Airtec, Inc.

Part 135 operator · designator 4TQA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: Airtec, Inc.

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

14 reports on file.

O · 2007-04-06 Matched by certificate designator
N949SP · ATA 1400

WHILE INSTALLING KIT MK172-25-10C TO COMPLY WITH SB 04-25-01 R4 AND AD 2007-05-10, ONE OF THE PARTS IN THE KIT WAS MACHINED IMPROPERLY. THE HEIGHT ADJUSTING NUT HAD THE THRU HOLE FOR THE ULTRALOC WITH MIS FORMED THREADS. THE MINOR DIAMETER OF THE THREAD WAS GREATER THAN THE MAJOR DIAMETER OF THE THREADS ON THE ULTRALOC. THE CROSS HOLE FOR MOUNTING WAS INCORRECTLY LOCATED WITH INSUFFICIENT EDGE DISTANCE, AND THE PILOT HOLE WAS OFFSET GIVING AN EGG SHAPED HOLE.

Source: SDR 2007FA0000301 · FAA SDRS
W · 2007-04-06 Matched by certificate designator
N949SP · ATA 1400

WHILE INSTALLING KIT MK172-25-10C TO COMPLY WITH SB 04-25-01 R4 AND AD 2007-05-10, ONE OF THE PARTS IN THE KIT WAS MACHINED IMPROPERLY. THE HEIGHT ADJUSTING NUT HAD THE THRU HOLE FOR THE ULTRALOC WITH MALFORMED THREADS. THE MINOR DIAMETER OF THE THREAD WAS GREATER THAN THE MAJOR DIAMETER OF THE THREADS ON THE ULTRALOC. THE CROSS HOLE FOR MOUNTING WAS INCORRECTLY LOCATED WITH INSUFFICIENT EDGE DISTANCE, AND THE PILOT HOLE WAS OFFSET GIVING AN EGG SHAPED HOLE.

Source: SDR 2007FA0000310 · FAA SDRS
O · 2002-10-28 Matched by certificate designator
N949SP · ATA 6113

DURING PHASE 1 INSPECTION, MAINTENANCE FOUND AFT PROPELLER SPINNER BULKHEAD CRACKED AT ONE FLANGE BY THE PROPELLER BLADE CUT OUT ON ONE SIDE. REPLACED PROPELLER AFT SPINNER BULKHEAD & REINSTALLED PROPELLER.

Source: SDR 2002FA0001232 · FAA SDRS
R J · 2001-07-18 Matched by certificate designator
N949SP · ATA 7313

SECOND FLIGHT OF THE DAY, TEMP 89F, DA 9444. ENGINE START WAS DIFFICULT, TAXI AND ENGINE RUN UP NORMAL. AIRCRAFT TOOK THE RUN WAY FOR TAKE OFF. WHEN THROTTLE WAS OPENED TO FULL POWER, ENGINE HAD POPPING NOISE AND WOULD ONLY DEVELOP 2000 RPM. TAKE OFF WAS ABORTED FOR LOW POWER. A CLEAR LINE WAS INSTALLED FROM THE FUEL INJECTION SERVO TO THE FLOW DIVIDER IAW PRECISION AIRMOTIVE TROUBLE SHOOTING MANUAL AND EXCESSIVE VAPOR IN THE LINE WAS DISPLACING THE FUEL WHEN THE ENGINE WAS RUN. THE ENGINE WAS ALLOWED TO COOL COMPLETELY AND RESTARTED, NO VAPOR WAS DETECTED AND ALL OPERATION WAS NORMAL INCLUDING FUEL FLOW WITH THE ENGINE DEVELOPING FULL POWER. AIRCRAFT TEST FLOWN AND RELEASED.

Source: SDR 2001FA0000145 · FAA SDRS
O · 2001-03-16 Matched by certificate designator
N949SP · ATA 7322

ENGINE RSA-5AD1 FUEL SERVO WILL NOT MEET SPECIFICATIONS. FUEL FLOW BELOW 1700 RPM IS TOO HIGH. IDLE SPEED AND MIXTURE CAN NOT BE SET TO MFG SPECIFICATIONS WITH SATISFACTORY ENGINE OPERATION. FUEL SERVO REMOVED, SENT FOR REPAIRS. MAJOR REPAIRS ACCOMPLISHED AND SERVO REFLOWED TO PRECISION FLOW SHEET 30075-02 DATED 5 JAN 00. REINSTALLED FUEL SERVO, ADJUSTED IAW MFG SPECIFICATIONS, OPERATIONAL AND FLIGHT CHECKED SATISFACTORY.

Source: SDR 20010410AP013 · FAA SDRS
O · 2001-02-15 Matched by certificate designator
N949SP · ATA 5347

PILOT REPORTED HIS SEAT LOCK PINS WOULD NOT RELEASE. MAINTENANCE FOUND THE PILOTS SEAT LOCK CONTROL WAS BROKEN. THIS SAME CONTROL WAS REPLACED 431.0 HOURS PRIOR FOR THE SAME PROBLEM. BOTH CONTROL ASSEMBLYS HAVE PN 1611020-05 REPLACE CONTROL ASSEMBLY, OPERATIONAL CHECK SATISFACTORY.

Source: SDR 20010323CW015 · FAA SDRS
O · 2001-01-08 Matched by certificate designator
N949SP · ATA 8011

PILOT ATTEMPTED ENGINE START, STARTER WOULD NOT ROTATE. MAINTENANCE FOUND STARTER HAD TWO TERMINALS MELTED WHERE THAT ATTACH TO COMMUTATOR BRUSHES. REPLACED STARTER, OPERATIONAL CHECKED SAT.

Source: SDR 20010222CW009 · FAA SDRS
J · 2001-01-08 Matched by certificate designator
N949SP · ATA 8011

PILOT ATTEMPTED ENGINE START. FIRST FLIGHT OF THE DAY, STARTER WOULD NOT ROTATE. MAINTENANCE FOUND STARTER HAD TWO TERMINALS MELTED WHERE THEY ATTACH TO COMMUTATOR BRUSHES. REPLACED STARTER, OPERATIONAL CHECKED SAT.

Source: SDR 20010323CW017 · FAA SDRS
S · 2000-11-01 Matched by certificate designator
N949SP · ATA 3240

DURING PHASE 2 INSPECTION, PARKING BRAKE CROSSOVER CABLE, BELLCRANK BOLT WAS BACKED OUT AND RESTRICTING PILOT''S R-RUDDER PEDAL, FWD TRAVEL. WITH THE BOLT BACKED OUT OF THE BELLCRANK, PARKING BRAKE INOP. THE FIBERLOCK NUT WAS FOUND DOWN UNDER THE RUDDER PEDALS AND THE BOLT WAS BENT SLIGHTLY. NO PREVIOUS WORK ACCOMPLISHED ON PARKING BRAKE OR RUDDER PEDALS. IT IS ASSUMED THE NUT WAS NOT TIGHTENED ON INSTALL. THE ONLY WRITE-UP ON ACFT ENTERING PHASE INSPECT WAS PARKING BRAKE INOP. SUBMITTER RECOMMENDED THE AN3-13A BOLT SECURING THE PARKING BRAKE CROSSOVER CABLE BELLCRANK PN 0713070-9 BE INSTALLED FROM RT TO LT INSTEAD OF PRESENT INSTALL LT TO RT. (X)

Source: SDR 20001130SH004 · FAA SDRS
O · 1999-12-16 Matched by certificate designator
N949SP · ATA 7110

DURING PHASE 2 INSPECTION, FOUND 4 LOWER COWL ATTACH SHOCK MOUNTS TORN AT THE BASE. LOCATED AT THE 2, 3, AND 4 O'CLOCK POSITIONS AND THE LOWER L. REPLACED SHOCK MOUNTS.

Source: SDR 2000ZZZX21 · FAA SDRS
O · 1999-12-16 Matched by certificate designator
N949SP · ATA 7111

DURING PHASE 2 INSPECTION, FOUND LOWER COWL SHOCK MOUNT BRACKET CRACKED AT THE 4 O'CLOCK POSITION. THE OTHER HALF OF THE SHOCK MOUNT BRACKET WAS ALSO CRACKED, P/N 045303-3. REPLACED BOTH BRACKETS.

Source: SDR 2000ZZZX22 · FAA SDRS
O · 1999-12-16 Matched by certificate designator
N949SP · ATA 7111

DURING PHASE 2 INSPECTION, FOUND LOWER COWL SHOCK MOUNT BRACKET CRACKED AT THE 4 O'CLOCK POSITION. THE OTHER HALF OF THE SHOCK MOUNT BRACKET WAS ALSO CRACKED, P/N 045303-3. REPLACED BOTH BRACKETS.

Source: SDR 2000ZZZX23 · FAA SDRS
R J · 1999-10-18 Matched by certificate designator
N949SP · ATA 2822

NEW 172S CONDUCTING FLIGHT TRAINING AT AIRFIELD ABOVE 6,000 FEET WITH DENSITY ALTITUDE AT 9,000 FEET AND AMBIENT TEMP APPROXIMATELY 89 DEGREES FAHRENHEIT. TAXI AND RUN-UP CHECKS SATISFACTORY. ON TAKEOFF ROLL, PILOT REPORTED POWER LOSS AND REJECTED TAKEOFF. AIRCRAFT RETURNED TO MAINT AND SHUT DOWN. APPROX 20 MINUTES LATER, MAINT ATTEMPTED TO START ENGINE, WITH BOOST PUMP ON, MIXT AND THROTTLE FULL OPEN. NO FUEL FLOW COULD BE ATTAINED DUE TO FUEL VAPORIZATION. AFTER ALLOWING ENGINE TO COOL SUFFICIENTLY, ENGINE START AND RUN-UP WERE NORMAL.

Source: SDR 99ZZZX4155 · FAA SDRS
W · 1999-07-09 Matched by certificate designator
N949SP · ATA 2720

NEW CESSNA WITH 97.4 HOURS SINCE NEW. DURING FIRST PHASE 2 INSPECTION, FOUND PILOT'S AND COPILOT'S RUDDER PEDALS WERE NOT ALIGNED PARALLEL TO ONE ANOTHER. THE PILOT'S 'R' AND COPILOT'S 'L' RUDDER PEDAL MOUNT ARMS WERE MISDRILLED WHERE THEY MOUNT TO THE RUDDER PEDAL CROSS-OVER SHAFT. REPLACED BOTH ARMS WITH CORRECTELY DRILLED PARTS FROM CESSNA AND ALIGNMENT IS NOW CORRECT.

Source: SDR 99ZZZX2732 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N949SPCESSNA 172S1999Valid RegistrationMatched by certificate designator