WESTWIND AVIATION, INC.

Part 135 operator · designator WIWA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: WESTWIND AIR SERVICE, WESTWIND AVIATION, INC., Westwind Aviation, Inc.

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

Accident · 2003-05-26 Matched by aircraft (N-number)
Cessna T207A (N9317M) None injury
Source: NTSB case LAX03LA164

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

8 reports on file.

K R Y · 2020-09-16 Matched by certificate designator
N9317M · ATA 8550

THE PILOTS REPORTED THAT HE SET TAKEOFF POWER, ENGINE PARAMETERS READ NORMAL AND UPON REACHING 40 KNOTS HE SAW A ROLL BACK. HE EXECUTED AN ABORTED TAKEOFF AND HEARD SOME ENGINE SPUTTERING FOLLOWED BY THE ENGING SHUTTING OFF. MAINTENANCE FOUND NO ABNORMAL PROBLEMS ON THE FIRST FEW RUN UPS, BUT UPON FUTURE INSPECTION THEY DID FIND AN OIL LEAK APPEARING TO COME FROM THE TURBO CHARGER. HOWEVER, IT IS NOT CONFIRMED THAT THE TURBO CHARGER IS THE ISSUE. AT THIS TIME WE DO NOT KNOW THE CAUSE OF THIS ENGINE FAILURE.

Source: SDR WIWA2020F00000 · FAA SDRS
R J · 2008-08-13 Matched by certificate designator
N30591 · ATA 7712

ON 8/13/2008 AT APPROX 07:40 AM, AIRPLANE WHILE PERFORMING AERIAL APPLICATION EXPERIENCED A LOSS OF ENGINE POWER AND MADE AN EMERGENCY LANDING IN A FIELD. SUBSEQUENT INVESTIAGATION REVEALED THE IDLER GEAR BRG (PN 3103035-1) IN THE TORQUE SENSOR HAD FAILED ALLOWING THE LOSS OF DRIVE INPUT TO THE FUEL CONTROL RESULTING IN LOSS OF ENGINE POWER AND EMERGENCY LANDING. (K)

Source: SDR WIW2008F00000 · FAA SDRS
E · 2007-05-02 Matched by certificate designator
N122JB · ATA 6111

VIBRATION REPORTED BY PILOT. OPERATOR WAS UNABLE TO DYNAMIC BALANCE. OPERATOR NOTICED ONE BLADE HAS ROTATIONAL PLAY. UPON DISASSEMBLY NR 2 BLADE LINK BUSHING P/N A4564 WAS FOUND CRACKED WITH PIECES MISSING. THE LINK P/N B4743 AND BLADE ACTUATING PIN P/N B5072-1 WERE DAMAGED FROM METAL TO METAL CONTACT.

Source: SDR 26519A · FAA SDRS
O · 2005-07-28 Matched by certificate designator
N9482M · ATA 5342

PILOT FOUND VERTICAL STABILIZER LOOSE ON PREFLIGHT. MAINTENANCE INSPECTED AND FOUND RT FWD ATTACHMENT FITTING BROKEN. REPLACED BOTH FWD FITTINGS WITH NEW PARTS. (K)

Source: SDR 2005FA0001134 · FAA SDRS
R J · 1999-08-13 Matched by certificate designator
N9482M · ATA 8120

ON ROLL-OUT, AIRCRAFT WOULD NOT DEVELOP POWER. ONLY REACHED 24 MAP. APC WAS FOUND WITH CARBON AND METAL CONTAMINATION. AIRCRAFT HAD TURBOCHARGER CATASTROPHIC FAILURE 2 WEEKS PRIOR. POSSIBLE CAUSE WAS METAL PARTICLES FROM TURBO FAILURE CONTAMINATED SEAT VALVE IN CONTROLLER AND CAUSED APC TO FAIL.

Source: SDR 99ZZZX3403 · FAA SDRS
J · 1999-07-27 Matched by certificate designator
N9482M · ATA 8120

PILOT REPORTED GOOD M.A.P. AT TAKEOFF. TWO MINUTES INTO FLIGHT, M.A.P. DROPPED TO 23 INCHES. THIRTY SECONDS LATER, M.A.P. DROPPED TO 20 INCHES. SUSPECT THIS IS WHEN TURBO FROZE UP AND RESTRICTED EXHAUST FLOW LIMITING ENGINE POWER. SUBMITTER STATED NO PASSENGERS ONBOARD OR THIS WOULD HAVE BEEN AN EMERGENCY LANDING.

Source: SDR 99ZZZX3111 · FAA SDRS
E · 1997-10-07 Matched by certificate designator
N75870 · ATA 6111

PILOT REPORTED SLIGHT ENGINE VIBRATION AND PROPELLER SLOW TO RESPOND IN RETURN TO LOW PITCH. DISASSEMBLY REVEALED ONE BLADE WAS CRACKED 180 DEGREES NEAR BEARING SURFACE AT ROOT END. CAUSE UNKNOWN. CATASTROPHIC FAILURE IMMINENT. BLADE UNDER ANALYSIS AT MCCAULEY.

Source: SDR 97ZZZX4446 · FAA SDRS
O · 1997-07-29 Matched by certificate designator
N9317M · ATA 6114

PENETRANT INSPECTION DURING NORMAL OVERHAUL INDICATED A FINE LINEAR CRACK OR SCRATCH. SUBSEQUENT EDDY CURRENT TESTING USING PHASE PLANE ANALYSIS INSTRUMENTATION REVEALED A CRACK APPROXIMATELY 1.5 INCHES LONG, ESTIMATED OVER .040 INCH DEEP ON THE EXTERIOR SURFACE OF NR 3 BLADE SOCKET ON THE LEADING EDGE SIDE SLIGHTLY ABOVE CENTERLINE OF THE HUB. THIS CONDITION IS NOT COMMONLY FOUND IN THE 'THREADLESS' STYLE OF MCAULY HUBS AND MAY BE OVERLOOKED WITHOUT EDDY CURRENT TEST.

Source: SDR 97ZZZX3748 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N1129GCESSNA 208B2001Valid RegistrationMatched by certificate designator
N122JBCESSNA 208B2003Valid RegistrationMatched by certificate designator
N208WWCESSNA 208B1998Valid RegistrationMatched by certificate designator
N71SCCESSNA 208B2003Valid RegistrationMatched by certificate designator
N7268ZCESSNA T206H1999Valid RegistrationMatched by certificate designator
N75870CESSNA T207A1980Valid RegistrationMatched by certificate designator
N785WWCESSNA 208B1999Valid RegistrationMatched by certificate designator
N786WWCESSNA 208B2004Valid RegistrationMatched by certificate designator
N9317MCESSNA T207A1980Valid RegistrationMatched by certificate designator
N9482MCESSNA T207A1981Valid RegistrationMatched by certificate designator