GOLDEN WEST AIRLINES, LLC

Part 135 operator · designator 3GWA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: FLYHOUSE, GOLDEN WEST AIRLINES, LLC

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

3 reports on file.

M · 2025-11-12 Matched by certificate designator
N163JW · ATA 7200

AT FL380, DESCENDED TO FL240. DISCONNECTED THE AUTOTHROTTLES & PULLED THE ENGS TO IDLE. ACFT STARTED TO SHAKE WITH A LOW FREQUENCY. IMMEDIATELY CHECKED IF SPOILERS DEPLOYED AS IT FELT LIKE AN INTENSIFIED SPOILER DEPLOYMENT. THERE WAS NO SPOILER DEPLOYMENT. GOT A RED LT ENGINE TGT ICAS MESSAGE & SAW NEEDLE IN RED ARC WHILE BOTH ENGS AT IDLE. PERFORMED APPLICABLE CHKLIST & PERFORMED AN ENGINE SHUTDOWN OF LT ENG. DECLARED AN EMERGENCY WITH ATC. ONCE ENG SHUTDOWN & SECURED, AIRCRAFT FLEW NORMAL FOR SINGLE ENG OPS. NO VIBRATION. CONTINUED TO KVNY AS WE HAD ALREADY PASSED KLAS AND I WOULD HAVE DONE A SLOW AND STABLE DESCENT INTO VAN NUYS. ONCE LANDED, FIRE TRUCKS WERE WAITING. TAXI’D INTO FBO WITHOUT INCIDENT. AFTER PAX DISEMBARKED, CHECKED THE EXCEEDANCES PAGE & NONE LISTED. LOOKED AT HP FAN BLADES & SEEMED OK. THERE WAS NO OIL THAT WAS ABNORMAL UNDERNEATH ENG OR ANY FUEL LEAKS.

Source: SDR 3GWA2025111200270 · FAA SDRS
K · 2025-05-19 Matched by certificate designator
N163JW · ATA 2820

ON THURSDAY 15 MAY 2025 GIV N163JW S/N 1071 DEPARTED KVNY GOING TO MMTL. DURING TAKEOFF ONE OF THE PASSENGERS NOTICED FUEL SPRAYING OFF THE OUTBOARD RIGHT WING. THE CREW CALLED ATC STATED THEIR PROBLEM AND ASKED TO RETURN TO KVNY, AT WHICH TIME THE TOWER DECLARED IT AN EMERGENCY. WHILE TURNING AROUND TO COME BACK TO KVNY THE FUEL STOPPED SPRAYING AFTER ABOUT 10. MINUTES. FOUND A BUILDUP OF A CORROSION PREVENTATIVE PRIMER CAUSING THE FLOAT VALVE TO STICK AND HANGUP. THEY CLEANED THE VALVE AND PERFORMED OPERATIONAL CHECK WITH NO DEFECTS NOTED. I ELECTED TO ALSO PERFORMED A MAINTENACE CHECK FLIGHT TO VERIFY THE ISSUE WAS FIXED NO DEFECTS NOTED DURING OR AFTER THE FLIGHT

Source: SDR 3GWA2025051900362 · FAA SDRS
E · 2011-03-06 Matched by certificate designator
N769MS · ATA 2435

STARTER GENERATOR DEVELOPED VIBRATIONS IN FLIGHT. STARTER GEN CONTINUED TO WORK. AFTER REMOVAL, AT FIRST LOOK IT SEEMED THAT BEARING HAD DETERIORATED. MFG TOOK STARTER GENERATOR FOR TEARDOWN.

Source: SDR 2011FA0000229 · FAA SDRS

Linked aircraft

No aircraft currently linked.