HALO FLIGHT INC

Part 135 operator · designator H7FA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: HALO FLIGHT INC

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

4 reports on file.

K · 2024-05-31 Matched by certificate designator
N30HF · ATA 2150

AIR COMM AIR CONDITIONING SYSTEM HIGH PRESSURE LINE LOCATED AT COMPRESSOR TO ENGINE DECK CONTINUOUSLY LEAKING AND HAVING TO REPLACE. THIS LINE DOES NOT LEAK AT THE SAME POINT ALL THE TIME BUT AT DIFFERENT LOCATIONS. WE HAVE REPLACED 4 LINES NOW IN 221.4 HRS OF OPERATION.

Source: SDR 2024FA0000415 · FAA SDRS
C · 2016-11-12 Matched by certificate designator
N30HF · ATA 7712

PILOT EXPERIENCED HIGH TORQUE INDICATION ON INSTRUMENT. TROUBLESHOOTING WAS PERFORMED AND FOUND TO BE INTERNAL TO THE ENGINE GEARBOX TORQUEMETER. UPON REMOVAL OF ENGINE, DELIVERY TO OVERHAUL FACILITY, AND DISASSEMBLY OF GEARBOX AND TORQUEMETER, PLASTIC MEDIA WAS DISCOVERED INTERNAL TO TORQUEMETER.

Source: SDR 2016F00236 · FAA SDRS
O · 2004-04-06 Matched by certificate designator
N30HF · ATA 1430

THE ENGINE WAS SPLIT AT THE (C) FLANGE. AFTER REMOVAL OF THE C.T. DISC, IT WAS NOTED THAT 2 BOLTS HOLDING THE INNER EXIT DUCT TO THE ENGINE HAD SHEARED OFF AND WERE LODGED IN THE AREA, WITH THE REMAINDER OF THE BOLT SHANKS LEFT IN THE BOLT HOLES. DAMAGE WAS NOTED ON THE C.T. DISC. SAFETY WIRE WAS PRESENT IN ALL THE BOLTS INCLUDING THE SHEARED BOLT HEADS.

Source: SDR 040604 · FAA SDRS
O · 2004-03-24 Matched by certificate designator
N30HF · ATA 7230

PILOT REPORTS (GRINDING) SOUND WHEN PROPELLER IS SPUN BY HAND. THE ENGINE WAS SPLIT AT THE (C) FLANGE WHERE DEBRIS WAS NOTED AT THE 6 O'CLOCK AREA BETWEEN THE COMPRESSOR TURBINE BLADES AND SHROUD SEGMENTS. AFTER REMOVAL OF THE CT DISK, IT WAS NOTED THAT FOUR BOLTS HOLDING THE INNER EXIT DUCT TO THE ENGINE WERE MISSING. THE DEBRIS WERE THE REMAINS OF THE FOUR BOLTS. SAFETY WIRE WAS NOT PRESENT IN THE REMAINING FOUR BOLTS. 370 HOURS SINCE ENGINE O/H.

Source: SDR 033104 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N30HFBELL 4072007Valid RegistrationMatched by certificate designator
N31HFMatched by certificate designator
N33HFBELL HELICOPTER TEXTRON CANADA 4072015Valid RegistrationMatched by certificate designator
N429HFBELL HELICOPTER TEXTRON CANADA 4292013Valid RegistrationMatched by certificate designator