N127AM

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AIR METHODS LLC (QMLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2020-07-06 Matched by certificate designator
ATA 5313

DURING INSPECTION A .500" CRACK WAS FOUND IN THE STRINGER.

Source: SDR QMLA2020070620032 · FAA SDRS
K J · 2017-11-26 Matched by certificate designator
ATA 6320

AFTER TAKEOFF, NOTICED MAIN GEARBOX OIL PRESSURE DROPPING BUT INITIALLY STAYING IN ACCEPTABLE RANGE WITH NO SIGNIFICANT INCREASE IN TEMPERATURE. FLIGHT CONTINUED FOR A FEW MINUTES AND THEN PRESSURE DROPPED TO WARNING INDICATION LEVEL. EXECUTED AN UNSHEDULED LANDING WITHOUT INCIDENT. FOUND A LOSE OIL LINE AT THE TRNSMISSION OIL COOLER ASSY, INSPECTED LINE FOR DAMAGE, NONE FOUND. SECURED, TORQUED THE OIL LINE, SERVICED THE TRANSMISSION, PERFORMED A SERVICABILITY CHECK, GROUND RUN FOR 1 HOUR IAW MM WITH NO ABNORMAL INDICATIONS AND RETURNED THE AIRCRAFT TO SERVICE.

Source: SDR QMLA2017112617131 · FAA SDRS
K B · 2017-08-03 Matched by certificate designator
ATA 2810

ON REMOVAL OF LOWER FUEL CELL INSPECTION PANELS, DISCOVERED THE LOWER RT FUEL CELL WAS LEAKING FUEL AT THE FWD AND AFT FUEL PROBE PANELS. FUEL PROBE PANELS ARE DELAMINATING FROM THE MAIN FUEL CELL.

Source: SDR QMLA2017080317076 · FAA SDRS
M J · 2017-07-23 Matched by certificate designator
ATA 7922

AFTER TAKE OFF DURING CLIMB OUT, THE NR 2 ENGINE OIL TEMP. ROSE TO 120 DEGREES. AND A HIGH OIL TEMP CAUTION LIGHT ILLUMINATED. PILOT STARTED DESCENT AND AFTER LANDING SHUT ENGINE DOWN AND TAXIED TO PARKING LOCATION WITH NO FURTHER DIFFICULTY.

Source: SDR QMLA2017072317070 · FAA SDRS
J · 2017-06-02 Matched by certificate designator
ATA 3230

AFTER DEPARTURE, ON A TRAINING FLIGHT, RAISED THE GEAR AND GOT A RED GEAR UNSAFE INDICATION, ESTABLISHED A STEADY CRUISE AT 80KIAS AND CHECKED INDICATIONS AND HYDRAULIC SYSTEM PRESSURE. NORM UTILITY PRESSURE INDICATED RED AT 474 PSI NOT CHARGING. ALL OTHER HYDRAULIC PRESSURES WERE IN THE GREEN. AFTER CYCLING THE GEAR A FEW TIMES WITH NO CHANGE IN PRESSURES OR GEAR INDICATION, CONSULTED THE EMERGENCY CHECKLIST AND EXECUTED THE EMERGENCY LOWER GEAR PROCEDURE. UPON ACTIVATION OF THE EMERGENCY DOWN SYSTEM I GOT A 3 GREEN INDICATIONS. HEADED BACK TO MHV AND HAD AN UNEVENTFUL LANDING. NOTICED THAT THE AFTER BLOWING DOWN THE GEAR, THE UTILITY SYSTEM STARTED CHARGING AGAIN AND THE NORM UTILITY PRESSURE WAS IN THE GREEN AT 1350 PSI AT LANDING.

Source: SDR QMLA2017060217056 · FAA SDRS
J · 2017-05-29 Matched by certificate designator
ATA 3222

PILOT INDICATED HIGH OIL TEMP RED LIGHT CAUTION IN CRUISE FLIGHT, OTHER INDICATIONS IN THE GREEN. PERFORMED PRECAUTIONARY LANDING. PILOT AND CREW INDICATED 3 GREEN SAFE LANDING GEAR INDICATION. NOSE LANDING GEAR COLLAPSED WHILE TOUCHING DOWN. RT MAIN GEAR PARTIALLY EXTENDED. NO ATTEMPT MADE TO UTILIZE EMERGENCY DOWN CONTROL FOR MAIN LANDING GEAR.

Source: SDR QMLA2017052917053 · FAA SDRS
K B · 2017-05-08 Matched by certificate designator
ATA 2810

IN FLIGHT CREW REPORTED AN ODOR OF FUEL THROUGHOUT THE CABIN. AIRCRAFT WAS INSPECTED AND FOUND THAT THE LT FORWARD FUEL CELL HAD A SMALL PIN HOLE SIZE LEAK AROUND THE FORWARD FUEL QUANTITY PROBE MOUNT FLANGE RUBBER SEAM. THE RT FORWARD FUEL CELL APPEARS DRY HOWEVER IT HAS A LINE ACROSS THE AFT PORTION THAT COULD HAVE BEEN CAUSED BY SEAPAGE THROUGH THE RUBBERIZED FABRIC AT SOME POINT AND IS SUSPECT TO FUTURE FAILURE. THE LT FUEL CELL HAD BEEN RECENTLY REPLACED.

Source: SDR QMLA2017050817050 · FAA SDRS
B · 2017-04-27 Matched by certificate designator
ATA 2120

APPROXIMATELY 15 MINUTES INTO FLIGHT CREW REPORTED AN ODOR OF FUEL THROUGHOUT THE CABIN. AIRCRAFT WAS RETURNED TO BASE.

Source: SDR QMLA2017042717044 · FAA SDRS
O · 2015-07-31 Matched by certificate designator
ATA 7921

DISCOVERED DURING A SCHEDULED MAINTENANCE EVENT THE FOLLOWING DISCREPANCY. WHILE PERFORMING BULLETIN 109EP-1222 & AMC EO-06-6322-EO-452, 200 HOUR INSPECTION OF RIGHT SIDE OIL COOLER BLOWER FAN IMPELLER PLAY MEASUREMENT, HE FOUND THE PULLEY TO BE SLIPPING ON IMPELLER SHAFT. UPON FURTHER DISASSEMBLY, THERE WAS REVEALED A SHEARED SHAFT WHERE THE PULLEY CONNECTS TO THE IMPELLER SHAFT. THIS AIRCRAFT REMAINS OUT OF SERVICE AT THE TIME OF THIS SUBMISSION AWAITING PARTS.

Source: SDR QMLA2015073115064 · FAA SDRS
O · 1998-11-16 Matched by certificate designator
ATA 5411

DURING C-CHECK INSPECTION, NR 1 FRAME ON LEFT AND RIGHT ENGINE NACELLES WERE FOUND TO HAVE CRACKS INBOARD AND OUTBOARD OF MOUNT HOLES FOR LEFT AND RIGHT SIDE OF ENGINE FORWARD TORQUE MOUNT. REMOVED AND REPLACED NR 1 FRAME ON LEFT AND RIGHT ENGINE NACELLES. (M)

Source: SDR ASOA98102 · FAA SDRS
O · 1998-11-16 Matched by certificate designator
ATA 5411

FLUORESCENT PENETRANT INSPECTION INDICATED CRACKS IN RT ENGINE FORWARD NACELLE NR 1 FRAME. SUBMITTER STATED SEEMED TO BE A REPETITIVE DISCREPANCY AS PREVIOUSLY DETAILED AND REPORTED AND POSSIBLE CAUSE IS STILL UNDETERMINED. WOULD SUSPECT ENGINE TORQUE AND VIBRATION AS POSSIBLE CONTRIBUTING FACTORS. WOULD SUGGEST TIMED INTERVALS FOR REPETITIVE INSPECTION OF AREA.

Source: SDR 98ZZZX4708 · FAA SDRS
O · 1998-11-16 Matched by certificate designator
ATA 5320

LEFT VERTICAL STABILIZER CHINE ANGLE IS CRACKED .250 INCH BY .010 AND HAS WORKING RIVETS. SUBMITTER SUGGESTED CAUSE AS FATIGUE/VIBRATION AND RECOMMENDED A DETAILED INSPECTION BE CALLED OUT DURING C-CHECK INSPECTION.

Source: SDR 98ZZZX4706 · FAA SDRS
O · 1998-11-16 Matched by certificate designator
ATA 5411

FLUORESCENT PENETRANT INSPECTION INDICATED CRACKS IN LT ENGINE FORWARD NACELLE NR 1 FRAME. SEEMS TO BE A REPETITIVE DISCREPANCY AS PREVIOUSLY DETAILED AND REPORTED. SUBMITTER STATED CAUSE IS STILL UNDETERMINED. WOULD SUSPECT ENGINE TORQUE AND VIBRATION TO BE POSSIBLE CONTRIBUTING FACTORS AND SUGGEST TIMED INTERVALS FOR REPETITIVE INSPECTION OF AREA.

Source: SDR 98ZZZX4704 · FAA SDRS
O · 1998-11-16 Matched by certificate designator
ATA 5320

RIGHT VERTICAL STABILIZER CHINE ANGLE IS CRACKED .250 INCH BY .010 INCH AND HAS WORKING RIVETS. SUBMITTER SUGGESTED POSSIBLE CAUSE AS FATIGUE/VIBRATION AND RECOMMENDED A DETAILED INSPECTION BE CALLED OUT DURING C-CHECK INSPECTION.

Source: SDR 98ZZZX4705 · FAA SDRS
O · 1998-11-16 Matched by certificate designator
ATA 5320

DURING C-CHECK INSPECTION, CORROSION WAS DISCOVERED BETWEEN FUSELAGE FRAMES 13A AND 15A, FS 4214.0 TO FS 4992.0 ON LOWER PASSENGER/CREW ENTRANCE DOOR SURROUNDING STRUCTURE ANGLE. SUBMITTER SUGGESTED POSSIBLE CAUSE AS MOISTURE PENETRATION.

Source: SDR 98ZZZX4707 · FAA SDRS
O · 1996-08-29 Matched by certificate designator
ATA 5230

FLT 7268 - ROA-ATL - DURING CRUISE FLIGHT AT 20,000 FEET, CABIN PRESSURIZATION STARTED TO CLIMB. CREW ELECTED TO MAKE AN EMERGENCY DESCENT TO 10,000 FEET AND CONTINUE TO ATL, WHERE LANDING WAS MADE SAFELY AND WITHOUT INCIDENT. REMOVED AND REPLACED CARGO DOOR SEAL. OPERATIONAL AND LEAK CHECKS WERE GOOD AND AIRCRAFT WAS RELEASED FOR FURTHER SERVICE. (M)

Source: SDR ASOA96033 · FAA SDRS
J · 1996-05-23 Matched by certificate designator
ATA 7320

LEVELING OFF AT 2000 FEET DEPARTING DFW, LEFT ENGINE SURGED SLIGHTLY AND SHUTDOWN COMPLETELY WITH AUTOFEATHER. NO LIMITATIONS WERE EXCEEDED. AN EMERGENCY WAS DECLARED AND THE AIRCRAFT RETURNED TO DFW WHERE A LANDING WAS MADE WITHOUT INCIDENT. UPON INSPECTION FOUND P3 LINE BROKEN AT LEFT ENGINE OVERSPEED GOVERNOR. REPLACED P3 LINE AT HMU TO OVERSPEED GOVERNOR. OPS CHECKS GOOD ON GROUND RUN-UP. AIRCRAFT RELEASED FOR SERVICE. (M)

Source: SDR ASOA96016 · FAA SDRS
L · 1995-07-25 Matched by certificate designator
ATA 3350

STL - EMERGENCY PATH LIGHTING DOES NOT TEST LIGHTS INOP. MAINTENANCE REPLACED FWD EMERGENCY BATTERY PACK. (M)

Source: SDR RAIA950743 · FAA SDRS
N · 1995-07-10 Matched by certificate designator
ATA 3150

STL - FLT 7452 - TRIM WARNING SOUNDED ON TAKEOFF. MAINTENANCE RESET AURAL WARNING CIRCUIT BREAKER. SYSTEM CHECK GOOD. (X)

Source: SDR RAIA950706 · FAA SDRS
N · 1995-03-19 Matched by certificate designator
ATA 3260

MSN - FLT 7171 - RT MAIN INTRANSIT LIGHTS ON BOTH CHANNELS WOULD NOT EXTINGUISH WHEN GEAR WAS SELECTED UP. MAINTENANCE CLEANED UPLOCK SENSOR BOX AND ADJUSTED RT MAIN GEAR UPLOCK SENSOR STRIKER ARM. GEAR SWINGS REVEALED NORMAL. (X)

Source: SDR RAIA950330 · FAA SDRS
B · 1995-03-14 Matched by certificate designator
ATA 2150

STL - FLT 7151 - NORMAL FLIGHT LEFT PACK SMELLS BAD. MAINTENANCE REPAIRED LEFT RAM AIR DOOR. GROUND TEST OF LEFT PACK REVEALED NORMAL OPERATION AND NOTED NO SMELL. (X)

Source: SDR RAIA950322 · FAA SDRS
B · 1995-02-17 Matched by certificate designator
ATA 4950

STL - APU HAS SMOKE COMING FROM COMPARTMENT AND BLEED LINE UNDER BELLY. MAINTENANCE REPLACED DUCT SECTION UNDER BELLY. GROUND RUNS REVEALED NORMAL. (Z)

Source: SDR RAIA950226 · FAA SDRS
O · 1995-02-17 Matched by certificate designator
ATA 3454

STL - FLT 7458 - PILOT REPORTED BOTH VORS WILL NOT RECEIVE. MAINTENANCE REPAIRED COAX CONNECTOR TO ANTENNA PHASE COUPLER. SYSTEM CHECK OK. (Z)

Source: SDR RAIA950228 · FAA SDRS
L · 1995-02-14 Matched by certificate designator
ATA 3350

STL - SEVERAL AFT EMERGENCY LIGHTS ARE INOP. MAINTENANCE REPLACED AFT EMERGENCY LIGHTING BATTERY. (Z)

Source: SDR RAIA950224 · FAA SDRS