Awesome Flight, LLC.

Part 135 operator · designator 2AFA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: Awesome Flight, LLC.

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

3 reports on file.

O · 2025-12-04 Matched by certificate designator
N326AG · ATA 2300

RIGHT ACP NOT WORKING AND STUCK MIC DURING CRUISE, FLIGHT CREW RETURNED TO BASE. R & R REMOTE ELECTRONIC UNIT IAW WITH SAAB 340 AMM 23-50-05-04, OPS TEST SATISFACTORY.

Source: SDR 4EZF2025120800001 · FAA SDRS
E F · 2017-07-19 Matched by certificate designator
N188DD · ATA 6310

FAILURE OF ACTUATOR ASSEMBLY. THE BRACKETS DISCONNECTING THAT CAUSED THE UPPER BREAK.” MR. WEBSTER ALSO STATED THIS WAS A “MAINTENANCE ISSUE THAT SHOULD HAVE BEEN ADDRESSED. WE HAVE A SERVICE BULLETIN OUT JUST FOR THAT.” HOWEVER, UNDER THE CURRENT SERVICE BULLETIN 94 THE INSPECTION REQUIREMENT WAS ONLY DUE TO BE INSPECTED “AT THE NEXT 100-HOUR INSPECTION OR ANNUAL INSPECTION, WHICHEVER OCCURS FIRST.” IT IS IMPORTANT TO NOTE THAT WHEN THIS SERVICE BULLETIN WAS PUBLISHED THE HELICOPTER WAS NOT YET DUE FOR ITS NEXT 100-HOUR INSPECTION. THE FAILURE OCCURRED PRIOR TO THE NEXT 100 HOUR INSPECTION WHICH WAS DUE IN 13 HOURS.

Source: SDR 2AFA20170719001 · FAA SDRS
E R · 2012-02-18 Matched by certificate designator
N188DD · ATA 8530

REMOVAL OF THE NR 1 CYLINDER FOR VISUAL INSPECTION REVEALED A FAILURE OF THE INTAKE VALVE. ENGINE MONITOR SHOWED MASSIVE INGESTION OF ENGINE OIL INTO REMAINING CYLINDERS CAUSING LOSS OF POWER FROM OIL FOULING OF UNAFFECTED SPARK PLUGS. AFFECTED CYLINDER SHOWED CATASTROPHIC DAMAGE TO PISTON AND COMBUSTION AREA FROM MULTIPLE PHYSICAL CONTACT. VALVE FURTHER FRACTURED AND PARTS BECAME WEDGED IN THE INDUCTION TUBE AS WELL AS THE COMMON MANIFOLD AREA. WHEN THE INTAKE ROCKER ASSEMBLY WAS REMOVED ALONG WITH THE CAP, DISCOVERED THE TOP OF VALVE, ABOVE VALVE KEYS WAS THE AREA OF SEPARATION AND FAILURE. VISUAL INSPECTION WITH A 30X MICROSCOPE, MECHANIC'S CONSIDERED OPINION THAT THE FAILURE OF THE INTAKE VALVE MAY HAVE BEEN CAUSED FROM A STRESS RISER CREATED DURING MANUFACTURING AT EITHER THE MACHINING, HEAT TREATING PROCESS, OR PERHAPS WAS AT A MOLECULAR LEVEL DURING THE CREATION OF THE RAW MATERIAL. IT SHOULD BE DULY NOTED THAT THE AIRCRAFT WAS IN COMPLIANCE WITH SERVICE BULLETIN SB388C EXACTLY 85.8 HOURS EARLIER AND NO DEFECT OR ABNORMALITIES WERE NOTED AT THE TIME OF THE INSPECTION.

Source: SDR 2AFA20120218001 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N326AGROBINSON HELICOPTER CO R662014Valid RegistrationMatched by certificate designator