N160AM

BELL HELICOPTER TEXTRON CANADA 407 · 2010 · Valid Registration

Registered owner: AIR METHODS LLC, CO (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AIR METHODS LLC (QMLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

B · 2025-05-15 Matched by certificate designator
ATA 2121

DURING FLIGHT TO HOSPITAL MEDICAL CREW NOTIFIED THE PILOT THAT THEY SMELLED FUMES FROM AN ELECTRICAL SOURCE IN THE CABIN BUT DID NOT SEE ANY SMOKE. AN OFF-SITE LANDING WAS PERFORMED, AND MAINTENANCE NOTIFIED OF THE DISCREPANCY. PILOT REPORTED NO ODOR OR FUMES DETECTED UP FRONT. ON CALL AMTS INSPECTED CABIN ELECTRICAL OUTLETS, MEDICAL EQUIPMENT POWER CORDS AND AIRFRAME CABIN WIRING WITH NO DEFECTS NOTED. STRONG ODOR EMANATING FROM CABIN AIR CONDITIONING OUTLETS LED TO DISCOVERING THE AFT BLOWER MOTOR TO BE SOURCE. PULLED CB, SECURED AND PLACARDED AIR CONDITIONING SYSTEM AS INOP. AIRCRAFT RETURNED TO BASE.

Source: SDR QMLA2025051520055 · FAA SDRS
B · 2017-08-17 Matched by certificate designator
ATA 2121

ABOUT 12 MILES OUT FROM BASE, NOTICED AN ELECTRICAL BURNING ODOR AND SMOKE SLOWLY CREEPING INTO THE FRONT CABIN FROM THE REAR. SHUT OFF ALL ELECTRICAL SYSTEMS AND OPENED THE FRONT 2 WINDOWS FOR VENTILATION. LANDED THE AIRCRAFT .

Source: SDR QMLA 201708171708 · FAA SDRS
O · 1995-11-15 Matched by certificate designator
ATA 5753

RIGHT OUTBOARD FLAP, P/N 35165050259, HAS A CRACK APPROXIMATELY .75 INCH LONG ON THE TRAILING EDGE, ON THE UNDERSIDE, 12 INCHES FROM INBOARD END. REPAIRED WITH A DOUBLER. (M)

Source: SDR 95ZZZM703 · FAA SDRS
J · 1995-10-30 Matched by certificate designator
ATA 2460

DURING CRUISE FLIGHT, LT BUS TIE OPEN WARNING FOLLOWED BY LT DC GENERATOR FAIL WARNING. CAPTAIN LOST HEADSET AUDIO WHICH IS POWERED FROM LT GENERATOR BUS. THIS OCCURRENCE CAUSED LOSS OF COMMUNICATION BETWEEN COCKPIT CREW AT A TIME CREW COORDINATION IS CRITICAL. COMMUNICATION IS LOST DUE TO LOSS OF DC BUS POWER. SUBMITTER STATES BUS TIE PROTECT DEVICES TEND TO BE OVERLY SENSITIVE IN OPERATION.

Source: SDR 95ZZZX6596 · FAA SDRS
O · 1995-08-02 Matched by certificate designator
ATA 5753

DURING ROUTINE MAINTENANCE, A CRACK WAS FOUND 10 INCH FROM O/B EDGE 3.5 INCH FROM TRAILING EDGE. REPAIRED WITH PATCH 4 INCH BY 5 INCH. (M)

Source: SDR 95ZZZM478 · FAA SDRS
O · 1995-07-14 Matched by certificate designator
ATA 7250

LEFT ENGINE ITT ROSE ABOVE LIMITS MOMENTARILY. WHEN THE ENGINE WAS SEPARATED FROM THE POWER SECTION, DISCOVERED THE CT VANE RING HAD A SECTION COMPLETELY BURNED THROUGH. THE INVESTIGATION IS LOOKING AT THE FUEL NOZZLES AS A POSSIBLE CAUSE. THE FUEL NOZZLES ARE CHANGED OUT AT 480.0 HOURS

Source: SDR 96ZZZX4 · FAA SDRS
O · 1995-05-24 Matched by certificate designator
ATA 5753

DURING SCHEDULED MAINTENANCE, A .875 INCH CRACK WAS FOUND 15 INCHES FROM OUTBOARD EDGE AND 6 INCHES FROM TRAILING EDGE OF RIGHT INBOARD FLAP. STOPPED DRILLED AND INSTALLED DOUBLER.

Source: SDR 95ZZZM201 · FAA SDRS
O · 1995-05-03 Matched by certificate designator
ATA 5753

DURING ROUTINE MAINTENANCE A CRACK 1 INCH WAS FOUND ON TRAILING EDGE SKIN APPROXIMATELY 1 FOOT INBOARD OF END CAP. ON TE FLAP (P/N 3516505259). STOP DRILLED AND INSTALLED DOUBLER. (M)

Source: SDR 95ZZZM20 · FAA SDRS
J · 1995-04-13 Matched by certificate designator
ATA 6120

FLT 5630 - AFTER TAKEOFF LEFT TORQUE AND PROP RPM INDICATION FLUCTUATED. FOUND BETA CABLE LOOSE, TIGHTENED CABLE, RERIGGED LEFT ENGINE. OPS CHECK NORMAL. (M)

Source: SDR 95ZZZM16 · FAA SDRS
O · 1995-03-01 Matched by certificate designator
ATA 5753

ON SCHEDULED MAINTENANCE, A SMALL CRACK INBD END CAP, WAS FOUND 4 INCHES UP FROM T/E ON TOP OF FLAP. REPAIRED WITH PATCH.

Source: SDR 95ZZZX1968 · FAA SDRS