STAPLES AVIATION

Part 135 operator · designator BPYA

Data confidence: Records are linked by certificate number, aircraft registration, or a name match that a reviewer has confirmed. Each record below shows how it was linked.

Also recorded as: LAKE PLACID FLYING SERVICE INC, Lake Placid Airways Inc., STAPLES AVIATION

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

7 reports on file.

O · 2015-02-03 Matched by certificate designator
N83D · ATA 8520

DURING CRUISE FLIGHT, NR 1 AND NR 2 CONNECTING RODS FAILED AT THE CRANK JOURNALS CAUSING THE ENGINE TO SEIZE. THE RODS BROKE BOTH CASE HALVES AND THE LT MAGNETO FROM THE CASE. REASON IS UNKNOWN. 1515.1 HRS SMOH.

Source: SDR BPY2015F00000 · FAA SDRS
K J · 2005-07-26 Matched by certificate designator
N545PZ · ATA 2910

HYDRAULIC HOSE TO NOSE LANDING GEAR CYLINDER FAILED IN FLIGHT. THIS CAUSED TOTAL DEPLETION OF HYDRAULIC FLUID AND SUBSEQUENT HYDRAULIC PUMP FAILURE. PILOT WAS UNABLE TO EXTEND LANDING GEAR MANUALLY BECAUSE OF NOT ENOUGH FLUID. A GEAR UP LANDING WAS MADE WITH MINOR DAMAGE TO AIRCRAFT.

Source: SDR 2005F00091 · FAA SDRS
O · 2000-06-13 Matched by certificate designator
N545PZ · ATA 5510

THREE OF FOUR BALANCE WEIGHT SUPPORT BRACKETS WERE CRACKED ALONG THE BEND RADIUS. CRACKS WERE 1.25 INCHES, 1.50 INCHES, AND 1.75 INCHES ON EACH. THIS WAS NOTICED DURING STABILIZER BEARING REPLACEMENT WITH THE STABLIZER OFF THE AIRCRAFT. SUBMITTER RECOMMENDED FREQUENT INSPECTIONS. UNKNOWN CAUSE. (X)

Source: SDR 20000613SH011 · FAA SDRS
O · 2000-06-13 Matched by certificate designator
N545PZ · ATA 5510

THREE OF FOUR BALANCE WEIGHT SUPPORT BRACKETS WERE CRACKED ALONG THE BEND RADIUS. CRACKS WERE 1.25 INCHES, 1.50 INCHES, AND 1.75 INCHES ON EACH. THIS WAS NOTICED DURING STABILIZER BEARING REPLACEMENT WITH THE STABLIZER OFF THE AIRCRAFT. SUBMITTER RECOMMENDED FREQUENT INSPECTIONS. UNKNOWN CAUSE. (X)

Source: SDR 20000613SH012 · FAA SDRS
O · 2000-06-13 Matched by certificate designator
N545PZ · ATA 5510

THREE OF FOUR BALANCE WEIGHT SUPPORT BRACKETS WERE CRACKED ALONG THE BEND RADIUS. CRACKS WERE 1.25 INCHES, 1.50 INCHES, AND 1.75 INCHES ON EACH. THIS WAS NOTICED DURING STABILIZER BEARING REPLACEMENT WITH THE STABLIZER OFF THE AIRCRAFT. SUBMITTER RECOMMENDED FREQUENT INSPECTIONS. UNKNOWN CAUSE. (X)

Source: SDR 20000613SH013 · FAA SDRS
J · 1997-04-25 Matched by certificate designator
N8091Q · ATA 8500

MSS/HPN - AT 9,500 FEET APPROXIMATELY 15 MINUTES INTO THE FLIGHT, THE LEFT ENGINE RPM STARTED FLUCTUATING ABOUT 150 RPM. ABOUT 5 MINUTES LATER THAT ENGINE FAILED COMPLETELY. AFTER ATTEMPTING A RE-START AND CHECKING GAUGES (FUEL FLOW, 20 FEET MANIFOLD, PRESSURE) THE ENGINE WAS FEATHERED AND A PRECAUTIONARY LANDING WAS MADE AT COLUMBIA COUNTY. IT APPEARS THERE WAS A CAMSHAFT FAILURE.

Source: SDR 97ZZZX2572 · FAA SDRS
R · 1996-06-24 Matched by certificate designator
N33247 · ATA 8530

TEMPORARY POWER LOSS DURING CRUISE. SUSPECT CAUSE: BROKEN PISTON RING WHICH BECAME WEDGED BETWEEN PISTON AND CYLINDER WALL. REPLACED COMPLETE CYLINDER ASSY.

Source: SDR 96ZZZX3441 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N33247CESSNA U206F1975Valid RegistrationMatched by certificate designator
N545PZCESSNA 177RG1976Valid RegistrationMatched by certificate designator
N545PZCESSNA 177RG1976Valid RegistrationOperator named in NTSB report
N638GBMatched by certificate designator
N83DCESSNA 414A1981Valid RegistrationMatched by certificate designator