N119RM

CESSNA 750 · 1998 · Valid Registration

Registered owner: BALD 3 LLC, TX (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
HERA FLIGHT, LLC (5JHA)Certificate holderMatched by certificate designator
HERA FLIGHT, LLC (5JHA)Operator2026-05-09 – 2026-05-09Operator named in NTSB report

Accident & incident history

Acc · 2026-05-09 Operator named in NTSB report
CESSNA 750 None injury Part 91HERA FLIGHT, LLC Not yet finalized — may be revised.
Source: NTSB case ERA26LA206

Maintenance disclosures

N · 2025-03-07 Matched by certificate designator
ATA 2613

THE LH AND RH HYDRAULIC TEMP SENSORS GIVE FALSE INDICATIONS. WE HAVE REPLACED 5 SENSORS IN THE LAST FEW YEARS AND THE LATEST ONE THAT IS BRAND NEW FAILED AFTER TWO WEEKS IN SERVICE.

Source: SDR 5JHA2025030700160 · FAA SDRS
J · 2022-08-20 Matched by certificate designator
ATA 5300

ON TAKEOFF THE CREW SAW THE MAIN CABIN DOOR CAS MESSAGE ILLUMINATE AS WELL AS THE CABIN VENT DOOR CAS MESSAGE. BOTH CAME ON AT 11,000 FEET WHILE DEPARTING ASPEN. THEY RETURNED TO ASPEN AND LANDED WITHOUT INCIDENT. MAINTENANCE FOUND THE INTERIOR CABIN DOOR HANDLE LOOSE. IT WAS TIGHTENED AND OPS CHECK GOOD.

Source: SDR 2022F00334 · FAA SDRS
L · 2018-07-15 Matched by certificate designator
ATA 2720

DURING FLIGHT CONTROL CHECKS, PRIOR TO FLIGHT, IT WAS DISCOVERED THAT THE UPPER RUDDER CHANNEL B FAILED THE PRE-FLIGHT CHECKS. THE UPPER RUDDER POSITION WOULD STAY FULLY DEFLECTED UNTIL RESET. THE MAINTENANCE FOUND THE CHANNEL B RUDDER POSITION SENSOR DEFECTIVE. THE SENSOR WAS REPLACED AND OPS AND TRAVEL CHECKS WERE NORMAL.

Source: SDR 9JLA2018080919551 · FAA SDRS
K · 2018-04-23 Matched by certificate designator
ATA 2910

DURING POST FLIGHT INSPECTIONS, THE RT THRUST REVERSER PRESSURE HYDRAULIC LINE WAS FOUND TO BE CHAFED BY NEARBY B-NUT CAUSING A HYDRAULIC LEAK. . THE LOCATION OF THE CHAFED HYDRAULIC LINE WAS WITHIN THE AFT MAINTENANCE BAY ON THE RT SIDE OF THE COMPARTMENT JUST ABOVE AND AFT OF THE WATER SEPARATOR. THE B-NUT WAS LOCATED AFT OF A CHECK-VALVE THE CHAFED HYDRAULIC LINE ROUTES VERTICALLY AFT OF THE WATER SEPARATOR. THE AREA CHAFED IS NOT READILY SEEN AND COULD BE MISSED DURING VISUAL INSPECTION. THE HYD LINE WAS REPLACED AND ADJUSTMENTS WERE MADE TO ACHIEVE CLEARANCE.

Source: SDR 9JLA2018042711498 · FAA SDRS
K B · 2018-02-15 Matched by certificate designator
ATA 2150

WHILE WAITING FOR PASSENGERS WITH THE APU RUNNING AND THE AIR CONDITIONING OPERATING, THE CREW REPORTED THAT VISIBLE SMOKE WAS SEEN IN THE COCKPIT WITH THE ODORS OF SOMETHING GETTING HOT, WERE UNABLE TO CONTROL THE COCKPIT TEMP. THE CREW SHUTOFF THE COCKPIT AIR CONDITIONING PACK AND THE ODOR AND SMOKE DISSIPATED. TROUBLESHOOTING DETERMINED THAT THE COCKPIT AIR CONDITIONING PACK OIL SEALS FAILED ALLOWING THE AC PACK OIL TO BYPASS. THE PACK WAS REPLACED WITH A NEW UNIT. OPS CHECKED SATISFACTORY. THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2018021911496 · FAA SDRS