N111PV

BEECH 200 · 1981 · Valid Registration

Registered owner: HENSON BUILDERS LLC, TX (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AIRMED INTERNATIONAL, LLC (MDGA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

K · 2020-04-03 Matched by certificate designator
ATA 3242

AIRCRAFT HAD A BRAKING ISSUE, REMOVED AND REPLACED THE BRAKE WITH A OVERHAULED UNIT AND BLED AS NECESSARY. OPS CHECKED GOOD AIRCRAFT RETURNED TO SERVICE.

Source: SDR MDGA2020043000000 · FAA SDRS
J · 2016-03-15 Matched by certificate designator
ATA 3200

THE FLIGHT DEPARTED RNWY 1L, UPON GEAR RETRACTION, ATC POINTED OUT HELICOPTER TRAFFIC AT MY 11O’CLOCK POSITION, INSTRUCTED ME TO KEEP THAT TRAFFIC IN SIGHT & TURN TO HEADING 240. GLANCED DOWN AT THE GEAR HANDLE & OBSERVED THE RED LIGHT IN THE HANDLE WAS ILLUMINATED. WITH THE HANDLE IN THE UP POSITION, OBSERVED THE LT MLG WAS STILL EXTENDED. ATC CALLED & CLEARED ME TO CLIMB TO 15,000FT. TOUCHED DOWN, FELT A SHIMMY TYPE VIBRATION. SOMETHING WASN’T RIGHT SO PULLED BOTH FUEL CONDITION LEVERS TO FUEL CUTOFF. PULLED BOTH PROP LEVERS TO FEATHER. BY THEN, COULD FEEL THE REAR OF THE BELLY SCRAPING ON THE RNWY, KEPT THE NOSE UP AS LONG AS COULD. FLEW THE NOSE WHEEL TO THE GND, ALL 3 GEARS HAD COLLAPSED. THE ACFT IMMEDIATELY BEGAN TO VEER TO THE LEFT OF THE RNWY CENTERLINE, NO STEERING CONTROL VIA THE RUDDER, THE ACFT BEGAN TO EXIT THE RNWY INTO THE GRASS. THE ACFT CAME TO A COMPLETE & ABRUPT STOP WITH EVERYTHING FWD OF THE WING ROOT IN THE GRASS. THE MAIN CABIN DOOR AREA WAS STILL ON THE ASPHALT. WE COULD SMELL TIRE SMOKE, BUT THERE WAS NO INDICATION OF A FIRE.

Source: SDR ZP7A20160315001 · FAA SDRS
O · 2013-02-23 Matched by certificate designator
ATA 3243

BRAKES ON CAPTAINS SIDE DID NOT OPERATE PROPERLY AFTER LANDING. CO-PILOT TOOK OVER BRAKING AND STEERING AND TAXIED SAFELY TO THE RAMP. MAINTENANCE INSPECTED THE BRAKE SYSTEM AND FOUND THE CAPTAINS NR 1 BRAKE CYLINDER TO BE LEAKING AND THE NR 2 BRAKE MASTER CYLINDER FAILED. AIRCRAFT IS STILL IN MAINTENANCE, THE BRAKE MASTER CYLINDERS AT FAULT ARE CURRENTLY BEING REPLACED.

Source: SDR ZP7A20130223001 · FAA SDRS