N116AX

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
ALASKA CENTRAL EXPRESS INC (YADA)Operator2013-03-08 – 2013-03-08Operator named in NTSB report

Accident & incident history

Acc · 2013-03-08 Operator named in NTSB report
BEECH 1900C Fatal injury Part 135ALASKA CENTRAL EXPRESS INC
Source: NTSB case ANC13FA030

Maintenance disclosures

F · 2013-01-11 Matched by certificate designator
ATA 3230

CREW ON FLT 145, DISCOVERED ON APPROACH THAT THE AIRPLANE LANDING GEAR WOULD NOT EXTEND. TOWER WAS NOTIFIED. INITIATED MANUAL GEAR EXTENSION PROCEDURES, WHICH WERE SUCCESSFUL. LANDED WITHOUT INCIDENT. MX FOUND THE 60 AMP LANDING GEAR CIRCUIT BREAKER IN LT NACELLE TRIPPED. THE GEAR WAS RETRACTED AND EXTENDED SEVERAL TIMES BUT THE DEFECT COULD NOT BE DUPLICATED. AN OPS CHECK FLIGHT WAS CONDUCTED SUCCESSFULY WITH NO REOCCURRANCE OF THE LANDING GEAR ISSUE. RELEASED BACK TO SERVICE.

Source: SDR YADA2013F00016 · FAA SDRS
N F · 2012-10-10 Matched by certificate designator
ATA 2841

ON DEPARTURE, PILOT EXPERIENCED A FUEL IMBALANCE THAT REQUIRED FULL AILERON TRIM TO CORRECT. ACFT RETURNED TO BASE, MX DETERMINED 1 FUEL QUANTITY INDICATOR WAS INDICATING INCORRECT FUEL QUANTITY. THE FUEL TANKS WERE SUMPED AND THE FAULTY GUAGE THEN INDICATED CORRECTLY. THE FUEL TANKS WERE TOPPED OFF AND THE GUAGES AGAIN CHECKED FOR PROPER INDICATION. THE ACFT WAS THEN RETURNED TO SERVICE.

Source: SDR YADA2012F00188 · FAA SDRS
O · 2012-07-30 Matched by certificate designator
ATA 5610

ON CLIMBOUT, PASSING THROUGH 500 FT, THE OUTER PLY OF THE PILOT'S WINDSHIELD CRACKED FROM TOP TO BOTTOM. LANDED WITHOUT INCIDENT. THE WINDSHIELD WAS REPLACED BY MX.

Source: SDR YADA2012F00156 · FAA SDRS
N · 2011-11-07 Matched by certificate designator
ATA 3297

ON TAKEOFF ROLL, THE LANDING GEAR "IN TRANSIT" LIGHT ILLUMINATED. THE CREW ABORTED THE TAKEOFF AND TAXIED BACK TO THE HANGAR. THE LIGHT REMAINED ILLUMINATED UNTIL THE LT ENGINE WAS SHUTDOWN. MX DISCOVERED THAT A WIRE HAD COME LOOSE FROM A LANDING GEAR WARNING CIRCUIT BREAKER. THOUGH THE CIRCUIT BREAKER APPEARED TO BE FUNCTIONAL IT WAS REPLACED AS A PRECAUTIONARY MEASURE. THE LANDING GEAR WARNING SYS CHECKED GOOD THROUGH SUBSEQUENT GEAR SWINGS AND AN OPS CHECK FLIGHT.

Source: SDR YADA2011110700001 · FAA SDRS
F · 2011-06-03 Matched by certificate designator
ATA 3416

PILOT REPORTED HIS ENCODING ALTIMETER WAS INOPERATIVE ON TAKEOFF. THIS SITUATION ALSO RENDERED THE ALTITUDE ALERTER AND TRANSPONDER MODE C INOPERATIVE. EXCESS FUEL WAS BURNED OFF AND THE ACFT RETURNED TO BASE. MX REPLACED THE PILOT'S ENCODING ALTIMETER, PERFORMED A SYS LEAK CHECK, AND RECERTIFIED THE TRANSPONDER SYS. ACFT WAS THEN RELEASED FOR SERVICE.

Source: SDR YADA060311001 · FAA SDRS
O · 2010-10-18 Matched by certificate designator
ATA 5520

2 MINUTES OUT OF LANDING,THE PILOT REPORTED (ON LANDING) THAT HE HAD TAKEN A LIGHTNING STRIKE TO THE NOSE OF THE ACFT. INSP OF THE ACFT REVEALED THAT THE TIP OF THE RT ELEVATOR HAD "BLOWN UP". A MECHANIC HAS BEEN DISPATCHED TO THE SCENE WITH AN ELEVATOR AND WILL FURTHER INVESTIGATE FOR MORE DAMAGE.

Source: SDR YADA1018201000002 · FAA SDRS
J · 2010-10-07 Matched by certificate designator
ATA 3243

ON LANDING, LT BRAKES LOCKED UP. PILOT STATED THAT AFTER LANDING THE LT BRAKES ACTIVATED WITHOUT INPUT FROM EITHER CREW MEMBER. THE DEGREE OF BRAKING ACTION WAS SLIGHT INITIALLY BUT BUILT AS TAXI PROGRESSED TO THE POINT THAT THE ACFT COULD NOT BE TAXIED AFTER DEPARTING THE RUNWAY. MX WAS DISPATCHED TO THE SCENE AND FOUND THE BRAKES TO BE FREE AND OPERATING NORMALLY. ACFT WAS THEN TOWED TO THE HANGAR WITHOUT FURTHER INCIDENT. MX WAS UNABLE TO FIND ANY ISSUES WITH THE ACFT WHEELS/BRAKE SYS AND WAS UNABLE TO DUPLICATE THE PROBLEM. A CHECK INTO THE ACFT HISTORY REVEALED THAT 5 DAYS PRIOR THERE WAS AN OCCURANCE ON THE RAMP IN WHICH A PILOT REPORTED "LITTLE" BRAKING ACTION ON THE LT SIDE. AT THAT TIME THE BRAKE SYSTEM WAS BLED AND OPERATED NORMALLY. FURTHER OPS CHECKS PRODUCED INCONSISTENT BRAKING ACTION FROM THE PILOTS LT PEDAL. THE LT BRAKE MASTER CYLINDER WAS CHANGED AND THE SYSTEM OPERATIONALLY CHECKED NORMAL.

Source: SDR YAD2010F00000 · FAA SDRS