N130UE

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

Accident · 1995-03-05 Unresolved
Beech 1900 None injuryoperator not yet resolved
Source: NTSB case CHI95LA094

Maintenance disclosures

R · 2018-04-17 Matched by certificate designator
ATA 7321

DURING APPROACH, THE NR 1 POWER OUTPUT REDUCED AND WOULD NOT RESPOND TO INPUT. THE ENGINE WAS SHUT DOWN AND AIRCRAFT LANDED WITHOUT INCIDENT. TROUBLESHOOTING REVEALED NO DAMAGED P3 OR PY LINES. REPLACED FUEL CONTROL UNIT.

Source: SDR JDWA201804190001 · FAA SDRS
P · 1997-09-01 Unresolved
ATA 3260

GRI - NOSE GEAR DOWNLOCK LIGHT FAILED TO ILLUMINATE AFTER SELECTING GEAR DOWN. REPLACED NOSE GEAR DOWN AND LOCK SWITCH. (M)

Source: SDR GLBA97137 · FAA SDRS
B · 1996-12-05 Unresolved
ATA 2121

FLO - WHITE SMOKE FILLED COCKPIT AND CABIN. TURNED OFF ENVIRONMENTAL VALVES. MAINTENANCE FOUND AFT VENT BLOWER INOPERATIVE. RAN AIRCRAFT WITH BLEEDS OPEN AND COULD NOT DUPLICATE AT THIS TIME. MEL'D BLOWERS AND LATER REPLACED AFT VENT BLOWER. (M)

Source: SDR GLBA96231 · FAA SDRS
N · 1996-05-24 Unresolved
ATA 3260

SPI - CREW REPORTED THAT GEAR POSITION LIGHTS REMAINED GREEN AFTER SELECTING GEAR UP. THEY MADE AN AIR TURN-BACK AND LANDED UNEVENTFULLY. MAINTENANCE REMOVED AND REPLACED 'DOWN AND LOCKED' ANNUNCIATOR ASSY. OPS CHECK WAS GOOD. (X)

Source: SDR GLBA96100 · FAA SDRS
J · 1996-04-18 Unresolved
ATA 2460

SPI - CREW REPORTED, LEFT GENERATOR ANNUNICATOR ILLUMINATED WHILE TAXIING AND THEY RETURNED TO GATE. MAINTENANCE REMOVED AND REPLACED BUS TIE CONTROL PRINTED CIRCUIT BOARD. OPS CHECK WAS GOOD. (M)

Source: SDR GLBA96074 · FAA SDRS
P · 1996-04-03 Unresolved
ATA 3233

SPI - CREW OBSERVED NOSE GEAR POSITION LIGHT WAS NOT ILLUMINATED WITH GEAR SELECTED DOWN. THEY MADE AN UNEVENTFUL LANDING. MAINTENANCE REMOVED AND REPLACED NOSE LANDING GEAR ACTUATOR. LEAK CHECK AND OPS CHECK WERE GOOD. (X)

Source: SDR GLBA96065 · FAA SDRS
O · 1996-01-02 Unresolved
ATA 7120

SPI - DURING VISUAL INSPECTION OF AREA 'A' AS REQUIRED BY AD 95-12-18, A CRACK WAS FOUND. THE RIGHT ENGINE TRUSS WAS REPLACED WITH SERVICEABLE.

Source: SDR 96ZZZX459 · FAA SDRS
C · 1995-03-05 Unresolved
ATA 6110

MSP - DURING TAXI TO THE TERMINAL, THE RT PROPELLER CONTACTED A RAMP BAGGAGE CART. THE PROPELLER WAS CHANGED AND AS A PRECAUTION, ENGINE AND TRUSS WERE CHANGED. SMALL REPAIRS WERE ACCOMPLISHED TO THE FUSELAGE SKIN IAW THE BEECH SRM.

Source: SDR 95ZZZX1961 · FAA SDRS
J · 1995-02-19 Unresolved
ATA 7532

MSP - ON APPROACH THE RT ENGINE STALLED, AFTER WHICH THE CREW SHUT DOWN AND SECURED THE ENGINE. AN UNEVENTFUL LANDING WAS ACCOMPLISHED. MAINTENANCE REPLACED THE COMPRESSOR BLEED VALVE. AFTER A SUCCESSFUL TEST FLIGHT, THE AIRCRAFT WAS RELEASED FROM MAINTENANCE.

Source: SDR 95ZZZX1956 · FAA SDRS
O · 1995-02-08 Unresolved
ATA 5311

SPW - DURING ROUTINE INSPECTION, MAINTENANCE FOUND THE FUSELAGE FRAME CRACKED AT THE POINT WHERE THE FIRST AIR DOOR SNUBBER BRACKET IS ATTACHED. REPAIRED FRAME IAW BEECH SRM 51-70-00, PAGE 52.

Source: SDR 95ZZZX1953 · FAA SDRS