N1SH

RAYTHEON AIRCRAFT COMPANY 390 · Valid Registration

Registered owner: LUX 11 HOLDINGS LLC, TX (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
ELDORADO AIR, LLC (QZJA)Certificate holderMatched by certificate designator

Accident & incident history

Accident · 1976-09-04 Unresolved
PIAGGO 136-L2 Serious injuryoperator not yet resolved
Source: NTSB case NYC76FFJ31

Maintenance disclosures

J · 2021-03-08 Matched by certificate designator
ATA 7500

UPON DEPARTURE, THE CREW NOTICED THE FOLLOWING MECHANICAL IRREGULARITY: “UNSCHEDULED BLEED AIR AS AIRCRAFT ROTATED OFF RUNWAY. PRESSURIZATION CONTROLLER INDICATED -1,400 FPM. ATTEMPTED TO STOP HOT AIR BY TURNING OFF PRESSURIZATION AND BLEED AIR. DID NOT SOLVE ISSUE. ONLY WAY TO STOP BLEED AIR FROM RUSHING IN WAS TO REDUCE THRUST.” THE CREW NOTIFIED ATC AND THEN PROMPTLY DIVERTED TO NEARBY MATHER AIRPORT. AFTER AIRCRAFT SHUTDOWN AT MATHER, THE CREW NOTIFIED COMPANY PERSONNEL /IMMEDIATELY COMPLETED AN ELDORADO AIR LLC DISCREPANCY LOG EA-FORM-102A PER THE ELDORADO AIR GOM “REPORTING MECHANICAL IRREGULARITIES” PROCEDURES IN SECTION F, F.1 AND GROUNDED THE AIRCRAFT.

Source: SDR QZJA20210308004 · FAA SDRS
J · 2020-11-17 Matched by certificate designator
ATA 7532

ON NOVEMBER 17, 2020 THE PILOT REPORTED: ABORTED THE TAKEOFF AT KABQ AT APPROXIMATELY 1712Z IN N1SH DUE TO A LOUD RUSHING OF AIR NOISE IN THE COCKPIT, FOLLOWED BY A LOT OF HOT AIR ENTERING THE COCKPIT. THIS HAPPENED AS THE THROTTLES WERE BROUGHT TO THEIR T/O POSITION. ELECTED TO ABORT THE T/O AS THIS WAS NOT A NORMAL CONDITION. UPON EXITING THE RUNWAY AND TAXIING, CYCLED THE THROTTLES AND RAN A PRESSURIZATION TEST AND BLEED AIR TEST AND ALL WAS NORMAL. ALL OTHER INDICATIONS WERE NORMAL. TAXIED BACK FOR ANOTHER TAKEOFF ATTEMPT WHICH WAS WITHOUT INCIDENT.

Source: SDR QZJA20201119002 · FAA SDRS