N118SF

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

Inc · 2008-02-18 Unresolved
Hawker Beechcraft Corp. 99 None injury Part 135operator not yet resolved
Source: NTSB case CHI08IA085

Maintenance disclosures

N · 2009-11-27 Matched by certificate designator
ATA 3297

ON APPROACH, NO NOSE GEAR DOWN LOCK LIGHT. PILOT CHECKED THE DOWN POSITION BY OPERATING HANDPUMP. LANDED WITHOUT INCIDENT. MECHANIC CALLED OUT, WIRE FROM THE DOWNLOCK SWITCH (PN 1CH25) WAS FOUND TO BE BROKEN. WIRE WAS REPAIRED, SYS OPS CHECK WAS OKAY. PLANE DEPARTED THE FOLLOWING DAY WITHOUT FURTHER INCIDENT.

Source: SDR JDWA118SF2 · FAA SDRS
R · 2009-01-26 Matched by certificate designator
ATA 6120

ON CLIMB OUT, LEFT PROPELLER RPM DROPPED FROM 2200 TO 1900 RPM. PILOT TOOK NOTE AND CALLED IN FOR RETURN. MAINTENANCE HAS NOT DETERMINED THE CAUSE AT THIS POINT, TROUBLE SHOOTING IS CURRENTLY IN PROGRESS, SUSPECTING EITHER PROP GOV OR OVERSPEED GOV.

Source: SDR JDWA118SF1 · FAA SDRS
B · 2008-02-18 Matched by certificate designator
ATA 2400

ON MONDAY THE 18TH OF FEBRUARY 2008, BEECH 99, N118SF, S/N U-32, SUBURBAN AIR FREIGHT POSITIONING FLIGHT, ROUTE NUMBER SUBAIR 13 OPERATING UNDER PART 91, DEPARTED OMAHA, NE EN ROUTE TO MOLINE, IL. AT APPROXIMATELY 20:30 HOURS JUST NORTH OF MUSCATINE, IA CENTER CLEARED THE FLIGHT FOR DESCENT OUT OF 9000 FT. PASSING THRU 8000 FT, THE PILOT SMELLED SMOKE AND AT THAT TIME THE PILOT NOTICED A GLOW COMING FROM INSIDE OF THE CENTER CONTROL COLUMN AND NOTICED A REFLECTION ON THE TOE OF HIS RIGHT SHOE. THE PILOT SHUT DOWN THE ELECTRICAL SYSTEMS AND PROCEEDED TO GET THE FIRE EXTINGUISHER OUT. FIRE EXTINGUISHER WAS NOT USED, AS THE GLOW AND THE SMOKE STOPPED. DECLARED AN EMERGENCY AND CONTINUED TO MOLINE, LANDED WITHOUT FURTHER PROBLEMS.

Source: SDR JDWA2008SAF01 · FAA SDRS
O · 1998-12-22 Unresolved
ATA 5512

DURING A ROUTINE INSPECTION, CRACKS WERE DISCOVERED IN THE TOP SKIN AND RIB AT STA 76 OF THE LEFT HORIZONTAL STABILIZER. THE CRACK RAN FOR SEVERAL INCHES FORWARD AND AFT OF THE FORWARD J-CHANNEL. SI NR 0131-130, HAD BEEN PREVIOUSLY CW. SUBMITTER STATED POSSIBLE CAUSE AS VIBRATION DUE TO SLIP STREAM.

Source: SDR 99ZZZX556 · FAA SDRS
O · 1998-12-22 Unresolved
ATA 5512

DURING A ROUTINE INSPECTION, CRACKS WERE DISCOVERED IN THE TOP SKIN OF THE LEFT HORIZONTAL STABILIZER BEGINNING UNDER THE DE-ICE BOOT TRAVELING AFT ALONG THE ROW OF RIVETS AT STA 87 TO THE FORWRD J-CHANNEL. SI NR 0131-130 HAD BEEN PREVIOUSLY C/W. SUBMITTER SUGGESTED POSSIBLE CAUSE AS VIBRATION DUE TO SLIP STREAM.

Source: SDR 99ZZZX557 · FAA SDRS
J · 1998-04-06 Matched by certificate designator
ATA 3231

PIC REPORTED THE INABILITY TO EXTEND THE LANDING GEAR ELECTRICALLY, WITH A LOUD BANG NOTED IMMEDIATELY UPON EXTENSION. THE LANDING GEAR WAS EXTENDED MANUALLY, AND THE AIRCRAFT LANDED WITHOUT FURTHER INCIDENT. SUBSEQUENT INVESTIGATION DISCLOSED A TRIPPED LANDING GEAR CIRCUIT BREAKER, AND A BENT RT OUTBOARD MLG DOOR ACTUATING CAM. THE GEAR DOOR ROLLER ASSY STRUCK THE UNDERSIDE OF THE LANDING GEAR ACTUATING CAM CAUSING THE GEAR TO BIND IN THE WHEEL WELL. INVESTIGATION FAILED TO DETERMINE A CAUSE. THE CAM ASSY MAY HAVE BEEN MIS-RIGGED, OR FAILED TO SNAP OVERCENTER DUE TO WEAK RETURN SPRINGS.

Source: SDR 98ZZZX1689 · FAA SDRS