LIMA NY CORP.

Part 135 operator · designator L87A

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: FLY THE WHALE, LIMA NY CORP.

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

4 reports on file.

O · 2017-06-26 Matched by certificate designator
N822BB · ATA 3210

WHILE PARKING AIRCRAFT, THE LEFT MAIN GEAR DRAG BRACE BROKE AT THE LOWER CIRCULAR BOLT FLANGE TO THE AXLE ASSEMBLE CASTING.

Source: SDR 2017062600138 · FAA SDRS
B G J · 2016-07-15 Matched by certificate designator
N822BB · ATA 2752

DURING APPROACH, THE PILOT DEPLOYED 1 NOTCH OF FLAPS THEN SEVERAL CIRCUIT BREAKERS TRIPPED FOR READING LIGHTS, AIRSPEED WARN, FIRE DETECTION, AND PRIMARY FLAPS. SAW A LITTLE SMOKE WITH A BURNED ELECTRIC ODOR IN COCKPIT. LANDED WITHOUT INCIDENT. MAINTENANCE TROUBLESHOT AND FOUND MELTED WIRING HARNESSES FROM THE CIRCUIT BREAKER PANEL UP TO THE PRIMARY FLAP MOTOR. REMOVED FLAP ACTUATOR ASSY. BENCH TESTED BOTH DRIVE MOTORS FOUND PRIMARY FLAP DRIVE MOTOR HAD A SHORT INTERNALLY AND THE CIRCUT BREAKER DID NOT TRIP IN TIME TO SAVE THE WIRING. ALSO NOTED THAT THE OTHER TRIPPED CIRCUIT BREAKERS ALL CAME OUT OF THE MAIN PANEL VIA THE SAME CONNECTOR. REPLACED THE FLAP ACTUATOR ASSEMBLY, THE PRIMARY FLAP 10 AMP CIRCUIT BREAKER AND DAMAGED WIRES AS REQUIRED.

Source: SDR FVAA2016072000335 · FAA SDRS
O · 2011-02-22 Matched by certificate designator
N822BB · ATA 5511

DURING PHASE 10 INSP FOUND THE HORIZ STAB FWD FACE OF THE MAIN SPAR BENT AND CRACKED IN THE CTR OF THE WEB AREA IN BETWEEN THE MAIN ATTACHMENT POINTS TO FUSELAGE STRUCTURE WITH THE STABILIZER REMOVED FROM THE ACFT TAILCONE.

Source: SDR 2011F00042 · FAA SDRS
O · 2011-02-11 Matched by certificate designator
N822BB · ATA 5511

ACTC=4354, DURING PHASE 10 INSP, FOUND HORIZONTAL STAB FWD SPAR BENT AND CRACKED, IN THE CENTER WEB AREA, IN BETWEEN THE FWD ATTACH POINTS. MFG CUSTOMER SERVICE AND ENGINEERING WERE CONTACTED AND SENT PHOTOS. OPERATOR SUSPECTS ACFT CLEANING PERSONNEL STANDING ON TOP OF HORIZ STAB DURING CLEANING OPERATION. THIS PRACTICE WILL NO LONGER BE ALLOWED. ALSO, LARGE RED "NO STEP" PLACARDS WILL BE OPSITIONED ON TOP OF LT AND RT HORIZ STAB OF THESE ACFT.

Source: SDR 2011FA0000145 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N18NMTEXTRON AVIATION INC 208B2016Valid RegistrationMatched by certificate designator
N261PJTEXTRON AVIATION INC 208B2018Valid RegistrationMatched by certificate designator
N301CVMatched by certificate designator
N380TAMatched by certificate designator
N401STEXTRON AVIATION INC 208B2015Valid RegistrationMatched by certificate designator
N425LHMatched by certificate designator
N622TPTEXTRON AVIATION INC 208B2017Valid RegistrationMatched by certificate designator
N624ALCESSNA 208B2006Valid RegistrationMatched by certificate designator
N801VWCESSNA 2082008Valid RegistrationMatched by certificate designator
N822BBMatched by certificate designator