AERODYNAMIC JETS, LLC

Part 135 operator · designator L99A

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: AERODYNAMIC JETS, LLC, Copper River Air Taxi, LLC

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

2 reports on file.

E · 2024-11-01 Matched by certificate designator
N125DG · ATA 7250

FLIGHT CREW CONTACTED WILLIAMS INTERNATIONAL (W.I.) OEM PRODUCT SUPPORT TO REPORT A VIBRATION ISSUE ON THE LEFT-HAND ENGINE INSTALLED ON THE AIRCRAFT. W.I. PRODUCT SUPPORT RECOMMENDED A VIBRATION SURVEY. AN AUTHORIZED SERVICE FACILITY COMPLETED THE VIBRATION SURVEY AND CONTACTED W.I. PRODUCT SUPPORT TO REPORT VIBRATION LEVELS EXCEEDING LIMITS ESTABLISHED IN THE FJ44-3A LINE MAINTENANCE MANUAL, ELEVATED INTER-TURBINE TEMPERATURE (ITT) INDICATION, AND EVIDENCE OF AN OIL LEAK. OEM PRODUCT SUPPORT THEN RECOMMENDED A BORESCOPE INSPECTION OF THE ENGINE; HOWEVER, THE SERVICE FACILITY PERFORMED A GROUND-RUN ON THE ENGINE TO TROUBLESHOOT THE ELEVATED ITT AND OIL LEAK ISSUES, AND DURING THAT RUN, THE LEFT-HAND ENGINE BEGAN TO EXHIBIT UNUSUAL NOISES, AND SMOKE WAS OBSERVED TO BE EMANATING FROM THE TAILPIPE. PRODUCT SUPPORT THEN DIRECTED REMOVAL OF THE ENGINE FOR SHIPMENT TO THE REPAIR STATION FOR DISASSEMBLY AND EVALUATION OF ENGINE COMPONENTS. ENGINE DISASSEMBLY REVEALED ONE PARTIALLY RELEASED HIGH-PRESSURE TURBINE (HPT) BLADE TIP AND THE NO. 3 BEARING EXHIBITED DAMAGE. ADJACENT STATIC ENGINE HOT-SECTION COMPONENTS EXHIBITED SECONDARY DAMAGE FROM THE HPT BLADE ANOMALY.

Source: SDR 2024F00270 · FAA SDRS
E · 2024-11-01 Matched by certificate designator
N125DG · ATA 7250

FLIGHT CREW CONTACTED WILLIAMS INTERNATIONAL (W.I.) OEM PRODUCT SUPPORT TO REPORT A VIBRATION ISSUE ON THE LEFT-HAND ENGINE INSTALLED ON THE AIRCRAFT. W.I. PRODUCT SUPPORT RECOMMENDED A VIBRATION SURVEY. AN AUTHORIZED SERVICE FACILITY COMPLETED THE VIBRATION SURVEY AND CONTACTED W.I. PRODUCT SUPPORT TO REPORT VIBRATION LEVELS EXCEEDING LIMITS ESTABLISHED IN THE FJ44-3A LINE MAINTENANCE MANUAL, ELEVATED INTER-TURBINE TEMPERATURE (ITT) INDICATION, AND EVIDENCE OF AN OIL LEAK. OEM PRODUCT SUPPORT THEN RECOMMENDED A BORESCOPE INSPECTION OF THE ENGINE; HOWEVER, THE SERVICE FACILITY PERFORMED A GROUND-RUN ON THE ENGINE TO TROUBLESHOOT THE ELEVATED ITT AND OIL LEAK ISSUES, AND DURING THAT RUN, THE LEFT-HAND ENGINE BEGAN TO EXHIBIT UNUSUAL NOISES AND SMOKE WAS OBSERVED TO BE EMANATING FROM THE TAILPIPE. PRODUCT SUPPORT THEN DIRECTED REMOVAL OF THE ENGINE FOR SHIPMENT TO THE REPAIR STATION FOR DISASSEMBLY AND EVALUATION OF ENGINE COMPONENTS. ENGINE DISASSEMBLY REVEALED ONE PARTIALLY-RELEASED HIGH-PRESSURE TURBINE (HPT) BLADE TIP AND THE NO. 3 BEARING EXHIBITED DAMAGE. ADJACENT STATIC ENGINE HOT-SECTION COMPONENTS EXHIBITED SECONDARY DAMAGE FROM THE HPT BLADE ANOMALY.

Source: SDR 2024F00271 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N125DGCESSNA 525B2006Valid RegistrationMatched by certificate designator