N992AF

BEECH C-99 · 1983 · Valid Registration

Registered owner: UAS TRANSERVICES INC, FL (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AMERIFLIGHT, LLC (JIKA)Certificate holderMatched by certificate designator

Accident & incident history

Incident · 2001-05-14 Matched by aircraft (N-number)
Beech C-99 None injuryAMERIFLIGHT, LLC
Source: NTSB case SEA01IA093

Maintenance disclosures

K · 2024-06-27 Matched by certificate designator
ATA 7312

DURING CRUISE FLIGHT WITH THE AUTO PILOT ACTIVE THE FLIGHT CREW NOTICED THE #1 FUEL FLOW GAUGE WAS NOT WORKING. AFTER PERFORMING SEVERAL CHECKS RELATED TO THE INDICATOR, HE VISUALLY CHECKED THE LEFT WING AND NOTICED FUEL FLOWING OUT OF THE ENGINE NACELLE. HE NOTIFIED ATC AND PERFORMED AN IN-FLIGHT SHUTDOWN OF THE AFFECTED ENGINE FOLLOWED BY AN EMERGENCY LANDING. THE AIRCRAFT LANDED SAFELY WITHOUT FURTHER INCIDENT. MAINTENANCE FOUND THAT THE O-RING FOR THE FUEL LINE TO THE FUEL/ OIL HEATER HAD DETERIORATED AND FAILED IN FLIGHT. THEY REPLACED THE FAULTY PACKING AND PERFORMED MULTIPLE LEAK CHECKS TO INCLUDE ENGINE POWER ON. NO OTHER DEFECTS WERE NOTED, AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR JIKA2024062801 · FAA SDRS
B · 2012-04-28 Matched by certificate designator
ATA 7230

DURING CLIMBOUT, PILOT REPORTED SMOKE IN THE COCKPIT WITH THE LEFT BLEED AIR ON. TURNED OFF BLEED AIR AND RETURNED TO THE AIRPORT. NO EMERERGENCY DECLARED. MAINTENANCE HAD CONDUCTED A POWER RECOVERY WASH ON THE ENGINES PRIOR TO FLIGHT, IT WAS DISCOVERED THAT THERE WAS RESIDUAL SOAP IN THE COMPRESSOR WHICH THEN VAPORIZED & BURNED WHEN THE ENGINE WAS RUNNING, AND THE SMOKE CAME INTO THE COCKPIT WHEN THE BLEEDS WERE TURNED ON.

Source: SDR JIKA2012042801 · FAA SDRS