DYNAMIC VENTURES INC

Part 135 operator · designator 8DYA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: DYNAMIC VENTURES INC

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

6 reports on file.

O · 2009-05-12 Matched by certificate designator
N441JK · ATA 5210

DURING THE SID INSP THE UPPER CABIN DOOR WAS REMOVED FOR INSP. THE HINGE PIVOT BOLTS COULD NOT BE REMOVED BECAUSE THE BOLTS, BUSHINGS AND BRGS WERE ALL RUSTED SOLID. THIS CAUSED THE BOLTS TO PIVOT IN THE FUSELAGE STRUCTURE INSTEAD OF THE BEARINGS CAUSING EXCESSIVE WEAR OF THE FUSELAGE DOOR MOUNT HOLES. THERE IS NO REQUIREMENT TO REMOVE THE UPPER DOOR EXCEPT DURING THE SID INSP CALLED OUT IN THE LATEST MANUAL REVISION NR 16.

Source: SDR 2009FA0000406 · FAA SDRS
O · 2009-05-12 Matched by certificate designator
N441JK · ATA 3230

DURING THE SID INSP THE NLG WAS REMOVED FOR INSP. THE DRAG BRACE RT BRG PLATE HOLES WERE ALL FOUND EXCESSIVLY ELONGATED REQUIRING STRUCTURAL REPAIR. SUSPECT DAMAGE WAS CAUSED BY NORMAL TOWING OVER THE LIFE OF THE ACFT. THIS WOULD NOT BE DETECTED UNLESS THE NOSE GEAR IS REMOVED AS REQUIRED BY THE SID INSP CALLED OUT IN THE LATEST MANUAL REVISION 16.

Source: SDR 2009FA0000407 · FAA SDRS
O · 2009-05-12 Matched by certificate designator
N441JK · ATA 3213

DURING THE SID INSP OF THE MLG TRAILING LINK, THE PIVOT PIN WAS FOUND TO HAVE EXCESSIVE AMOUNTS OF RUST AND PITS.

Source: SDR 2009FA0000408 · FAA SDRS
O · 2009-05-12 Matched by certificate designator
N441JK · ATA 3211

WITH THE LT MAIN GEAR REMOVED FROM THE WING FOR SID INSP, THE AFT TRUNNION BRG WAS FOUND VERY LOOSE IN THE AFT TRUNNION SUPPORT.

Source: SDR 2009FA0000409 · FAA SDRS
B · 2003-09-24 Matched by certificate designator
N441JK · ATA 7500

REPORTED SMOKE IN COCKPIT UPON TAKEOFF. A/C RETURNED IMMEDIATELY AND PERFORMED NORMAL LANDING. INSP REVEALED A CRACKED V-BRAND CLAMP CONNECTING BLEED AIR SUPPLY LINES IN RT WING ROOT AREA ADJACENT TO SURFACE DEICE PRESSURE REGULATORS. SMOKE WAS DETERMINED TO ORIGINATE FROM A PLASTIC/VINYL HOSE INSIDE CABIN ADJACENT TO FUSELAGE SKIN WHICH HAD BURNED AND MELTED. SUSPECT HEAT FROM BLEED AIR SUPPLY LINES CAUSED LOCAL AREA TO CONDUCT HEAT THROUGH THE SKIN TO THE EXTENT NECESSARY TO MELT THE TUBING. INSP REVEALED NO OTHER APPARENT HEAT RELATED DAMAGE. SUBMITTER NOTES THAT THE CRACK IN THE V-BAND CLAMP OCCURRED AT JUNCTION OF BARREL BOLT, AND NO SAFETY DEVICES WERE INCORPORATED ON ANY OF CLAMPS IN AREA.

Source: SDR 2003FA0001068 · FAA SDRS
O · 1996-04-22 Matched by certificate designator
N6860C · ATA 5730

INBOARD FORWARD SIDE OF RIGHT INBOARD FLAP IS CHAFING INTO THE SKIN AT THE WING STUB. FITTING PN 5825017-1 OR PN 5825017-2, WHICH IS RIVETED TO THE FORWARD INBOARD SIDE OF THE RIGHT INBOARD FLAP, IS CHAFING AGAINST THE WING SKIN.

Source: SDR 96ZZZX2472 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N441JKMatched by certificate designator
N6860CCESSNA 4411982Registration pendingMatched by certificate designator