N145HH

EUROCOPTER DEUTSCHLAND GMBH MBB-BK 117 C-2 · 2009 · Valid Registration

Registered owner: HARTFORD HOSPITAL, CT (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AIR METHODS LLC (QMLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

B · 2025-02-28 Matched by certificate designator
ATA 2120

CREWMEMBER REPORTED FUEL ODOR IN CABIN.MECHANIC INSPECTED AIRCRAFT FUSELAGE AND ENGINES FOR FUEL LEAKS. PERFORMED GROUND RUN AND WATCHED FOR ANY LEAKS. NO EVIDENCE OF FUEL LEAKS OR FUEL SMELL FOUND. AIRCRAFT RETURNED RO SERVICE AND THERE ARE NO COMPONENTS CAUSING DIFFUCULTY OR DAMAGED.

Source: SDR QMLA2025022820030 · FAA SDRS
J · 2023-12-02 Matched by certificate designator
ATA 6300

DURING RETURN FLIGHT FROM BAYSTATE HOSPITAL BACK TO BASE, WHILE OVER BRADLEY AIRPORT (KBDL) THE RIGHT-SIDE MAIN ROTOR TRANSMISSION PRESSURE INDICATION DROPPED TO 0. LANDING WAS PERFORMED AT KBDL MANAGEMENT, OCC, AND MAINT. WHERE THEN NOTIFIED.

Source: SDR QMLA2023120520111 · FAA SDRS
J R · 2017-07-10 Matched by certificate designator
ATA 7200

WHILE ENROUTE, AIRCRAFT HAD A VARNR LIGHT ILLUMINATE AND EXPERIENCED AN APPROXIMATE 30% ENGINE SPLIT WITH NR 2 ENGINE GOING LOW. AIRCRAFT VARTOM’S SYSTEM WENT INTO MANUAL MODE. PILOT ATTEMPTED TO BEEP UP THE NR 2 ENGINE WITH COLLECTIVE TRIM SWITCH WITH NEGATIVE RESULTS. COLLECTIVE TRIM SWITCH WOULD ONLY INCREASE THE NR 1 ENGINE, WHICH WAS ONLY DONE MOMENTARILY TO CHECK IF SWITCH WAS WORKING. THE NR 2 ENGINE WOULD NOT RESPOND TO COLLECTIVE TRIM SWITCH. ELECTED TO DO A RUN ON LANDING AS A PRECAUTION IN ORDER TO NOT EXCEED ANY LIMITATIONS ON THE NR 1 ENGINE. NO DAMAGE TO AIRCRAFT AND NO LIMITATIONS EXCEEDED.

Source: SDR QMLA2017071017065 · FAA SDRS
B · 2015-10-15 Matched by certificate designator
ATA 7170

DURING TAKEOFF, THE CREW NOTICED A STRONG FUEL SMELL IN CABIN. FOUND THE COMMON DRAIN LINE ON THE NR 2 ENG DECK TO BE CLOGGED. THIS ALLOWED AN ACCUMULATION OF FUEL AFTER MULTIPLE STARTS, WHICH RESULTED IN THE FUEL SMELL IN THE CABIN. CLEANED DRAIN WITH AIR GND RUN. ACFT OPERATIONS CHECKED OK.

Source: SDR QMLA2015101515098 · FAA SDRS
K · 2014-04-29 Matched by certificate designator
ATA 6730

THE TAIL ROTOR ACTUATOR WAS FOUND SEEPING. THIS ACTUATOR WAS IN SERVICE FOR 146 HOURS, ABOUT THE AVERAGE TIME FOR REPLACEMENT EXPERIENCED AT THIS FACILITY WITH THIS ACFT. THE LEAKAGE RATE EXCEEDS THE LIMITS SPECIFIED IN THE MBB BK117C-2 AMM IAW CH 67-34-00, 6-1 F 3 C & F LEAKAGE RATES & CH 29-00-00, 5-1 TABLE 1.

Source: SDR QMLA2014042914045 · FAA SDRS
O · 2012-04-11 Matched by certificate designator
ATA 6220

BOLTS SECURING RINGS TO MAIN ROTOR HEAD INNER SLEEVES LOOSE.

Source: SDR QMLD2012041103961 · FAA SDRS