIFIED ATC AND PERFORMED AN IN-FLIGHT SHUTDOWN OF THE AFFECTED ENGINE FOLLOWED BY AN EMERGENCY LANDING. THE AIRCRAFT LANDED SAFELY WITHOUT FURTHER INCIDENT. MAINTENANCE FOUND THAT THE O-RING FOR THE FUEL LINE TO THE FUEL/ OIL HEATER HAD DETERIORATED AND FAILED IN FLIGHT. THEY REPLACED THE FAULTY PACKING AND PERFORMED MULTIPLE LEAK CHECKS TO INCLUDE ENGINE POWER ON. NO OTHER DEFECTS WERE NOTED, AND THE AIRCRAFT WAS RETURNED TO SERVICE.
DURING CLIMBOUT, PILOT REPORTED SMOKE IN THE COCKPIT WITH THE LEFT BLEED AIR ON. TURNED OFF BLEED AIR AND RETURNED TO THE AIRPORT. NO EMERERGENCY DECLARED. MAINTENANCE HAD CONDUCTED A POWER RECOVERY WASH ON THE ENGINES PRIOR TO FLIGHT, IT WAS DISCOVERED THAT THERE WAS RESIDUAL SOAP IN THE COMPRESSOR WHICH THEN VAPORIZED & BURNED WHEN THE ENGINE WAS RUNNING, AND THE SMOKE CAME INTO THE COCKPIT WHEN THE BLEEDS WERE TURNED ON.