N1110J

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AMERIFLIGHT, LLC (JIKA)Certificate holderMatched by certificate designator
Arctic One LlcOperator2012-02-16 – 2012-02-16Operator named in NTSB report

Accident & incident history

Acc · 2012-02-16 Operator named in NTSB report
Embraer EMB120 None injury Part 121Arctic One Llc
Source: NTSB case DCA12CA042
Accident · 1968-06-25 Unresolved
Bell 47G3B1 None injuryoperator not yet resolved
Source: NTSB case LAX69D0041
Accident · 1966-03-20 Unresolved
Bell 47G3B1 Minor injuryoperator not yet resolved
Source: NTSB case MIA66A0108

Maintenance disclosures

B · 2023-04-24 Matched by certificate designator
ATA 2100

THE FLIGHT CREW REPORTED SMOKE IN THE COCKPIT DURING DESCENT INTO KMFR. THE AIRCRAFT LANDED IN KMFR WITHOUT INCIDENT. EMERGENCY VEHICLES WERE DISPATCHED. PDX MAINTENANCE DROVE OUT TO AIRCRAFT AND DEFERRED LH PACK. MAINTENANCE DROVE TO KMFR AND DEFERRED THE LH PACK IAW MEL 21-50-2. A/C WAS PLACARDED AND DEFERRED PER MEL AND RETURNED TO SERVICE. AIRCRAFT IS CURRENTLY DOWN, AND THIS MEL SQUAWK IS BEING WORKED ALONG WITH OTHER MAINTENANCE TASKS. SUPPLEMENTAL SDR WILL BE SUBMITTED ONCE THE AIRCRAFT HAS BEEN REPAIRED AND MEL HAS BEEN CLEARED.

Source: SDR JIKA20230427401 · FAA SDRS
K J · 2012-12-18 Matched by certificate designator
ATA 7261

NR 2 OIL PRESSURE WAS FLUCTUATING BETWEEN 55-40 PSI. NR 2 OIL PRESSURE AURAL WARNING ENGINE "OIL" SHUTDOWN. REPLACED NR 2 PCU IAW MM 61-21-00. GROUND OPS AND LEAK CHECK GOOD. PCU WAS FOUND TO BE LEAKING EXTERNALLY AT REAR OF UNIT.

Source: SDR FXGA201212260001 · FAA SDRS
O · 2012-10-26 Matched by certificate designator
ATA 5553

DURING INSPECTION, FOUND RT VERTICAL STABILIZER TO FUSELAGE ATTACH ANGLE CRACKED AT THE AFT PRESSURE BULKHEAD.

Source: SDR FXGA20121030001 · FAA SDRS
O · 2011-12-07 Matched by certificate designator
ATA 5210

DURING "A" CHECK, DISCOVERED A CORRODED SUPPORT OF THE MAIN CABIN DOOR WHICH REQUIRED THE SUPPORT REPLACEMENT.

Source: SDR FXGA2012018001 · FAA SDRS
O · 2011-12-07 Matched by certificate designator
ATA 5730

DURING "A" CHECK DISCOVERED CRACKS ON LOWER WING SKIN AROUND ACCESS PANELS, 143FB AT WING STATION Y-657, 143BB LT WING STATION Y-657, AND 521AB LT WING STATION YA1359.

Source: SDR FXGA2012018002 · FAA SDRS
F · 2011-08-31 Matched by certificate designator
ATA 2711

AILERON JAMMED AT TOP OF CLIMB. PULLED AILERON DISCONNECT. RIGHT AILERON THEN APPEARED TO MOVE FREELY. INSPECTED AIRCRAFT AND DETERMINED AILERON TRIM TAB ACTUATOR TO BE THE CAUSE.

Source: SDR FXGA20111006001 · FAA SDRS
O · 2011-08-29 Matched by certificate designator
ATA 5730

FOUND LOOSE AND MISSING RIVET ON LOWER WING SKIN STA Y4534 AFT OF STRINGER 10. REPAIRED IAW EMB-120 SRM 51-40-03B.

Source: SDR FXGAN1110J8292011 · FAA SDRS
G · 2011-04-13 Matched by certificate designator
ATA 2435

EMERGENCY BUSS OFF LIGHT ILLUMINATED. REPLACED NR (2) ENGINE STARTER GENERATOR AND RESET CB0471, EMER 1 BUS CIRCUIT BREAKER. OPS CHECKED ALL BUSSES AND TRANSFER FUNCTION IAW MM 24-52-00. NO DEFECTS NOTED.

Source: SDR FXGA20110413001 · FAA SDRS
O · 2010-11-03 Matched by certificate designator
ATA 5210

DISCOVERED UPPER RT LATCHING MECHANISM ON FWD DOOR BROKEN, REPLACED BACKSTOP/STOPPER (ASSY PN 120-25452-006) IAW AMM 52-11-00.

Source: SDR FXGA110J · FAA SDRS
O · 2010-10-14 Matched by certificate designator
ATA 5210

A DEEP NICK WAS FOUND ON THE MAIN DOOR 1.5" AFT OF FRAME 15, APPROX 12.5" ABOVE DOOR CUTOUT. REPAIRED DAMAGE IAW EO 1051 AND SRM 52-10-01.

Source: SDR FXGAN1110J · FAA SDRS
O · 2007-02-01 Matched by certificate designator
ATA 3230

ON GEAR RETRACTION RED GEAR LIGHTS A AND B REMAINED ON AND LT MAIN GEAR DOOR WOULD NOT SHUT. MAINTENANCE INVESTIGATION REVELED THAT THE PN 19659 BUSHINGS IN BOTH THE LT AND RT UP-LOCK HOOK SUPPORT ASSY. PN 19552 WERE AT MINIMUM OVERHAUL TOLERANCES. IN COLD TEMPERATURES (-35F TO -40F) THESE CLEARANCES WERE TOO TIGHT. BUSHINGS WERE REAMED TO THE UPPER O/H CLEARANCE LIMITS. ASSY REASSEMBLED AND OPERATIONALY CHECKED. AC RETURNED TO SERVICE WITH NO ADDITIONAL PROBLEMS. (K)

Source: SDR FXG2007F00001 · FAA SDRS
F · 2002-04-16 Matched by certificate designator
ATA 2752

RIGHT OUTBOARD FLAP CAME DOWN 5 DEGREES SITTING ON RAMP WITH ENGINES OFF AND APU RUNNING. RAN QRH AND FLAP FAILED TO RETRACT. REPLACED RIGHT OUTBOARD FLAP ACTUATOR. OPERATED FLAPS SEVERAL TIMES. OPS CHECK GOOD. NO LEAKS FOUND.

Source: SDR SWIA200210811 · FAA SDRS
K F J · 2002-04-13 Matched by certificate designator
ATA 2752

TEN MINUTES AFTER TAKEOFF, THE RIGHT SIDE HYDRAULIC RESERVOIR LOW LEVEL LIGHT ILLUMINATED, FOLLOWED SHORTLY BY THE RIGHT SIDE MAIN PUMP LOW PRESSURE LIGHT. RETURNED TO LAX AFTER COMPLETING QRH PROCEDURES. RIGHT HYDRAULIC PUMP OUT OF FLUID APPROX 15 MINUTES. INSTALLED SERVICEABLE LEFT HYDRAULIC FLAP ACTUATOR IAW EMB MM 27-50-00. INSTALLED NEW HYDRAULIC PUMP. RAN ENGINE, NO LEAKS NOTED. CYCLED FLAPS, OPS CHECK GOOD. CHECKED ACTUATOR, NO LEAKS NOTED. ALL OPS CHECKS GOOD.

Source: SDR SWIA200210784 · FAA SDRS
O · 2002-01-07 Matched by certificate designator
ATA 5260

ON DOOR OPENING 3RD AND 4TH STAIRS FROM THE TOP DID NOT EXTEND. REPOSITIONED BOTTOM STEP SPRING AND REPLACED STEP SPRING ON 3RD STEP DOWN FROM TOP. OPS CHECK GOOD.

Source: SDR SWIA200210533 · FAA SDRS
J · 2001-12-11 Matched by certificate designator
ATA 3010

VERTICAL FIN LEADING EDGE DEICE BOOT FAILED INFLIGHT WITH BOTH TIMERS 1 AND 2. FOUND GREEN CORROSION AROUND PIN-B IN CONNECTOR AT S0213 (VERTICAL FIN PRESSURE SWITCH). REMOVED AND REPLACED CONNECTOR P1080 AND SOCKET-B IN CONNECTOR. GROUND OPS CHECK OK WITH LEFT AND/OR RIGHT ENGINE AIR.

Source: SDR SWIA200110433 · FAA SDRS
F J · 2001-08-20 Matched by certificate designator
ATA 2750

FLAP CONTROL FAULT DURING FLAP RETRACTION AND AGAIN WHEN SETTING FLAPS TO 25 DEGREES FOR LANDING. ALL LIGHT BARS FLASHING. QRH RESET PROCEDURE WORKED BOTH TIMES.REMOVED AND REPLACED FLAP SELECTOR IAW MM 27-51-00. OPS CHECK GOOD ON GROUND.

Source: SDR SWIA200110121 · FAA SDRS
O · 2001-08-18 Matched by certificate designator
ATA 2752

RT NACELLE FLAP POT IS ERRATIC.REMOVED AND REPLACED RIGHT NACELLE FLAP ACTUATOR. OPS CHECKS GOOD IAW MM 27-50-08.

Source: SDR SWIA200110106 · FAA SDRS
J · 2001-06-18 Matched by certificate designator
ATA 3414

''HIGH SPEED'' AURAL WARNING/TRIPLE CHIME SOUNDED ON TAKEOFF ROLL - IAS APPROXIMATELY 40 KNOTS. TAKEOFF ABORTED. REMOVED AND REPLACED PILOT'S AIRSPEED INDICATOR IAW MM 34-14-00 TO START HISTORY. COULD NOT DUPLICATE BEFORE REPLACEMENT. OPS AND LEAK CHECK GOOD. P/N: 320AS1 S/N ON: AH789 S/N OFF: AH752

Source: SDR SWIA972643 · FAA SDRS
F J · 2001-06-06 Matched by certificate designator
ATA 2752

ON FINAL AFTER SELECTING FLAPS 25, FLAP ASYMMETRY WARNING, FOUR SEGMENTS SHOWING ON RIGHT INBOARD AND ONE SEGMENT ON LEFT INBOARD FLAP INDICATOR. AIRCRAFT WAS CONTROLLABLE. LEFT INBOARD FLAP ACTUATOR FEEDBACK POT FAILED INSULATION RESISTANCE CHECK PER PARKER TROUBLESHOOTING GUIDE. REMOVED AND REPLACED LEFT INBOARD FLAP ACTUATOR IAW MM 27-50-07. OPS CHECK GOOD. NO LEAKS FOUND. P/N: 320300-1005 S/N ON: 1029 S/N OFF: 0059

Source: SDR SWIA972621 · FAA SDRS
O · 2000-12-28 Matched by certificate designator
ATA 3413

ON TAKEOFF ROLL CAPTAINS VSI/TCAS DISPLAY WENT BLANK AND REMAINED BLANK THROUGHOUT ABORTED TAKEOFF. STARTED WORKING DURING TAXI BACK. CHECKED SECURITY OF DISPLAY ELECTRICAL CONECTOR. CYCLED DISPLAY POWER. NO DISCREPANCIES FOUND DURING INSPECTION.

Source: SDR SWIA972232 · FAA SDRS
J · 2000-10-21 Matched by certificate designator
ATA 3260

AFTER TAKEOFF, THE LANDING GEAR WAS SELECTED UP, THE A AND B DOWN PROXIMITY LIGHTS REMAINED LIT, AS WELL AS ALL A AND B DISAGREEMENT LIGHT. AFTER TWO MINUTES, GEAR CAME UP. CYCLED TWO TIMES WITH SAME RESULT. RETURNED TO SFO. REPLACED LANDING GEAR CONTROL BOX. CYCLED THE GEARS SEVERAL TIMES. OPS CHECKS GOOD. P/N ON: 120-38594-501, S/N: 120009R, S/N OFF: 120081R.

Source: SDR SWIA972043 · FAA SDRS
L · 2000-07-04 Matched by certificate designator
ATA 3350

EMERGENCY LIGHTS FRONT LEFT FLOOR AND MIDDLE CEILING AND SIDE INOP. REPLACED FORWARD EMERGENCY LIGHT BATTERY, OPS CHECKS GOOD. S/N: 263, S/N OFF: 12741896.

Source: SDR SWIA971858 · FAA SDRS
O · 2000-07-04 Matched by certificate designator
ATA 3350

EMERGENCY LIGHTING INOP FORWARD FLOOR AND LEFT WALL EXIT SIGN. AFTER PROPER CHARGING, OPS CHECK OF EMERGENCY LIGHTING SYSTEM PER MM 335000 CHECKS GOOD.

Source: SDR SWIA971857 · FAA SDRS
F · 2000-06-28 Matched by certificate designator
ATA 2750

ON DESCENT, FLAP AND ADVANCED STALL WARNING LIGHTS ILLUMINATED ALONG WITH CONTROL FAULT LIGHT AND SECOND ROW OUTBOARD FLAP LIGHTS ON FLAP PANEL. FOLLOWED QRH AND RESET, WARNINGS CORRECTED. AFTER LANDING ALL WARNINGS RETURNED AND WOULD NOT RESET. CLEANED FLAP ACTUATOR, CANNON PLUG AND RERACKED FLAP CONTROL UNIT, OPS CHECK GOOD.

Source: SDR SWIA971851 · FAA SDRS
F · 2000-06-28 Matched by certificate designator
ATA 2750

ON DESCENT, FLAP AND ADVANCED STALL WARNING LIGHTS ILLUMINATED ALONG WITH CONTROL FAULT LIGHT AND SECOND ROW OUTBOARD FLAP LIGHTS ON FLAP PANEL. FOLLOWED QRH AND RESET, WARNINGS CORRECTED. AFTER LANDING ALL WARNINGS RETURNED AND WOULD NOT RESET. REMOVED AND REPLACED FLAP CONTROL UNIT (P/N 3075001007), (S/N 0287). CYCLED FLAPS SEVERAL TIMES, ALL INDICATIONS NORMAL.

Source: SDR SWIA971852 · FAA SDRS
J · 2000-02-13 Matched by certificate designator
ATA 3010

LEADING EDGE VERTICAL FIN LIGHT ILLUMINATED ON ICE PROTECTION PANEL. RETURNED TO PDX. INSTALLED SERVICEABLE VERTICAL FIN DEICE BOOT IAW 301000, OPS CHECK GOOD. (P/N 29S70513539) ON, (S/N ME27100) ON, (S/N ME314140) OFF.

Source: SDR SWIA971692 · FAA SDRS
F J · 1999-12-29 Matched by certificate designator
ATA 3230

AFTER TAKEOFF, SELECTED LANDING GEAR UP, ALL LIGHTS ON GEAR CONTROL PANEL ILLUMINATED. NO GEAR DOOR NOISE OR GEAR RETRACTION HEARD CYCLED LANDING GEAR HANDLE WITH THE SAME RESULTS. RETURNED TO LAX. REPLACED RIGHT GEAR UPLOCK A HARNESS. OPS CHECK GOOD.

Source: SDR SWIA971639 · FAA SDRS
J · 1999-08-08 Matched by certificate designator
ATA 3416

CAPTAINS ALTIMETER FAILED CLIMBING THROUGH 13,100. OFF FLAG DISPLAYED. RETURNED TO SEA. REMOVED AND REPLACED CAPTAIN'S ALTIMETER IAW MM 34-12-03. CHECKS GOOD.

Source: SDR SWIA971543 · FAA SDRS
N · 1997-10-21 Matched by certificate designator
ATA 2751

FLAP DISAGREEMENT WARNING WHEN FLAP SELECTED FOR LANDING APPROACH. COULD NOT DUPLICATE DISCREPANCY. OPERATIONAL CHECK OF FLAP SYSTEM IAW EMB M/M WAS SATISFACTORY.

Source: SDR COMA9710436 · FAA SDRS
N · 1997-10-03 Matched by certificate designator
ATA 2934

GREEN HYDRAULIC SYSTEM LOW LEVEL WARNING INDICATION INFLIGHT. REPLACED THE RESERVOIR QUANTITY TRANSDUCER.

Source: SDR COMA9710422 · FAA SDRS
O · 1997-08-01 Matched by certificate designator
ATA 5753

WHEN FLAPS SELECTED TO 15 DEGREES FLAP DISAGREEMENT WARNING ON. COULD NOT DUPLICATE DISCREPANCY. CLEANED FLAP TRACKS, OPERATION OF FLAPS NORMAL.

Source: SDR COMA9710343 · FAA SDRS
L · 1997-07-12 Matched by certificate designator
ATA 3350

EMERGENCY FLOOR PATH LIGHTING, ROWS 1 THRU 5, IS INOP. REPLACED EMERGENCY LIGHT BATTERY.

Source: SDR COMA9710331 · FAA SDRS
O · 1997-02-11 Matched by certificate designator
ATA 2710

AILERONS BINDING AND NOISY WHEN MOVED LT OR RT. REPLACED THE AUTO PILOT SERVO. PART TOTAL CYCLES, 20,917.

Source: SDR COMA9710131 · FAA SDRS
L · 1996-12-11 Matched by certificate designator
ATA 3350

EMERGENCY EXIT LIGHT AT ROW 5C IS INOP. REPLACED THE EMERGENCY BATTERY PACK.

Source: SDR COMA9610395 · FAA SDRS
L · 1996-10-25 Matched by certificate designator
ATA 2210

DURING AUTO PILOT TEST THE ELEVATOR TRIM RUNS WILD. AUTO PILOT SYSTEM PLACED ON DEFERRED MAINTENANCE LIST.

Source: SDR COMA9610310 · FAA SDRS
O · 1996-09-30 Matched by certificate designator
ATA 6120

NR 2 FLIGHT IDLE STOP CB POPPED. REPLACED NR 2 FLIGHT IDLE STOP CIRCUIT BREAKER.

Source: SDR COMA9610292 · FAA SDRS
O · 1996-08-20 Matched by certificate designator
ATA 2150

BOTH LT AND RT COOLING PACKS FAIL TO COOL PROPERLY. REPLACED THE LT AND RT PRESSURE REGULATING VALVES.

Source: SDR COMA9610249 · FAA SDRS
O · 1996-07-19 Matched by certificate designator
ATA 3241

ANTI-SKID LIGHT ILLUMINATED WHEN LANDING GEAR RETRACTED. REPLACED THE ANTI-SKID CONTROL BOX.

Source: SDR COMA9610227 · FAA SDRS
N · 1996-06-14 Matched by certificate designator
ATA 3418

COPILOTS STICK SHAKER ACTIVATED DURING TAKEOFF ROLL. REPLACED THE STALL WARNING COMPUTER.

Source: SDR COMA9610180 · FAA SDRS
O · 1996-06-07 Matched by certificate designator
ATA 7603

FLIGHT IDLE STOP SOLENOID CIRCUIT BREAKER TRIPPED, WOULD NOT RESET. REPLACED THE FLIGHT IDLE SOLENOID.

Source: SDR COMA9610172 · FAA SDRS
O · 1996-05-18 Matched by certificate designator
ATA 5610

CABIN WILL NOT HOLD PRESSURIZATION. ADJUSTED AND RESEALED PILOT'S DIRECT VISION WINDOW.

Source: SDR COMA9610149 · FAA SDRS
J · 1996-04-13 Matched by certificate designator
ATA 2752

FLAP DISAGREEMENT AND CONTROL FAULT WARNINGS. REPLACED THE RT OUTBD FLAP ACTUATOR.

Source: SDR COMA9610125 · FAA SDRS
O · 1996-03-31 Matched by certificate designator
ATA 2750

FLAP CONTROL FAULT WARNING. REPLACED THE FLAP CONTROL UNIT.

Source: SDR COMA9610123 · FAA SDRS
O · 1996-03-08 Matched by certificate designator
ATA 3231

RIGHT MLG DOOR FOUND IN THE OPEN POSITION DURING PREFLIGHT. REPLACED BROKEN DOOR LATCH ASSY.

Source: SDR COMA9610097 · FAA SDRS
Y · 1996-02-03 Matched by certificate designator
ATA 7200

DURING FLIGHT, RT ENGINE FAILED. REPLACED THE RT ENGINE.

Source: SDR COMA9610059 · FAA SDRS
O · 1996-01-12 Matched by certificate designator
ATA 7603

THE LT AND RT POWER LEVER FLIGHT IDLE STOP SOLENOIDS CIRCUIT BREAKERS WERE TRIPPED. RESET CIRCUIT BREAKERS AND SYSTEM TEST NORMAL.

Source: SDR COMA9610023 · FAA SDRS
N · 1996-01-10 Matched by certificate designator
ATA 3418

STICK SHAKER CAME ON DURING TAKEOFF ROLL. REPLACED THE LT ANGLE OF ATTACK VANE.

Source: SDR COMA9610019 · FAA SDRS
O · 1996-01-04 Matched by certificate designator
ATA 2750

FLAP ASYMMETRY WARNING DURING LANDING ROLL. REPLACED THE FLAP CONTROL BOX.

Source: SDR COMA9610002 · FAA SDRS
O · 1995-12-18 Matched by certificate designator
ATA 5320

RT WING ROOT FAIRING UPPER ATTACH ANGLE HAS NUMEROUS BROKEN RIVET HEADS AND POSSIBLE CRACKS. REPAIRED FAIRING SUPPORT ANGLE.

Source: SDR COMA9512030 · FAA SDRS
O · 1995-10-11 Matched by certificate designator
ATA 7603

THE RIGHT POWER LEVER FLIGHT IDLE STOP SOLENOID IS INOPERATIVE. REPLACED THE FLIGHT IDLE STOP SOLENOID.

Source: SDR COMA9511984 · FAA SDRS
K · 1995-04-14 Matched by certificate designator
ATA 2720

HYDRAULIC FLUID LEAK AT VERTICAL STABILIZER. REPLACED THE RUDDER POWER CONTROL UNIT.

Source: SDR COM11863 · FAA SDRS
J · 1995-04-10 Matched by certificate designator
ATA 2752

FLAP ASSYMETRY WARNING. RT OUTBD FLAP INDICATES 25 DEGREES WHEN SELECTED 15 DEGREES. REPLACED RT OUTBD FLAP ACTUATOR.

Source: SDR COM11856 · FAA SDRS
O · 1995-02-26 Matched by certificate designator
ATA 5320

DURING INSPECTION OF UNDER FLOOR LAVATORY AREA, THE DOUBLER FOR THE OAT SENSOR WAS FOUND TO HAVE CORROSION. THE DOUBLER WAS REPLACED BY A FABRICATED DOUBLER AND INSTALLED IN ACCORDANCE WITH AERODESIGN AIRCRAFT ENGINEERING REPORT 1452-1.

Source: SDR COM11797 · FAA SDRS
J · 1995-02-19 Matched by certificate designator
ATA 5753

INBOARD FLAPS WOULD NOT RETRACT AFTER TAKEOFF. REPLACED ROLLERS ON LT INBOARD FLAP.

Source: SDR COM11793 · FAA SDRS