Meridian Air Group, Inc.
Also recorded as: Meridian Air Group, Inc.
Accident & enforcement record
Events that happened, regardless of the operator's own reporting. Each links to its public source.
NTSB accidents & incidents
No NTSB accidents or incidents linked to this operator.
FAA enforcement actions
FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.
Maintenance disclosure history
Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.
313 reports on file — showing most recent 50.
LT MLG OUTBOARD FLYING DOOR. THE ARTICULATING DOOR HINGE HAS A FAIR AMOUNT OF MOVEMENT VERTICALLY. REMOVED, LOCATED AND DRILLED WORN HINGE SECTION AND INSTALLED HINGE SECTION AND FLYING DOOR.
AFT END OF XCW 42 RIBS IS TORN ABOUT MIDWAY UPPER WEB. FABRICATED FILLER AND REPAIRED DOUBLER, LOCATED AND DRILLED FILLER AND DOUBLER, INSTALLED FILLER AND DOUBLER.
AFT CARGO COMPARTMENT INTERCOSTAL AT LONGERON 29 RIGHT HAS GOUGES ALONG AFT END AT STATION 785. REMOVED INTERCOSTAL, DRILLED UP AND INSTALLED NEW INTERCOSTAL.
INTERCOSTAL AT FRAME STATION 340 BETWEEN LONGERON 28 AND 29 DAMAGED. REMOVED INTERCOSTAL, FIT AND DRILLED UP AND INSTALLED NEW INTERCOSTAL.
AFT CARGO LONGERON 29 RIGHT HAS ELONGATED HOLES TWO EACH STATION 785 FRAME LOCATION. FABRICATED AND INSTALLED SECTION OF LONGERON. REMOVED AND INSTALLED SHOVEL CLIP.
FASTENER HOLES AT FRAME STATION 785 AND LONGERON 22 LEFT IS CRACKED. FABRICATED, LOCATED AND DRILLED AND INSTALLED FRAME SPLICE. REMOVED AND INSTALLED SHEAR TIE.
FASTENER HOLES DAMAGED IN CENTER TANK ON STRINGER 17 AFT SPLICE PLATE APPROXIMATELY 1 INCH LEFT OF STATION 0 BULKHEAD. SPOTFACED HOLE TO REMOVE DAMAGE, FABRICATED AND INSTALLED FASTENERS IN STRAP.
CENTER TANK FORWARD SPAR ACCESS WEB 8 EACH INSULATION ATTACH CLIPS REQUIRE REMOVAL TO FACILITATE OTHER MAINTENANCE. REMOVED AND INSPECTED CLIPS, FABRICATED AND INSTALLED CLIPS.
INTERCOSTAL AT FRAME STATION 332 BETWEEN LONGERON 28 AND 29 DAMAGED. REMOVED INTERCOSTAL, FABRICATED FIT AND DRILLED CLIPS AND INTERCOSTAL, INSTALLED INTERCOSTAL AND CLIP.
AT STATION 766 LONGERON 29 RIGHT INTERCOSTAL FORWARD ATTACH CLIP HAS ELONGATED HOLE. REMOVED ATTACH CLIP, FABRICATED AND INSTALLED CLIP.
REMOVED INTERCOSTAL FROM STATION 785 TO 800 AT LONGERON 29 RIGHT TO FACILITATE MAINTENANCE. FOUND ELONGATED HOLES. LOCATED AND DRILLED INTERCOSTAL, INSTALLED INTERCOSTAL.
REMOVED SHEAR TIE AT STATION 785 FROM LONGERON 21 LEFT TO 27 LEFT TO FACILITATE MAINTENANCE. SHEAR TIE HAS SEVERAL ELONGATED HOLES, LOCATED AND DRILLED AND INSTALLED SHEAR TIE.
STATION 930 FRAME AT THE RIGHT DORSAL FIN ATTACH ANGLE HAS A FASTENER PULLING THROUGH. REMOVED 2 HI-LOKS FROM RIGHT SIDE, REAMED 2 HOLES, FABRICATED AND INSTALLED SLEEVE BUSHING.
STATION 930 AT THE LEFT DORSAL FIN ATTACH ANGLE HAS TWO FASTENERS PULLING THROUGH. REMOVED 2 HI-LOKS, FABRICATED AND INSTALLED SLEEVE BUSHINGS.
FORWARD CARGO COMPARTMENT LOWER DOOR JAMB HAS SEVERAL AREAS OF MODERATE CORROSION STATION 312 TO 370. REMOVED DAMAGED SECTION FIT, DRILLED SECTION AND INSTALLED NEW SECTION.
FORWARD CARGO COMPARTMENT FLOOR SUPPORT AT STATION 218 HAS SEVERAL AREAS LIGHT CORROSION LONGERON 30 TO 28 RIGHT DOT 469. HEAT TREATED 2 DOUBLERS, LOCATED AND DRILLED DOUBLER, INSTALLED REPAIR DOUBLER, LOCATING AND DRILLED REMAINING FLOOR LINING, INSTALLED 2 NUT PLATES.
RIGHT WING XCW 58 LOWER WING TEE REQUIRES REPAIR OR REPLACEMENT DUE TO CORROSION REMOVAL. REMOVED WING TEE, RECEIVED NEW WING TEE, LOCATED AND DRILLED AND INSTALLED WING TEE.
INTERCOSTAL AT LONGERON 29 BETWEEN FRAME STATION 313 AND 370 HAS A LARGE HOLE ON UPPER AFT END. REMOVED AND INSTALLED INTERCOSTAL.
NOSE SKIN HAS 4 POSSIBLE CRACKS AT STATION 76.6, 18 INCHES LEFT OF CENTER AREA NEEDS TO BE STRIPPED AND VERIFIED. VERIFIED CRACKS LOCATED AND DRILLED PILOT HOLES AND FABRICATED DOUBLER.
INTERCOSTAL AT FRAME STATION 320 BETWEEN LONGERON 28 AND LONGERON 29 DAMAGED. FIT AND DRILLED INTERCOSTAL, REMOVED AND INSTALLED INTERCOSTAL.
AT FRAME STATION 786 FRAME TO SKIN SHEAR TIE HAS NUMEROUS ELONGATED HOLES FROM LONGERON 30 TO 27 LEFT. LOCATED AND DRILLED SHEAR TIE, REMOVED AND INSTALLED SHEAR TIE.
INTERCOSTAL AT FRAME STATION 360 BETWEEN LONGERON 29 DAMAGED. FIT AND DRILLED INTERCOSTAL REMOVED AND INSTALLED INTERCOSTAL.
INTERCOSTAL AT FRAME STATION BETWEEN LONGERON 28 AND 29 DAMAGED. FIT AND DRILLED INTERCOSTAL REMOVED AND INSTALLED INTERCOSTAL.
FORWARD CARGO COMPARTMENT HAS LIGHT CORROSION ON INTERCOSTAL AT STA 218-237 BETWEEN LONGERON 28R-27R. DRILLED UP NEW INTERCOSTAL, REMOVED AND INSTALLED INTERCOSTAL.
FORWARD CARGO DOOR HAS A CRACKED INTERCOSTAL OUTBOARD OF LOWER AFT STOP FITTINGS BELOW BEAM 1. LOCATED AND DRILLED INTERCOSTAL. REMOVED AND INSTALLED INTERCOSTAL.
LEFT ENGINE OIL TEMPERATURE IS PEGGED. PRESSURE AND QUANTITY IS NORMAL PER QRH. ENGINE NOT SHUT DOWN WITHIN 15 MINUTE LIMIT WHEN AIRCRAFT LANDED AT MILWAUKEE. FUEL TEMPERATURE ALSO DID NOT INCREASE. REPAIRED AND REPLACED LEFT ENGINE OIL TEMPERATURE CONNECTOR AND TEMPERATURE BULB.
AT CRUISE ALT LEFT ENGINE MASTER CAUTION, LEFT ENGINE OIL PRESSURE LOW ANNUNCIATOR ON. LEFT ENGINE OIL PRESSURE IS ZERO. LEFT OIL TEMP IS 20 DEGREES CELSIUS AND QUANTITY IS 17-18 QUARTS. SHUT DOWN BY SELECTION. REMOVED AND REPLACED ENGINE.
UNABLE TO RAISE LANDING GEAR AFTER TAKE OFF UNABLE TO TURN NOSE WHEEL AND NO AUTO PRESSURIZATION INITIALLY BUT IT STARTED WORKING 15 MINUTES INTO FLIGHT. RIGGED GROUND SENSING CABLES.
RIGHT ENGINE OIL QUANTITY DROPPED TO 4.5 QUARTS ALL OTHER INDICATIONS NORMAL. MAINTENANCE SERVICED ENGINE OIL AND RESECURED OIL CAP.
INTERCOSTAL AT STATION 817 AND LONGERON 3 LEFT IS CRACKED ON LOWER FLANGE. FABRICATED AND INSTALLED DOUBLER REPAIR.
FORWARD CARGO DOOR PAN, AFT SIDE MODERATELY CHAFED ON RADIUS, NEXT TO DOOR LATCH. FABRICATED AND INSTALLED DOUBLER.
FRAME IS CHAFED ON FORWARD SIDE IN AFT ACCCESSORY AT STATION 860 BETWEEN LONGERONS LEFT 5 AND LEFT 6. FABRICATED AND INSTALLED FRAME REPAIR PARTS.
LEFT SIDE AFT PRESSURE BULKHEAD SIDE STATION Z=34, 6 INCHES OUTBOARD OF DOOR CUTOUT FINGER DOUBLER IS CRACKED AROUND Z-RIVETS. ALSO AT STATION 40 FINGER DOUBLER HAS CRACK AROUND 1 RIVET. FABRICATED AND INSTALLED FINGER DOUBLER.
PASSENGER DOOR INTERCOSTAL IS CRACKED IN THE FLANGE AT HANDLE ASSY. REMOVED AND REPLACED INTERCOSTAL.
PASSENGER DOOR HANDLE HOUSING CRACKED. REMOVED AND REPLACED HOUSING.
MKE - FLT 132 - THE NR 2 NAVIGATIONAL RECEIVER IS INOPERATIVE ON VOR FREQUENCIES. REMOVED AND REPLACED NR 2 NAVIGATIONAL RECEIVER. (M)
CORROSION ON BOTTOM SIDE OF NR 4 SEAT TRACK AROUND FASTENER HOLES AT STATIONS 255 TO 264. FABRICATED AND INSTALLED SEAT TRACK SPLICE.
AFT CARGO COMPARTMENT FITTINGS FOR AFT CARGO DOOR HAVE ELONGATED HOLES WHERE CARGO DOOR HINGE THRU-BOLT GOES. FABRICATED AND INSTALLED BUSHING PLATES.
FUSELAGE SKIN HAS PUNCTURE ON RIGHT SIDE, STATION 897. FABRICATED AND INSTALLED REPAIR DOUBLER.
LEFT ELEVATOR TOP SKIN IS OIL CANNING AT STATION XHS 170. FABRICATED AND INSTALLED SKIN.
RIGHT INBOARD BUTE DOOR INBOARD RECEPTICAL BRACKET HAS NUT PLATES. INSTALLED WHERE CAMLOC RECEPTICALS SHOULD BE. FABRICATED AND INSTALLED SKIN DOUBLER, REPAIR ANGLE, AND INTERNAL DOUBLER.
ELONGATED HOLE ON AFT SPAR ATTACH ANGLE LEFT WING STATION XRS 161.7. FABRICATED AND INSTALLED REPAIR ANGLES. INSTALLED, FABRICATED REPAIR DOUBLER.
STATION 817 LOWER BULKHEAD WEB HAS SEVERAL TOOL MARKS ON THE FORWARD SIDE OUTBOARD OF LONGERON 27 RIGHT TO LONGERON 27 LEFT. FABRICATED AND INSTALLED DOUBLERS.
STRINGER 19 HAS CORROSION ON LOWER FORWARD FLANGE AT STATION 101. DRILLED AND INSTALLED NEW STRINGER SECTION 19 AND SPLICES.
GALLEY SERVICE DOOR HAS AN EXTERNAL SKIN DING BETWEEN NUMBER 3 AND 4 BEAM, 3 INCHES INBOARD OF VERTICAL INTERCOSTAL. FABRICATED AND INSTALLED REPAIR DOUBLER.
CABIN SUBFLOOR HAS AREAS OF LIGHT CORROSION AND BARE METAL BETWEEN STATION 275 TO 294 ADJACENT TO LONGERON 181 RIGHT. FABRICATED AND INSTALLED REPAIR PARTS AND BRACKET.
RIGHT PYLON HAS A CHAFED FRAME LOCATED AFT OF HYDRAULIC FLEX LINES. FABRICATED AND INSTALLED REPAIR DOUBLER.
RIGHT PYLON TRAILING EDGE ATTACH STRUCTURE IS CRACKED AT FORWARD INBOARD NUT PLATE ON TOP SIDE. FABRICATED AND INSTALLED NEW ANGLE.
LEFT ENGINE PYLON BOX AREA DIVIDER CRACKED THRU RIVET HOLES AFT OF THE AFT SPAR BOTTOM ATTACH AREA. STOP DRILLED CRACK. FABRICATED AND INSTALLED REPAIR ANGLES.
FIRST OFFICER I/B SEAT TRACK HOLES ELONGATED BEYOND .375 INCHES. FABRICATED AND INSTALLED DOUBLER. FABRICATED AND INSTALLED SEAT TRACK.
Linked aircraft
| N-number | Make / model | Year | Status | Link basis |
|---|---|---|---|---|
| N439WC | PILATUS PC-12/45 | 2002 | Valid Registration | Matched by certificate designator |
| N561ST | PILATUS PC-12/45 | 2004 | Valid Registration | Matched by certificate designator |
| N842MA | SOCATA TBM 700 | 2007 | Valid Registration | Matched by certificate designator |
| N900ME | SOCATA TBM 700 | 2014 | Valid Registration | Matched by certificate designator |